At The Repair Bench
Chris Prioli, AD2CS
A Monthly Column Describing A Recent Repair Bench Event
WWW.AD2CS.COM
MFJ-9987RT Remote Automatic Antenna Tuner
December 2025
|
Shortly before our 2025 HamFest, I received a communication from a gentleman located in Dover, Delaware who had some questions for me regarding his remote HF station and some problems he was currently experiencing. His system incorporates an Icom IC-7300, and MFJ-9987RT Auto-Tuner (Figure 1), and a BLA-350 linear amplifier. His problem was that the BLA-350 was dropping out on transmission due to a loss of input signal at the appropriate frequency. He described an earlier failure that he had attempted to repair. That failure was the annihilation of an RF hash choke at the signal input stage of the MFJ-998RT Auto-Tuner. After talking it through for a bit, we decided that the auto-tuner was the heart of his ongoing
|
difficulties, and that he should bring it to me for repairs. He did so after the HamFest on that rainy Sunday afternoon.
|
A brief description of the MFJ-998RT and its input circuit is called for here. Refer to the schematic excerpt at Figure 2 as you continue here. As the transmitted signal enters the auto-tuner, a sample of that signal is taken off at an input transformer (T1 in the schematic). It then passes through a 1mH RF hash choke. This choke is identified in the schematic as L41 and as being 1000µH, an equivalent value. Its location is clearly visible with the yellow oval on the photo in Figure 3 - the black cylinder
|
near the right of the oval. This is the choke that had been completely burned up in the failure event that started this odyssey. The owner, who is not a technician but who does try to make his own repairs, was told by another user online what the correct value of the choke should be, exactly what he should buy, and exactly where he should buy it. Unfortunately, that information was incorrect, as that user told the owner to purchase a 100µH choke when the schematic clearly calls for a value of 1000µH here. However, that was only a small part of the overall problem.
My initial overall physical exam of the unit revealed a small daughterboard, mounted to the mainboard in the vicinity of the input section, that showed some distinct charring. This board holds four resistors, and all of them exhibited signs of having been severely overheated. I decided that a closer look was called for here, so I removed the daughterboard for a better look at it, and I also identified it in the schematic.
According to the schematic, this board was serving as R121, stated to be a 25Ω 15W 1% resistor. According to the color code on the resistors, they were 100Ω each, which makes sense, as they were wired in parallel. Four 100Ω resistors in parallel would of course produce 25Ω net resistance. I desoldered one end of each of the four resistors to check them each individually. What I found was that three of the four resistors were open, and the fourth exhibited a measured resistance of 1065Ω - a far cry from the 25Ω called for in the schematic.
There were a couple of indications that these resistors had already been replaced. First of all was their size. In order for an array of four parallel resistors to provide 15W of power capability, each resistor would need to be rated at 3.5 Watts. These resistors were the same exact size as the 2W resistors in my inventory. Further, the resistors installed there were, according to their color codes, 5% tolerance rather than the 1% called for in the schematic. These points led me to believe that the resistors had been replaced at some point in the history of this unit, and not with the correct specification parts.
The daughterboard, also located within the yellow oval in Figure 3, was heavily charred in the vicinity of the one remaining “working” resistor - that is, the only one that was not open-circuit. Needless to say, this was because of two problems - a) all of the current flowing through the one resistor, and b) the inadequate power-handling capability of that one resistor. I decided that a better scheme was called for in the replacement of these resistors.
As I normally do not stock resistors rated higher than two watts, I set out to source some appropriate resistors for this job. What I found was that 3.5W resistors are not offered by my major suppliers. I then opted for 5W types - four 100Ω 5W 1% resistors in parallel would produce 25Ω ±1% at 20 Watts - a good solution. However, 5 Watt resistors are readily available only as wirewound resistors. Naturally, we do not want to introduce wirewound resistors into an RF circuit due to their inherent inductance. However, at least one manufacturer, Vishay, makes resistors of equivalent physical and electrical specifications available with non-inductive (Ayrton-Perry) windings. This seemed like a good option, but they are very expensive. I was hesitant to spend the better part of a hundred dollars of the customer’s money for this, so I went to bed that night with the problem on my mind. At about 0230, I awoke with a possible solution in mind. It would still not be exactly cheap pricewise, but it would be far better than the non-inductive wirewound alternative.
What I came up with was the idea of building ten series strings of resistors, using one each of a 240Ω 2W 1% metal-film resistor and a 10Ω 2W 1% metal-film resistor. This would give me ten strings of 250Ω ±1% each, which when taken in parallel, would provide a net resistance of 25Ω ±1%, and would do so at a power-handling capability of 40 Watts - 2 Watts each at twenty pieces. I mounted five strings each to a pair of 40mm x 60mm proto-boards, and then I connected the boards in parallel.
|
I identified a suitable location on the mainboard to install this board sandwich, and after attaching a pair of solder lugs for securement to existing mounting screw locations, I secured the board arrangement to the mainboard. The location of this board sandwich can be seen within the red oval in the Figure 4 illustration. It should be noted that I did need to slightly trim the mainboard shield to provide clearance for the resistor array. The array is connected to the mainboard via the two white wires visible in the photo, which are secured to the mainboard at
|
the R121 location where the original daughterboard had been installed.
The repair was not complete at this point, however. I still needed to replace the RF hash choke with one of the correct value. While I normally stock this particular choke, a 5258-RC 1mH choke with a 0.55Ω DC resistance and a one-ampere current rating, I happened to be out of stock on it, but I already had it coming in my weekly stock order. This was a lucky break for the customer, as no shipping charges would be applied for any special-order parts.
We set up a try-out session for the day that he would come to pick up the repaired unit, in which I used my Icom IC-746 PRO and the Club’s antenna array as a test platform. This permitted the customer to see the unit in proper operation before heading back to Dover with the repaired unit. I particularly appreciate the opportunity for the customer to see a repaired unit operating normally when it is returned after a repair. Such an opportunity provides a level of satisfaction for the customer and a level of protection for me at the same time.
One important end note. The question that must be asked is how did this failure happen in the first place? I do not have any satisfactory answer to that question. One thing that came out in our conversations, however, was the fact that there was no lightning protection at all on this system. While this is not likely to be related to this failure, as the failure was on the tuner input side, it is nonetheless always recommended to have proper lightning protection on your system.
See you next month!
Baofeng BF-F8HP HT Transceiver - November 2025
|
Not very long ago, one of our fellow Club members had come to me with a radio that held some particular nostalgic value for him, as it was the first amateur-band radio he had ever owned. The problem was that the radio apparently had no TX audio output, though it showed full output power when transmitting. The problem was that no modulated audio was passed through in the resulting transmission.
My initial thought, after asking him if the radio had ever been dropped, was to look at the microphone solder joints where it is mounted to the mainboard in the radio. I disassembled the radio and carefully inspected, then tested, the microphone solder points, to find that it was OK, and that the problem was apparently |
elsewhere. I then had a bright idea, and decided to test the radio in transmit mode using an appropriate headset plugged into the K-1 jack pair on the side of the radio. Lo and behold, the audio came through in the transmission just fine when a headset was used, but not without one. That told me that the problem was most likely either a bad solder joint at one of the two jacks, or a failed switch within the mic jack. The owner decided that he wanted to repair the radio, so I took it to my shop for repair.
|
Once there, I opened up the radio again and then took a good look at the solder joints for the two jacks. This type of radio uses a pair of jacks mounted directly adjacent to each other, with a unique inter-connection between the two jacks. One, the upper jack, is a 3.5mm (1/8”) TRS jack having five terminals - meaning that it includes two switches. The other jack is a 2.5mm (3/32”) TRS jack with four terminals, having only one internal switch. The pinout for the jack set is shown in Figure 2.
|
This two-plug jack configuration is known in the amateur radio field as a “K-1 jack” and is generally considered a single jack, even though it is usually really made up of two discrete jacks installed side-by-side on the PCB.
The jacks used in the Baofeng radios are actually quite commonly used, so I stock a quantity of each of them. Replacement of the jacks was straight-forward and simply required desoldering the jacks. However, in a strange twist, the PCB does not have the typical round holes in the connecting pads for these jacks. Instead, the holes are actually slots that are very closely sized to the mating tabs on the jacks. The jacks that are used, the PJ-328A (3.5mm) and the PJ-208B (2.5mm) are often sold as dual-use through-hole and surface-mount devices. This duality is accomplished simply by bending the connecting tabs either out to the side for surface-mount use, or straight down for through-hole applications.
Disassembly of the BF-F8HP requires removal and replacement of the LCD display panel from the mainboard as well as desoldering of the antenna jack center conductor from the board. In reality, the antenna jack does not need to be desoldered for disassembly, but it sure makes re-assembly a more simplified task if it is desoldered.
|
Handling of the LCD panel calls for some care and absolute cleanliness. As is often the case with LCD panels, the connections to the panel are made through rubber connecting strips called “zebra strips” because they are frequently striped black and white when viewed on-edge. These strips are more properly known as “elastomeric connectors” and their use is illustrated at Figure 3. When installed, they must be clean - especially of skin oil - and carefully aligned with the edges of the LCD panel where the contact points are located, and with their mating contact pads on the PCB to which the LCD panel is mounted. |
Very often, after being disassembled, upon reassembly the LCD panel has missing characters or even complete lines of dots missing in the array that forms the characters on the display. This can be corrected by disassembling, cleaning, and properly positioning the panel and the zebra strips again. Once properly installed, the full display will be restored.
Repairs to this radio will most often also require the desoldering of the speaker connecting wires from the mainboard, so that the radio housing can be separated from the chassis. Proper tools are also important, as despite the fact that these radios are Chinese-made products, they actually use JIS screws whose drive ends are easily stripped when the wrong screwdriver is used. The use of a JIS screwdriver is imperative when working on these radios. On reassembly, take care to reserve the two long screws for securement of the LCD panel frame to the mainboard and chassis. The shorter screws used in all of the other locations will not work here - they are too short and will not reach the threads in the chassis.
This was an extremely simple repair, especially because I had the correct parts on hand. I should point out that I had originally considered using a pair of jacks from a “dead” Baofeng BF-F8HP that was given to me for parts. However, this particular radio, a very early version of this model, used a different jack setup with round pins in a slightly different pattern than that of the subject radio. I think that I actually came across that before, which is why I had the correct jacks in stock. Due to their age and the fact that they are used as a pair, both connected and disconnected simultaneously, I decided to replace both jacks. Needless to say, post-repair the radio worked flawlessly.
While I would not normally recommend making a repair that costs more than the replacement cost of the radio, as I mentioned earlier, this particular radio has a certain nostalgic value to its owner, which made it worth the cost of repairs to him. It is really interesting how one can become attached to an innate piece of technology, but it does happen, and quite frequently at that.
See you next month!
MFJ-949E Deluxe Versa Tuner II - October 2025
prepared, in this case, means having equipment redundancies that will allow the rapid substitution of one piece of equipment for another that may be operating at some sub-par level. This is exactly what happened at Field Day 2025, where I was serving as band chair for the 20-meter phone team.
I had brought both automatic and manual antenna tuners for both of my radios, the Icom IC-718 and the Icom IC-746 PRO. The initial setup with which we would face the start of the event was settled on as being the IC-718 radio, connecting through the MFJ-949 antenna tuner. The MFJ-949 was chosen simply because of its larger cross-needle SWR meter on its front panel. The trouble started almost immediately after we connected the MFJ-949 into the circuit.
As we went to tune the radio/antenna combination, team member Lee Hafele WA2LH noted that the SWR indication was jumping around repeatedly but quite erratically as he attempted to tune the system. At the time, I simply put the MFJ-949 aside, swapped in my MFJ-941 in its place, and enjoyed the rest of Field Day. Now, a bit more than a week after Field Day, I got around to checking out the MFJ-949, so as to see why it was displaying SWR variations.
I had noted that the inductor selector switch felt rather “mushy” when operated, and since that was what we were adjusting when we noticed the SWR excursions, I decided to start there. Of course, apart from the fact that the switch was loose in its mounting and the knob was incorrectly indexed, the switch itself was OK. I secured the switch properly in the front panel. As to the mis-indexed switch knob, that was a simple matter of placing the switch in its “A” position (selecting the highest tap on the coil) and then installing the knob with its pointer aligned with that “A” position marking on the front panel.
In a similar manner, both of the tuning capacitors were loosely mounted to the front panel. This was less noticeable because the capacitors do not have detents as the inductor switch has, but it was an annoyance nonetheless. I corrected that problem by once again tightening the securing shaft nuts - one on each capacitor - and then properly indexing the knobs to the front panel markings.
OK - I found a couple of minor issues and corrected them, but they were not causal to the problem at hand. I decided to perform an in-depth physical examination of the unit. I began by focusing on the signal path.
The MFJ-949 was marketed as a “Deluxe Versa Tuner II” and the unit tries hard to live up to the hype. It has a large cross-needle SWR/Power meter on the front panel, with switched meter illumination available when a 13.8VDC supply is connected to the power jack on the rear panel. The meter is selectable to either a 30W or a 300W value range, and it is also able to switch between average (“AVG”) or peak (“PEAK”) power displayed on the meter.
The front panel function switch provides for four separate outputs, all of which are available via either the “TUNED” or the “BYPASS” operational mode. The four outputs on each mode are as follows :
I had brought both automatic and manual antenna tuners for both of my radios, the Icom IC-718 and the Icom IC-746 PRO. The initial setup with which we would face the start of the event was settled on as being the IC-718 radio, connecting through the MFJ-949 antenna tuner. The MFJ-949 was chosen simply because of its larger cross-needle SWR meter on its front panel. The trouble started almost immediately after we connected the MFJ-949 into the circuit.
As we went to tune the radio/antenna combination, team member Lee Hafele WA2LH noted that the SWR indication was jumping around repeatedly but quite erratically as he attempted to tune the system. At the time, I simply put the MFJ-949 aside, swapped in my MFJ-941 in its place, and enjoyed the rest of Field Day. Now, a bit more than a week after Field Day, I got around to checking out the MFJ-949, so as to see why it was displaying SWR variations.
I had noted that the inductor selector switch felt rather “mushy” when operated, and since that was what we were adjusting when we noticed the SWR excursions, I decided to start there. Of course, apart from the fact that the switch was loose in its mounting and the knob was incorrectly indexed, the switch itself was OK. I secured the switch properly in the front panel. As to the mis-indexed switch knob, that was a simple matter of placing the switch in its “A” position (selecting the highest tap on the coil) and then installing the knob with its pointer aligned with that “A” position marking on the front panel.
In a similar manner, both of the tuning capacitors were loosely mounted to the front panel. This was less noticeable because the capacitors do not have detents as the inductor switch has, but it was an annoyance nonetheless. I corrected that problem by once again tightening the securing shaft nuts - one on each capacitor - and then properly indexing the knobs to the front panel markings.
OK - I found a couple of minor issues and corrected them, but they were not causal to the problem at hand. I decided to perform an in-depth physical examination of the unit. I began by focusing on the signal path.
The MFJ-949 was marketed as a “Deluxe Versa Tuner II” and the unit tries hard to live up to the hype. It has a large cross-needle SWR/Power meter on the front panel, with switched meter illumination available when a 13.8VDC supply is connected to the power jack on the rear panel. The meter is selectable to either a 30W or a 300W value range, and it is also able to switch between average (“AVG”) or peak (“PEAK”) power displayed on the meter.
The front panel function switch provides for four separate outputs, all of which are available via either the “TUNED” or the “BYPASS” operational mode. The four outputs on each mode are as follows :
- COAX 2
- COAX 1
- BAL WIRE LINE
- DUMMY LOAD
|
One of the deluxe features in this antenna tuner is the fact that it has an internally-mounted dummy load. As a result, there is no Dummy Load connector on the rear panel. In point of fact, the rear panel is remarkable for its simplicity, In addition to the three SO-239 connectors labeled COAX 1, COAX 2, and TRANSMITTER, there are three binding posts for the balanced wire antenna connection, a DC power socket for the meter illumination power source, and a ground terminal. In keeping with the clean appearance of the rear panel, each of the SO-239 connector sockets is secured to panel by two aluminum pop rivets. See Figure 2.
My deep-dive into the physicality of the MFJ-949 turned up the cause of the SWR excursions. The GCARC Club member and the individual who was working with me to match the radio and antenna via the MFJ-949 said at the time that the unit was behaving as if there was a loose connection. In a sense, he was |
exactly correct in his initial assessment. It turns out that two of the three SO-239 connectors were actually loose on the rear panel.
Despite the fact that the sockets themselves are of the four-hole flange type, MFJ chose to secure them with, as noted earlier, only two rivets (Figure 3). The SO-239’s are mounted from the inside of the unit, so the fact that there are two unused holes on each connector is not immediately evident. However, it is my belief that the choice to secure these connectors with only two rivets is directly causal to the problem that this unit exhibited.
It must be understood that the flange of the SO-239 connector is an integral part of the circuit and must therefore be tight and secure. This is necessary to a) avoid the introduction of unwanted resistance into the circuit, and b) to prevent SWR excursions that result from loose antenna connections.
The two connectors that were loose were the TRANSMITTER and COAX 2 connectors, with the TRANSMITTER socket being quite loose. This is evident in the Figure 2 illustration of the mounted SO-239, where black aluminum oxide marks are visible around the rivets. This looseness of the connectors was sufficient to interrupt the ground path through the connector shell and into the chassis of the MFJ-949. It is this interruption of the ground path that caused the intermittent fluctuation of the SWR indication.
You may be wondering at this point, why was the connector moving around? If the cable was tightened to the connector, and the antenna tuner was sitting firmly on the table, why should the connector shell move at all? The answer to that question has to do with the looseness of the inductor and capacitor controls on the front panel, but especially with the inductor switch. Because of the loose mounting of the switch, any manipulation of the inductor switch also caused movement of the entire unit on the table top, which in turn flexed the cable connection at the SO-239, causing movement of the connector on the chassis.
Despite the fact that the sockets themselves are of the four-hole flange type, MFJ chose to secure them with, as noted earlier, only two rivets (Figure 3). The SO-239’s are mounted from the inside of the unit, so the fact that there are two unused holes on each connector is not immediately evident. However, it is my belief that the choice to secure these connectors with only two rivets is directly causal to the problem that this unit exhibited.
It must be understood that the flange of the SO-239 connector is an integral part of the circuit and must therefore be tight and secure. This is necessary to a) avoid the introduction of unwanted resistance into the circuit, and b) to prevent SWR excursions that result from loose antenna connections.
The two connectors that were loose were the TRANSMITTER and COAX 2 connectors, with the TRANSMITTER socket being quite loose. This is evident in the Figure 2 illustration of the mounted SO-239, where black aluminum oxide marks are visible around the rivets. This looseness of the connectors was sufficient to interrupt the ground path through the connector shell and into the chassis of the MFJ-949. It is this interruption of the ground path that caused the intermittent fluctuation of the SWR indication.
You may be wondering at this point, why was the connector moving around? If the cable was tightened to the connector, and the antenna tuner was sitting firmly on the table, why should the connector shell move at all? The answer to that question has to do with the looseness of the inductor and capacitor controls on the front panel, but especially with the inductor switch. Because of the loose mounting of the switch, any manipulation of the inductor switch also caused movement of the entire unit on the table top, which in turn flexed the cable connection at the SO-239, causing movement of the connector on the chassis.
|
It is my firm belief that, had the SO-239 connectors been mounted with four fasteners instead of the two that were used, it would probably have held better over time. I see the use of only two fasteners as a purely financial decision, and I see the use of rivets instead of threaded fasteners as a similar financially-motivated choice.
|
By the way, for those who may not be familiar with the term, a KEPS nut is basically a standard hex nut with a captive but rotatable externally-toothed lock washer attached. The use of these nuts simplifies the assembly process and reduces the parts piece count.
Granted - there may have been some concern about the heads of screws interfering with the connection of standard PL-259 coaxial connectors to the SO-239 sockets, but that fear is groundless, as I have learned clearly through my repairs to this unit. I used machine screws with standard pan heads, and the PL-259 shells fit perfectly despite the presence of the screw heads.
Testing of the MFJ-949 after the repairs showed that the problem was gone. Thus, the repair was completely successful and the antenna tuner is now back in fully-operational condition. This is a problem that will most likely affect any antenna tuner with riveted connectors, and most especially those with only two fasteners per jack. It is an easy fix, but it makes a great difference in the performance of the tuner.
The lesson to be learned from this repair is that the manufacturers may not always have the utmost in longevity designed into the construction of their products, and that we can sometimes improve upon what the manufacturers give us.
Testing of the MFJ-949 after the repairs showed that the problem was gone. Thus, the repair was completely successful and the antenna tuner is now back in fully-operational condition. This is a problem that will most likely affect any antenna tuner with riveted connectors, and most especially those with only two fasteners per jack. It is an easy fix, but it makes a great difference in the performance of the tuner.
The lesson to be learned from this repair is that the manufacturers may not always have the utmost in longevity designed into the construction of their products, and that we can sometimes improve upon what the manufacturers give us.
Daiwa SWX-777 SWR & Power Meter - September 2025
|
A couple of months ago (as I write this), a customer brought his Ham-Soku SWX-777 SWR & Power Meter to me for repair and modification. This unit is a very early product of the Daiwa Company of Japan, and is a dual-needle meter rated for frequencies from 1.8 to 30 MHz. It has two power ranges for which it is calibrated, which include 1000W forward with 200W reverse, and 200W forward with 40W reverse. His Instructions to me were to
|
clean the unit, and to install some illumination for the meter to enable its easy use in conditions of darkness.
When I examined the device, I discovered that someone had already been here to install meter illumination, and had done a clearly terrible job of it. First off, there are two points that must be understood right off the bat… 1) that the unit natively does not use any external electrical power but has circuitry that is powered by the measured signal, and 2) that the modifications that had been made had been designed to operate at 230VAC, the typical line voltage in use in the part of Africa where my customer was using this meter.
The previous modification had involved gluing to the rear panel of the unit a DPST pushbutton switch of the type typically used in a desktop computer as the main power switch. The 230VAC line cord was wired directly to this switch with one lead on each pole of the switch. The remaining two terminals of the switch held a length of line cord wire that was routed in through a drilled hole in the rear panel. There was no shock protection at the switch, and there was no chafing protection for the line cord as it passed through the drilled hole and into the unit. There also was no pushbutton cap on the switch actuator; it was a bare square post with which the switch is equipped.
Internally, the illumination circuit consisted of a small transformer, a single 1N4001 diode, a 1500µF/16V radial electrolytic capacitor, and a pair of wire leads that were routed into the meter enclosure, again through a drilled hole in that enclosure, at the upper right-hand corner of the meter face. One of these leads connected to the positive terminal of the capacitor, to which the cathode of the diode was also soldered. The diode anode was soldered to one of the transformer secondary leads. The other secondary lead was soldered to the negative terminal of the capacitor, as was the second wire lead that was routed into the meter enclosure. The capacitor was glued end-down in a vertical orientation to the floor of the unit, near the transformer. The incoming line cord, which had chafed through on the edge of the drilled hole in the rear panel, was connected to the two transformer primary leads. None of the various solder joints was taped, insulated, or covered in any way, and there was no chafe protection for the wire leads going into the small hole drilled into the meter enclosure.
A few words are in order about the meter itself as a component part of the SWX-777 overall unit. The meter is a cross-sweep dual-needle D’Arsonval movement with viewing dimensions of four inches wide by three inches high. This movement and face plate are mounted inside a steel enclosure that is four-and-an-eighth inches square, which in turn has a lens that matches the viewing area. The steel enclosure is just about an inch deep, and is closed at the back with a two-layer plastic plate through which the three meter connections pass. There is a positive lead for each needle and a common negative lead.
It was necessary for me to disassemble the meter assembly in order to access the internal illumination components. What I found surprised me. First of all, there was a small curl of steel drill shrapnel that had fallen into the meter movement and was held against the permanent magnet there, jamming one of the two needles of the meter. In addition, there was a small (half-inch diameter) circle of paper also stuck in the meter movement. This was apparently a label of some sort whose adhesive had failed, allowing the label to fall off and down into the meter. Finally, I found that the illumination had been provided by a rigid strip of miniature (0.120” x 0.140”) LED’s, with twelve individual LED’s in the strip. The LED’s had failed, which did not surprise me at all, as there was no current-limiting resistor in the LED circuit.
When I examined the device, I discovered that someone had already been here to install meter illumination, and had done a clearly terrible job of it. First off, there are two points that must be understood right off the bat… 1) that the unit natively does not use any external electrical power but has circuitry that is powered by the measured signal, and 2) that the modifications that had been made had been designed to operate at 230VAC, the typical line voltage in use in the part of Africa where my customer was using this meter.
The previous modification had involved gluing to the rear panel of the unit a DPST pushbutton switch of the type typically used in a desktop computer as the main power switch. The 230VAC line cord was wired directly to this switch with one lead on each pole of the switch. The remaining two terminals of the switch held a length of line cord wire that was routed in through a drilled hole in the rear panel. There was no shock protection at the switch, and there was no chafing protection for the line cord as it passed through the drilled hole and into the unit. There also was no pushbutton cap on the switch actuator; it was a bare square post with which the switch is equipped.
Internally, the illumination circuit consisted of a small transformer, a single 1N4001 diode, a 1500µF/16V radial electrolytic capacitor, and a pair of wire leads that were routed into the meter enclosure, again through a drilled hole in that enclosure, at the upper right-hand corner of the meter face. One of these leads connected to the positive terminal of the capacitor, to which the cathode of the diode was also soldered. The diode anode was soldered to one of the transformer secondary leads. The other secondary lead was soldered to the negative terminal of the capacitor, as was the second wire lead that was routed into the meter enclosure. The capacitor was glued end-down in a vertical orientation to the floor of the unit, near the transformer. The incoming line cord, which had chafed through on the edge of the drilled hole in the rear panel, was connected to the two transformer primary leads. None of the various solder joints was taped, insulated, or covered in any way, and there was no chafe protection for the wire leads going into the small hole drilled into the meter enclosure.
A few words are in order about the meter itself as a component part of the SWX-777 overall unit. The meter is a cross-sweep dual-needle D’Arsonval movement with viewing dimensions of four inches wide by three inches high. This movement and face plate are mounted inside a steel enclosure that is four-and-an-eighth inches square, which in turn has a lens that matches the viewing area. The steel enclosure is just about an inch deep, and is closed at the back with a two-layer plastic plate through which the three meter connections pass. There is a positive lead for each needle and a common negative lead.
It was necessary for me to disassemble the meter assembly in order to access the internal illumination components. What I found surprised me. First of all, there was a small curl of steel drill shrapnel that had fallen into the meter movement and was held against the permanent magnet there, jamming one of the two needles of the meter. In addition, there was a small (half-inch diameter) circle of paper also stuck in the meter movement. This was apparently a label of some sort whose adhesive had failed, allowing the label to fall off and down into the meter. Finally, I found that the illumination had been provided by a rigid strip of miniature (0.120” x 0.140”) LED’s, with twelve individual LED’s in the strip. The LED’s had failed, which did not surprise me at all, as there was no current-limiting resistor in the LED circuit.
|
Before I could do anything about the illumination itself, I had to correct the incoming power problems. It was beyond unsafe as it was, and it is a miracle that nobody was shocked or killed by the unit. I began by disconnecting the incoming line cord from the transformer primary leads, and then removed the switch from the rear panel of the SWX-777. I removed the wire leads from the switch and discarded the switch. I then marked
|
and drilled two holes in the rear panel of the unit, one on either side of the rear panel, avoiding the power-sensing tube that runs inside between the two SO-239 connectors on the rear panel. Into one of these new holes, I installed a double-pole toggle switch rated at 2A/250VAC. I then passed the line cord through the other new hole, installing a proper strain relief bushing into that hole to secure and protect the line cord. The line cord was then soldered to the toggle switch, with one lead on each pole. Next, I connected the transformer primary leads to the toggle switch. This completed the necessary corrections to the incoming power, and I could now continue with my testing and analysis of the illumination circuit.
When powered up on 230VAC via a step-up transformer on my bench (connected through my isolation transformer), I found that there was a ragged 17 volts of pulsating DC at the LED strip. Remember… in addition to the high voltage, there was no current limiting present, so it was inevitable that the LED’s would fail. Of course, the reason that there was about seventeen volts there was due to the fact - as I could then infer - that the small transformer that had been installed inside the SWX-777 was one with a nominal 12VAC secondary. Standard transformer theory holds that the pulsating DC produced by a half-wave rectifier will be at the peak voltage of the AC input to the rectifier. A transformer that is rated at 12VAC refers to the RMS voltage of the output sinusoidal waveform from the transformer… which would in turn equate to a peak voltage of about seventeen volts (12V x 1.414 = 16.968V).
I sourced and ordered a flexible self-adhesive and trimmable LED strip that uses 12V white LED’s. According to the specifications for the strip, there were 2400 LED’s in the entire strip, which draws 3000mA at 12VDC. The LED spacing is set at 400 LED’s per meter, or four per centimeter. I decided to install a 90mm strip of LED’s inside the meter in place of the former strip that had been glued into position across the top of the meter enclosure, facing downward across the meter face plate. At four LED’s per centimeter, this 90mm strip would thus include thirty-six LED’s. With the entire strip of 2400 LED’s drawing 3000mA, each LED would then draw 1.25mA, or 45mA for the 90mm strip. Now I could design and build a proper power supply that would power these LED’s for the long term.
I started with two four-terminal center-mount terminal lug strips and four 1N4001 diodes. I arranged the diodes into a full-wave bridge rectifier (FWBR) pattern and installed them to the terminal lug strips. Next, I added a 2200µF/16V aluminum electrolytic capacitor, with the positive terminal connected to the junction of two diode cathodes and the negative terminal connected to the junction of two diode anodes. These would become the positive and negative points of the power supply, respectively, with the capacitor providing filtering for the supply. Next, I added a heat-sinked LM7812 twelve-volt three-terminal voltage regulator IC, to which I had added a 0.22µF monolithic ceramic capacitor between the input (pin 1) and the ground (pin 2) terminals of the IC. In addition, I added a 0.1µF monolithic ceramic capacitor between the output (pin 3) and the ground terminals. I added a 270Ω 1% 2W metal film resistor to the output terminal of the voltage regulator IC and then soldered the input pin to the positive terminal of the FWBR and the ground pin to the negative terminal of the FWBR. To complete the power supply, I added heat shrink tubing as appropriate, and then I added a red and a black 22AWG stranded wire in about a ten-inch length each to the open lead of the 270Ω current-limiting resistor (red) and to the negative terminal of the power supply (black). Mounting holes were marked and drilled in the unit floor, and the power supply was then installed there using a pair of 4-40 x 1/4” machine screws and KEPS nuts. I was now ready to power the new LED strip.
OK - time for the “techy” stuff. How did I determine that I should use a 270Ω resistor for the current-limiting task? This is where Ohm’s Law comes in. The LED strip, with its thirty-six LED’s each drawing 1.25mA, would require 45mA total as I said earlier. The design output of my new power supply is a nominal twelve volts. According to Ohm’s Law, resistance is equal to the voltage divided by the current. Thus, we have the following :
With a calculated value of 266.67 ohms, the closest standard value is 270 ohms. Simple, right? So then… what was the actual final voltage and current supplied to the LED strip? Well, we already know that the current was somewhere in the vicinity of 45mA for the strip, which was comprised of a parallel string of individual LED’s. Let’s see if we can get more accurate with the LED current value.
The actual measured voltage out of the voltage regulator was 12.37VDC. Let’s substitute that in for the nominal twelve volts used in the design process, but this time, we will also use the actual measured resistance of the dropping resistor installed in the circuit :
Enough of the “techy” stuff – let’s get back to the modification work.
My next task was to enlarge the very small hole that had been drilled into the meter enclosure, with two goals in mind: a) to accommodate the two 22AWG wire leads entering there without the chance of chafing the wires, and b) to allow me to slide the LED strip into place inside the enclosure and against its upper inner surface.
I then soldered the red and black leads from the power supply to the LED strip, observing the proper polarity, and tested the operation of the new LED’s. They worked as intended. Next, I cut the red and black 22AWG leads mid-length and stripped about 3/16” of each cut end. I then installed bullet-type insulated connectors to these leads, male at the meter end and female at the power supply end. This allows for easy future removal of the meter assembly from the unit without the need to cut any wires, as the meter illumination is now a plug-in affair. I removed the cover paper from the LED strip’s adhesive, applied some tape over the solder joints where the leads attached, slid the LED strip into the meter enclosure, and pressed it into place. All that remained was to reassemble the meter and then to re-install it into the SWX-777 frame.
With the meter fully assembled and the leads for the LED plugged in (observing the wire colors), I did a final in-place test of the meter illumination and was very happy with the result. A Dymo-printed label set was installed to identify the purpose of the new switch on the rear panel. Finally, I installed the unit cover and called it “done”.
This was a fairly straight-forward modification of an existing unit, but all done with an eye towards a professional and finished appearance and the utmost in safety for the equipment user. It was quite surprising that anyone would have done a job the way the original LED strip was installed here, with its complete disregard for user safety or even the norms of electrical construction and assembly. In addition, the carelessness of drilling the meter enclosure and allowing a steel chip to fall into the meter movement is inexcusable. I can truly say that I am very happy with the final results on this job, and I hope that my customer is just as pleased.
When powered up on 230VAC via a step-up transformer on my bench (connected through my isolation transformer), I found that there was a ragged 17 volts of pulsating DC at the LED strip. Remember… in addition to the high voltage, there was no current limiting present, so it was inevitable that the LED’s would fail. Of course, the reason that there was about seventeen volts there was due to the fact - as I could then infer - that the small transformer that had been installed inside the SWX-777 was one with a nominal 12VAC secondary. Standard transformer theory holds that the pulsating DC produced by a half-wave rectifier will be at the peak voltage of the AC input to the rectifier. A transformer that is rated at 12VAC refers to the RMS voltage of the output sinusoidal waveform from the transformer… which would in turn equate to a peak voltage of about seventeen volts (12V x 1.414 = 16.968V).
I sourced and ordered a flexible self-adhesive and trimmable LED strip that uses 12V white LED’s. According to the specifications for the strip, there were 2400 LED’s in the entire strip, which draws 3000mA at 12VDC. The LED spacing is set at 400 LED’s per meter, or four per centimeter. I decided to install a 90mm strip of LED’s inside the meter in place of the former strip that had been glued into position across the top of the meter enclosure, facing downward across the meter face plate. At four LED’s per centimeter, this 90mm strip would thus include thirty-six LED’s. With the entire strip of 2400 LED’s drawing 3000mA, each LED would then draw 1.25mA, or 45mA for the 90mm strip. Now I could design and build a proper power supply that would power these LED’s for the long term.
I started with two four-terminal center-mount terminal lug strips and four 1N4001 diodes. I arranged the diodes into a full-wave bridge rectifier (FWBR) pattern and installed them to the terminal lug strips. Next, I added a 2200µF/16V aluminum electrolytic capacitor, with the positive terminal connected to the junction of two diode cathodes and the negative terminal connected to the junction of two diode anodes. These would become the positive and negative points of the power supply, respectively, with the capacitor providing filtering for the supply. Next, I added a heat-sinked LM7812 twelve-volt three-terminal voltage regulator IC, to which I had added a 0.22µF monolithic ceramic capacitor between the input (pin 1) and the ground (pin 2) terminals of the IC. In addition, I added a 0.1µF monolithic ceramic capacitor between the output (pin 3) and the ground terminals. I added a 270Ω 1% 2W metal film resistor to the output terminal of the voltage regulator IC and then soldered the input pin to the positive terminal of the FWBR and the ground pin to the negative terminal of the FWBR. To complete the power supply, I added heat shrink tubing as appropriate, and then I added a red and a black 22AWG stranded wire in about a ten-inch length each to the open lead of the 270Ω current-limiting resistor (red) and to the negative terminal of the power supply (black). Mounting holes were marked and drilled in the unit floor, and the power supply was then installed there using a pair of 4-40 x 1/4” machine screws and KEPS nuts. I was now ready to power the new LED strip.
OK - time for the “techy” stuff. How did I determine that I should use a 270Ω resistor for the current-limiting task? This is where Ohm’s Law comes in. The LED strip, with its thirty-six LED’s each drawing 1.25mA, would require 45mA total as I said earlier. The design output of my new power supply is a nominal twelve volts. According to Ohm’s Law, resistance is equal to the voltage divided by the current. Thus, we have the following :
With a calculated value of 266.67 ohms, the closest standard value is 270 ohms. Simple, right? So then… what was the actual final voltage and current supplied to the LED strip? Well, we already know that the current was somewhere in the vicinity of 45mA for the strip, which was comprised of a parallel string of individual LED’s. Let’s see if we can get more accurate with the LED current value.
The actual measured voltage out of the voltage regulator was 12.37VDC. Let’s substitute that in for the nominal twelve volts used in the design process, but this time, we will also use the actual measured resistance of the dropping resistor installed in the circuit :
Enough of the “techy” stuff – let’s get back to the modification work.
My next task was to enlarge the very small hole that had been drilled into the meter enclosure, with two goals in mind: a) to accommodate the two 22AWG wire leads entering there without the chance of chafing the wires, and b) to allow me to slide the LED strip into place inside the enclosure and against its upper inner surface.
I then soldered the red and black leads from the power supply to the LED strip, observing the proper polarity, and tested the operation of the new LED’s. They worked as intended. Next, I cut the red and black 22AWG leads mid-length and stripped about 3/16” of each cut end. I then installed bullet-type insulated connectors to these leads, male at the meter end and female at the power supply end. This allows for easy future removal of the meter assembly from the unit without the need to cut any wires, as the meter illumination is now a plug-in affair. I removed the cover paper from the LED strip’s adhesive, applied some tape over the solder joints where the leads attached, slid the LED strip into the meter enclosure, and pressed it into place. All that remained was to reassemble the meter and then to re-install it into the SWX-777 frame.
With the meter fully assembled and the leads for the LED plugged in (observing the wire colors), I did a final in-place test of the meter illumination and was very happy with the result. A Dymo-printed label set was installed to identify the purpose of the new switch on the rear panel. Finally, I installed the unit cover and called it “done”.
This was a fairly straight-forward modification of an existing unit, but all done with an eye towards a professional and finished appearance and the utmost in safety for the equipment user. It was quite surprising that anyone would have done a job the way the original LED strip was installed here, with its complete disregard for user safety or even the norms of electrical construction and assembly. In addition, the carelessness of drilling the meter enclosure and allowing a steel chip to fall into the meter movement is inexcusable. I can truly say that I am very happy with the final results on this job, and I hope that my customer is just as pleased.
|
I started with two four-terminal center-mount terminal lug strips and four 1N4001 diodes. I arranged the diodes into a full-wave bridge rectifier (FWBR) pattern and installed them to the terminal lug strips. Next, I added a 2200µF/16V aluminum electrolytic capacitor, with the positive terminal connected to the junction of two diode cathodes and the negative terminal connected to the junction of two diode anodes. These would become the positive and negative points of the power supply, respectively, with the capacitor providing filtering for the supply. Next, I added a heat-sinked
|
LM7812 twelve-volt three-terminal voltage regulator IC, to which I had added a 0.22µF monolithic ceramic capacitor between the input (pin 1) and the ground (pin 2) terminals of the IC. In addition, I added a 0.1µF monolithic ceramic capacitor between the output (pin 3) and the ground terminals. I added a 270Ω 1% 2W metal film resistor to the output terminal of the voltage regulator IC and then soldered the input pin to the positive terminal of the FWBR and the ground pin to the negative terminal of the FWBR. To complete the power supply, I added heat shrink tubing as appropriate, and then I added a red and a black 22AWG stranded wire in about a ten-inch length each to the open lead of the 270Ω current-limiting resistor (red) and to the negative terminal of the power supply (black). Mounting holes were marked and drilled in the unit floor, and the power supply was then installed there using a pair of 4-40 x 1/4” machine screws and KEPS nuts. I was now ready to power the new LED strip.
OK - time for the “techy” stuff. How did I determine that I should use a 270Ω resistor for the current-limiting task? This is where Ohm’s Law comes in. The LED strip, with its thirty-six LED’s each drawing 1.25mA, would require 45mA total as I said earlier. The design output of my new power supply is a nominal twelve volts. According to Ohm’s Law, resistance is equal to the voltage divided by the current. Thus, we have the following :
With a calculated value of 266.67 ohms, the closest standard value is 270 ohms. Simple, right? So then… what was the actual final voltage and current supplied to the LED strip? Well, we already know that the current was somewhere in the vicinity of 45mA for the strip, which was comprised of a parallel string of individual LED’s. Let’s see if we can get more accurate with the LED current value.
The actual measured voltage out of the voltage regulator was 12.37VDC. Let’s substitute that in for the nominal twelve volts used in the design process, but this time, we will also use the actual measured resistance of the dropping resistor installed in the circuit :
The actual measured voltage out of the voltage regulator was 12.37VDC. Let’s substitute that in for the nominal twelve volts used in the design process, but this time, we will also use the actual measured resistance of the dropping resistor installed in the circuit :
Enough of the “techy” stuff – let’s get back to the modification work.
My next task was to enlarge the very small hole that had been drilled into the meter enclosure, with two goals in mind: a) to accommodate the two 22AWG wire leads entering there without the chance of chafing the wires, and b) to allow me to slide the LED strip into place inside the enclosure and against its upper inner surface.
My next task was to enlarge the very small hole that had been drilled into the meter enclosure, with two goals in mind: a) to accommodate the two 22AWG wire leads entering there without the chance of chafing the wires, and b) to allow me to slide the LED strip into place inside the enclosure and against its upper inner surface.
I then soldered the red and black leads from the power supply to the LED strip, observing the proper polarity, and tested the operation of the new LED’s. They worked as intended. Next, I cut the red and black 22AWG leads mid-length and stripped about 3/16” of each cut end. I then installed bullet-type insulated connectors to these leads, male at the meter end and female at the power supply end. This allows for easy future removal of the meter assembly from the unit without the need to cut any wires, as the meter illumination is now a plug-in affair. I removed the cover paper from the LED strip’s adhesive, applied some tape over the solder joints where the leads attached, slid the LED strip into the meter enclosure, and pressed it into place. All that remained was to reassemble the meter and then to re-install it into the SWX-777 frame.
With the meter fully assembled and the leads for the LED plugged in (observing the wire colors), I did a final in-place test of the meter illumination and was very happy with the result. A Dymo-printed label set was installed to identify the purpose of the new switch on the rear panel. Finally, I installed the unit cover and called it “done”.
This was a fairly straight-forward modification of an existing unit, but all done with an eye towards a professional and finished appearance and the utmost in safety for the equipment user. It was quite surprising that anyone would have done a job the way the original LED strip was installed here, with its complete disregard for user safety or even the norms of electrical construction and assembly. In addition, the carelessness of drilling the meter enclosure and allowing a steel chip to fall into the meter movement is inexcusable. I can truly say that I am very happy with the final results on this job, and I hope that my customer is just as pleased.
With the meter fully assembled and the leads for the LED plugged in (observing the wire colors), I did a final in-place test of the meter illumination and was very happy with the result. A Dymo-printed label set was installed to identify the purpose of the new switch on the rear panel. Finally, I installed the unit cover and called it “done”.
This was a fairly straight-forward modification of an existing unit, but all done with an eye towards a professional and finished appearance and the utmost in safety for the equipment user. It was quite surprising that anyone would have done a job the way the original LED strip was installed here, with its complete disregard for user safety or even the norms of electrical construction and assembly. In addition, the carelessness of drilling the meter enclosure and allowing a steel chip to fall into the meter movement is inexcusable. I can truly say that I am very happy with the final results on this job, and I hope that my customer is just as pleased.
Kenwood TS-480SAT - August 2025
|
For quite a long while, the GCARC Remote HF Station actually sat idle most of the time, and when it did see use, it was generally at output levels of 35 watts or less, as it was customarily in use in conjunction with the Elecraft KPA-1500 RF amplifier, which has a maximum input power of about 35 to 40 watts. Recently, some additional
|
users have been set up on the radio system. These users have a general tendency not to use the KPA-1500 and instead to utilize the higher output power capabilities of the TS-480SAT (Figure 1), often pushing it to its full 100-watt output.
The radio lives in a steel cage in the HF room at the W2MMD Clubhouse. Its only cooling is by the random movement of air in the room. Most of the time, the room is unattended, meaning that there is nothing to cause any air movement in that room. In such a situation, the only movement of air is that which is caused by the convective movement due to the radiated heat of the radio and its ancillary components. As a result, the radio has a strong likelihood of overheating with extended high-power use. A common end result of such a situation is the failure of the radio’s final power amplifier transistors. Such was the case with our radio.
Preliminary output power testing showed that the output power never exceeded about fifty to sixty percent of the rated power, topping out between fifty and sixty watts, as indicated by the radio’s front panel power meter. Bench testing at my shop with the Bird 43 meter showed that the output power was actually right at 51 watts, of course well below rated output.
The radio lives in a steel cage in the HF room at the W2MMD Clubhouse. Its only cooling is by the random movement of air in the room. Most of the time, the room is unattended, meaning that there is nothing to cause any air movement in that room. In such a situation, the only movement of air is that which is caused by the convective movement due to the radiated heat of the radio and its ancillary components. As a result, the radio has a strong likelihood of overheating with extended high-power use. A common end result of such a situation is the failure of the radio’s final power amplifier transistors. Such was the case with our radio.
Preliminary output power testing showed that the output power never exceeded about fifty to sixty percent of the rated power, topping out between fifty and sixty watts, as indicated by the radio’s front panel power meter. Bench testing at my shop with the Bird 43 meter showed that the output power was actually right at 51 watts, of course well below rated output.
|
I then did some thermal testing and some voltage spot checks. One of the transistors in the power amplifier (PA) stage of this radio is a 2SC3421 transistor in a TO-126 package, shown as Q3 and used to control the bias applied to the final amplifier transistor pair. The final amplifiers are a pair of 2SC27872 flange-mount transistors, which have six connecting leaves. The pinout of this transistor, shown at Figure 2, is rather unusual, though it is actually fairly common for power amplifier transistors used in modern amateur radio transceivers.
The four outermost leaves are all connected to the emitter, while the narrower of the two center leaves is the collector leaf and its opposite leaf is the base terminal. These transistors are designated Q4 and Q5 in the TS-480SAT. The voltage testing showed the base and the emitter of the Q3 bias transistor to both be at the same voltage of 0.69VDC. The schematic calls for the emitter to be at 0.73VDC while the base should be at 1.41VDC. I suspected that |
this transistor was shorted, and so I removed it for out-of-circuit testing. That testing validated the suspicion; the transistor was indeed shorted. Moving on to the finals, while the voltages at Q4 were nearly normal, the voltages at Q5 were not, with the base showing 0VDC, the same as the emitter, which is held at chassis ground potential. Furthermore, while working, this transistor was completely cold, while its mate (Q4) showed temperatures over 85°C. This transistor too was shorted, so I decided to replace the finals as a pair. I ordered in the 2SC2782 replacement transistors, and I ordered the 2SC3421 bias transistor at the same time, together with a pair of MA-27B varistors, which we will discuss next.
The finals and the bias transistor are temperature-compensated through the use of specialized varistor diodes that are thermally responsive. In each case, an MA-27B varistor is physically placed across and in contact with the upper surface of the transistor body. The diode is then encased in thermally-conductive paste designed to ensure that the temperature of the transistor is carried into the diode. The diode is then electrically placed in a controlling and compensating circuit that adjusts transistor voltages based on temperature. It is important that these diodes be checked for functionality and installed back in place against the transistors that they are meant to control at the time of any replacement of the transistors. Curiously, these diodes were marketed by Matsushita, their original manufacturer, under the trade name “Stabistor diode”, a hint at their intended purpose in stabilizing the operating voltages of the circuit under the control of these devices.
Transistor replacement was fairly straight-forward, with the only difficulty being the not-so-easy removal of the solder from the existing transistors. It was evident that both finals and the bias transistor had been replaced at some point, because the soldering on those components was clearly not factory work. However, when the work was done, it was done with lead-free solder, thus making removal more difficult. In such a situation, it is best to simply dilute the lead-free solder with some leaded solder, and then remove that solder a little bit at a time, repeating the dilution process until all of the solder has been successfully removed.
The 2SC2782 transistors require a special approach to removal, as they use sheet metal leaves as their contact elements. The process here involves removing as much solder as is possible, and then using the tip of a hobby knife blade to gently lift a corner of the leaf while applying heat to it. Once one corner has been lifted, grip the corner with a pair of needle-nose pliers or a hemostat, and then continue gently pulling on the leaf while applying additional heat. Be patient. Eventually, the leaf will lift free of the PCB pad with no damage to the PCB or to the transistor. Repeat this process on each of the transistor leaves in turn. It helps a bit to remove the mounting screws from the transistor as a first step in the process. Doing so reduces the level of transistor heat conduction to the chassis, which will make the removal process easier.
Contrary to the removal process, it is important to install and tighten the transistor mounting screws prior to attempting to solder the leaves to the PCB. The idea is to ensure proper alignment of the transistor with its solder pads while installing the screws.
Post-repair, the radio called for what is known as a transmit alignment. This is a long and tedious process that consists of numerous steps, which must all be done in the correct sequence. The alignment process also requires the removal of three coaxial interconnect cables and replacement thereof with longer cables, removal and replacement of a flat ribbon cable with a longer cable, and the temporary insertion of a service plug into the DATA port on the front of the radio.
The longer cables are to maintain inter-board connectivity while the boards are removed from the radio and separated to provide access for test equipment connections to various points on the boards. It should be noted that these are so-called “service items” that were once available for purchase from Kenwood. Now, all that Kenwood still offers are the three coaxial cables, at a cost of about fourteen dollars each. The ribbon cable can be substituted with a slightly longer similar cable available from Digikey at a modest three-dollar cost.
The service plug is nothing more than a 6-pin mini-DIN plug with pins 3 and 6 shorted to each other. This plug is inserted into the DATA port during a specific power-up process of the radio, which places the radio into its built-in service mode.
The full alignment includes a total of seventy-nine steps, one of which is a write step (step #76) that stores all of the newly adjusted values to an EEPROM, which then governs the operation of the radio after a normal power-up.
Quite a bit of specialized test equipment is needed for the process. I used my Motorola R2001A Communications Service Analyzer to do the job, as it has all of the necessary equipment built in. This alignment process is not for the faint of heart nor for the inexperienced technician. It is best left to someone who has done this kind of work before.
The Kenwood service manual for the TS-480 provides all of the necessary instructions, but the process is laborious and requires attention to fine detail to get it right. Even at that, I found myself second-guessing myself and wondering if I did get it all right the first time, especially when the radio seemed not to operate correctly when placed back into the remote station cage. However, as has been since learned, another properly-functioning radio is now having the exact same operational symptoms in that cage, so I believe that my alignment is vindicated.
This was a repair that started out as an easy one, and then turned into quite an ordeal – after the actual mechanical portion of the repair was complete! Lesson to be learned here is to research what all is involved before jumping into a job – it might just turn out to be more than you really want to tackle, or maybe more than that for which you are prepared as regards skills, knowledge, and bench equipment.
See You Next Month!
The finals and the bias transistor are temperature-compensated through the use of specialized varistor diodes that are thermally responsive. In each case, an MA-27B varistor is physically placed across and in contact with the upper surface of the transistor body. The diode is then encased in thermally-conductive paste designed to ensure that the temperature of the transistor is carried into the diode. The diode is then electrically placed in a controlling and compensating circuit that adjusts transistor voltages based on temperature. It is important that these diodes be checked for functionality and installed back in place against the transistors that they are meant to control at the time of any replacement of the transistors. Curiously, these diodes were marketed by Matsushita, their original manufacturer, under the trade name “Stabistor diode”, a hint at their intended purpose in stabilizing the operating voltages of the circuit under the control of these devices.
Transistor replacement was fairly straight-forward, with the only difficulty being the not-so-easy removal of the solder from the existing transistors. It was evident that both finals and the bias transistor had been replaced at some point, because the soldering on those components was clearly not factory work. However, when the work was done, it was done with lead-free solder, thus making removal more difficult. In such a situation, it is best to simply dilute the lead-free solder with some leaded solder, and then remove that solder a little bit at a time, repeating the dilution process until all of the solder has been successfully removed.
The 2SC2782 transistors require a special approach to removal, as they use sheet metal leaves as their contact elements. The process here involves removing as much solder as is possible, and then using the tip of a hobby knife blade to gently lift a corner of the leaf while applying heat to it. Once one corner has been lifted, grip the corner with a pair of needle-nose pliers or a hemostat, and then continue gently pulling on the leaf while applying additional heat. Be patient. Eventually, the leaf will lift free of the PCB pad with no damage to the PCB or to the transistor. Repeat this process on each of the transistor leaves in turn. It helps a bit to remove the mounting screws from the transistor as a first step in the process. Doing so reduces the level of transistor heat conduction to the chassis, which will make the removal process easier.
Contrary to the removal process, it is important to install and tighten the transistor mounting screws prior to attempting to solder the leaves to the PCB. The idea is to ensure proper alignment of the transistor with its solder pads while installing the screws.
Post-repair, the radio called for what is known as a transmit alignment. This is a long and tedious process that consists of numerous steps, which must all be done in the correct sequence. The alignment process also requires the removal of three coaxial interconnect cables and replacement thereof with longer cables, removal and replacement of a flat ribbon cable with a longer cable, and the temporary insertion of a service plug into the DATA port on the front of the radio.
The longer cables are to maintain inter-board connectivity while the boards are removed from the radio and separated to provide access for test equipment connections to various points on the boards. It should be noted that these are so-called “service items” that were once available for purchase from Kenwood. Now, all that Kenwood still offers are the three coaxial cables, at a cost of about fourteen dollars each. The ribbon cable can be substituted with a slightly longer similar cable available from Digikey at a modest three-dollar cost.
The service plug is nothing more than a 6-pin mini-DIN plug with pins 3 and 6 shorted to each other. This plug is inserted into the DATA port during a specific power-up process of the radio, which places the radio into its built-in service mode.
The full alignment includes a total of seventy-nine steps, one of which is a write step (step #76) that stores all of the newly adjusted values to an EEPROM, which then governs the operation of the radio after a normal power-up.
Quite a bit of specialized test equipment is needed for the process. I used my Motorola R2001A Communications Service Analyzer to do the job, as it has all of the necessary equipment built in. This alignment process is not for the faint of heart nor for the inexperienced technician. It is best left to someone who has done this kind of work before.
The Kenwood service manual for the TS-480 provides all of the necessary instructions, but the process is laborious and requires attention to fine detail to get it right. Even at that, I found myself second-guessing myself and wondering if I did get it all right the first time, especially when the radio seemed not to operate correctly when placed back into the remote station cage. However, as has been since learned, another properly-functioning radio is now having the exact same operational symptoms in that cage, so I believe that my alignment is vindicated.
This was a repair that started out as an easy one, and then turned into quite an ordeal – after the actual mechanical portion of the repair was complete! Lesson to be learned here is to research what all is involved before jumping into a job – it might just turn out to be more than you really want to tackle, or maybe more than that for which you are prepared as regards skills, knowledge, and bench equipment.
See You Next Month!
MFJ-259/269 Series - July 2025
|
This month’s column is taking a slight departure from the norm. Instead of reporting on a failed piece of equipment, this article will discuss an ongoing repetitive failure that was caused by the design of the equipment. Now, that is not one-hundred-percent true, as the problem is much worse on some models or examples than it is on others. In fact, some users may never notice any problem with this issue, while others will be cursing MFJ every time they attempt to use the MFJ-259 or MFJ-269 (Figure 1) type of SWR analyzer.
Let’s see just what this is all about. On my bench, I have an MFJ-259D as well as an MFJ-269D. Why would I have both of these instruments? Simple – the first instrument purchased does not cover the entire ham band set, but it was the best option at the time of purchase. The MFJ-259D has frequency coverage from 0.1MHz (100kHz) through 232 |
MHz, but has no coverage for UHF frequencies. The MFJ-269D, which was offered after I purchased the MFJ-259D, adds in the missing UHF coverage, in two ranges labeled as “UHF LO” and “UHF HI”. Furthermore, the MFJ-259D is marked as being an “HF/VHF SWR ANALYZER”, while the MFJ-269D is marked as being an “HF/VHF/220MHz/UHF SWR ANALYZER”.
These two instruments are remarkably similar in outward appearance and design features. However, there are some important differences not only between the instruments themselves but also in the fabric and plastic film protective carrying case/covers offered by MFJ for these instruments. Starting with the cover, the MFJ-259D cover has a nicely rounded and perfectly positioned hole in the front panel plastic film at the site of the push-button power switch. The placement of this hole is important in that it can interfere with the switch operation and even cause inadvertent switch activation if it is not properly positioned.
There are three shaft holes provided in the film at the locations of the three front panel rotary controls installed on the instrument, but there is no such hole in the film at the location of either the GATE or the MODE pushbutton switch. These two switches are momentary-type switches and are not easily activated inadvertently, so no holes are really needed for these switches.
Going back to the POWER pushbutton switch, this switch is a latching “ON” type of switch. In my example of the MFJ-259D, the pushbutton actuator is a low-profile cap that is just barely proud of the raised ring that surrounds its hole in the instrument front panel when the switch is “OFF”. When this switch is “ON”, the actuator cap is recessed below the plane of the surrounding ring. This arrangement makes it almost impossible to inadvertently switch this instrument’s power switch “ON”, as a casual bump of almost any type would not depress the button below the surface of the surrounding ring.
As a result of the power switch actuator design, I have never had an inadvertent power-on of the instrument, so I have never had an unexpected depletion of the battery pack in my MFJ-259D. The same cannot be said, of course, of my MFJ-269D.
Before going into the problems with the MFJ-269D, let’s spend a minute or so discussing just why it is so annoying when the MFJ-269D battery pack is depleted. First of all is the plain and simple inconvenience of needing to change out the battery set in the middle of a job. Most folks just want to get on with the job, and do not want to be bothered with the tedious task of battery pack replacement.
Next is the hassle involved in getting to the battery pack. In order to service the battery pack on this unit, the instrument must first be removed from its protective carrying case/cover. This requires the use of a 1/16” Allen wrench to loosen the grub screws (set screws) in the knobs. Once the knobs have been removed, it is necessary to work the case off the instrument, carefully lifting the plastic film off the control shafts that extend through the film. While not difficult to do, a momentary lapse of attention will result in a torn film as it snags on one of the shafts.
Once the protective carrying case/cover has been removed, we can remove the two sheet metal screws that secure the battery compartment cover to the instrument body, revealing the ten (10) “AA”-size cells within. That’s right - ten “AA” cells make up the battery pack for this instrument. Repetitive battery failure on this unit gets to be an expensive proposition!
From the above, it is easily evident just why it is such a problem that this instrument goes through so many batteries, but… exactly why do the batteries need such frequent replacement? The answer is because of the design of the front panel power switch as well as the design of the protective carrying case/cover.
These two instruments are remarkably similar in outward appearance and design features. However, there are some important differences not only between the instruments themselves but also in the fabric and plastic film protective carrying case/covers offered by MFJ for these instruments. Starting with the cover, the MFJ-259D cover has a nicely rounded and perfectly positioned hole in the front panel plastic film at the site of the push-button power switch. The placement of this hole is important in that it can interfere with the switch operation and even cause inadvertent switch activation if it is not properly positioned.
There are three shaft holes provided in the film at the locations of the three front panel rotary controls installed on the instrument, but there is no such hole in the film at the location of either the GATE or the MODE pushbutton switch. These two switches are momentary-type switches and are not easily activated inadvertently, so no holes are really needed for these switches.
Going back to the POWER pushbutton switch, this switch is a latching “ON” type of switch. In my example of the MFJ-259D, the pushbutton actuator is a low-profile cap that is just barely proud of the raised ring that surrounds its hole in the instrument front panel when the switch is “OFF”. When this switch is “ON”, the actuator cap is recessed below the plane of the surrounding ring. This arrangement makes it almost impossible to inadvertently switch this instrument’s power switch “ON”, as a casual bump of almost any type would not depress the button below the surface of the surrounding ring.
As a result of the power switch actuator design, I have never had an inadvertent power-on of the instrument, so I have never had an unexpected depletion of the battery pack in my MFJ-259D. The same cannot be said, of course, of my MFJ-269D.
Before going into the problems with the MFJ-269D, let’s spend a minute or so discussing just why it is so annoying when the MFJ-269D battery pack is depleted. First of all is the plain and simple inconvenience of needing to change out the battery set in the middle of a job. Most folks just want to get on with the job, and do not want to be bothered with the tedious task of battery pack replacement.
Next is the hassle involved in getting to the battery pack. In order to service the battery pack on this unit, the instrument must first be removed from its protective carrying case/cover. This requires the use of a 1/16” Allen wrench to loosen the grub screws (set screws) in the knobs. Once the knobs have been removed, it is necessary to work the case off the instrument, carefully lifting the plastic film off the control shafts that extend through the film. While not difficult to do, a momentary lapse of attention will result in a torn film as it snags on one of the shafts.
Once the protective carrying case/cover has been removed, we can remove the two sheet metal screws that secure the battery compartment cover to the instrument body, revealing the ten (10) “AA”-size cells within. That’s right - ten “AA” cells make up the battery pack for this instrument. Repetitive battery failure on this unit gets to be an expensive proposition!
From the above, it is easily evident just why it is such a problem that this instrument goes through so many batteries, but… exactly why do the batteries need such frequent replacement? The answer is because of the design of the front panel power switch as well as the design of the protective carrying case/cover.
|
Starting again with the cover, it was disturbing to discover that no provision had been made in the plastic film for the power switch actuator pushbutton. This meant that I had to first install the cover and mark where to make a hole, then remove the cover and cut the required hole in its marked location. In addition, this model also has a latching pushbutton switch used to select either the “UHF LO” or the “UHF HI” frequency range when working with UHF frequencies. This switch too required the marking of a location and then the cutting of a hole at that location so as to be able to comfortably operate the switch (Figure 2). |
Once again going back to the power switch, the switch actuator on this model differs from that on the MFJ-259D in that it is a physically longer actuator, meaning that it sits considerably further out from the ring that surrounds the switch opening on the instrument front panel. This additional length also means that in its “ON” position, the actuator cap is still proud of the surrounding ring. Thus, it is very easy to inadvertently bump this switch and turn it “ON” without the user being aware that it has happened.
I typically store my two MFJ SWR analyzers by hanging them by their carrying case straps from the same hook on the wall of my shop. This arrangement then has one of these instruments hanging in front of and in contact with the other, often resulting in the inadvertent activation of the power switch on the MFJ-269D. The result is that almost every time I reach for it to use it, I find that the battery pack has been depleted and must be replaced before I can use the instrument.
Now we have arrived at the purpose of this article, and the nature of the “repair" that was made. In reality, this repair, actually a modification, was so simple that it is surprising to me that I had not thought of doing it sooner than I did.
I quickly realized that the MFJ switch design was poor and was the root cause of this problem. I set out to design a simple means of breaking the battery feed circuit between the battery pack and the power switch - something that could be easily installed, would not require major modification to the instrument, and would be easy to activate in order to kill the battery circuit whenever I wanted to do so. To be honest about it, I dragged my feet on this one, because I really did not want to start making holes willy-nilly in the enclosure. The protective carrying case/cover did not leave many alternatives as to location for a switch to be installed. Besides, what type of switch would I want to use? In reality, the simplest fix would have been to find a lower-profile switch actuator cap such as that used on the earlier models of this instrument. However, I think that I learned just why MFJ made the change – I could not find the low-profile actuator cap anywhere!
While I was perusing the MFJ-269D schematic one recent day, I realized that the DC power input jack used on the instrument is of the switching type as many of them are, but what is a bit different is that the switch was actually used in this circuit!
Quite often, the two terminals of the integrated switch in the DC power jack are simply tied together at the negative side of the supply. What was different here is that MFJ actually used the switch in the jack for the purpose of - wait for it - yes… disconnecting the battery pack when the wall wart power supply was connected to the instrument. Well, that is exactly what I wanted to do - to disconnect the battery pack. I realized that I could accomplish the task simply by inserting an appropriately-sized barrel connector dummy plug into the DC power jack!
|
I sourced a 5.5mm x 2.1mm power plug with a short twin-lead pigtail attached (Figure 3). I have several of them on hand, so that was no problem. I separated the two wires, and then I cut off the red wire right at the plug body - I only needed one wire for my purposes. I shortened the remaining black lead to about six inches, and then I crimped on a spade terminal with a heat-shrink tube covering. After shrinking the covering by applying hot air from my heat gun, I was ready to install the dummy plug.
|
|
I loosened one of the screws on the upper surface of the instrument, underneath the top flap of the carrying case. Then, I slid the spade lug under the screw head (Figure 4) and re-tightened the screw to secure the wired dummy plug to the instrument. Inserting the dummy plug barrel into the DC power jack (Figure 5) opens the battery circuit, making it impossible for the battery pack to become depleted inadvertently. This is such a simple solution to a nagging headache of a problem that had been annoying me for a couple of years. Every now and then a manufacturer does something that has unforeseen drawbacks, and it is up to those of us in the field to develop a solution to the problem presented. Sometimes that solution is so easy that it is often overlooked while searching for something more involved and complex. We are then making it harder on ourselves - harder than it needs to be. |
There is an old adage that says KISS! - Keep It Simple, Stupid! It is good advice that was never any truer than it was here.
See you next month!
See you next month!
Ameco PT Preamplifier - June 2025
|
Recently, Club member Darrell Neron AB2E brought to me for repair an old tube-type preamplifier unit known as an Ameco PT Preamplifier (Figure 1), which, at the time it was made, was a product of the Aerotron Company. This was the first of a series of different preamplifier models manufactured under the Ameco nameplate.
The problem with this one was that it would |
|
shut down as soon as the preamplifier circuit was energized, but it would function OK in bypass mode. Now, this unit is a very simple circuit, utilizing a single 6EH7 vacuum tube as the amplifying element. It also uses an older design dual filter capacitor, which had two 20µF 150V electrolytics in a single axial component (Figure 2). That was a common methodology in the past, in which the capacitor would have a single lead off the negative end, and two leads off the positive end, one for each section of the capacitor. These were so-called
|
“dry” electrolytics, which used a solid electrolyte rather than a liquid or paste-style compound.
Investigation of the unit showed that there was relatively little that could fail in the circuit. There are three solid-state diodes, several ceramic disc capacitors, several coils, an air-gap capacitor, several resistors, the dual electrolytic capacitor, two transformers, and the vacuum tube.
Going after the low-hanging fruit first, I immediately pulled and tested the vacuum tube, which surprised me by testing out at almost 100% of its new performance. I believe that this may actually be the original vacuum tube, as it is an Aerotron branded tube.
Some quick resistance checks showed that the resistors were all within their nominal tolerance values, and that the diodes were functional. While ceramic capacitors are fairly robust and do not fail often, they can and do sometimes fail. However, in this case, all of them tested OK, although there were two ceramic discs that were installed in a placement that nowadays is considered unsafe. More about them later.
I decided to test the dual filter capacitor for leakage, first in-circuit, which led to failed tests. I then tested the unit out-of-circuit, and once again found that both capacitors in the device had failed in a very leaky condition.
Investigation of the unit showed that there was relatively little that could fail in the circuit. There are three solid-state diodes, several ceramic disc capacitors, several coils, an air-gap capacitor, several resistors, the dual electrolytic capacitor, two transformers, and the vacuum tube.
Going after the low-hanging fruit first, I immediately pulled and tested the vacuum tube, which surprised me by testing out at almost 100% of its new performance. I believe that this may actually be the original vacuum tube, as it is an Aerotron branded tube.
Some quick resistance checks showed that the resistors were all within their nominal tolerance values, and that the diodes were functional. While ceramic capacitors are fairly robust and do not fail often, they can and do sometimes fail. However, in this case, all of them tested OK, although there were two ceramic discs that were installed in a placement that nowadays is considered unsafe. More about them later.
I decided to test the dual filter capacitor for leakage, first in-circuit, which led to failed tests. I then tested the unit out-of-circuit, and once again found that both capacitors in the device had failed in a very leaky condition.
|
I used my homebrewed capacitor leakage tester for testing the electrolytics, and it showed exactly what I thought that it might, what with the age of the dual capacitor. Needless to say, I replaced the dual capacitor with a pair of modern 20µF 150V axial-type electrolytics. After installation of the capacitors (Figure 3), the unit powered up and remained operational even in the pre-amp active mode of operation.
|
Now that the unit was operational, I went back to the two capacitors that I mentioned earlier as being installed in an unsafe manner. A few words about this topic are called for here.
It has long been a common practice to install ceramic capacitors in various configurations across the incoming AC power line to certain mains-powered electronic equipment. There are basically two different connection schemes that are widely used, an “X” scheme and a “Y” scheme.
In the “X” scheme, the capacitor is connected across the incoming AC line, from the Line lead to the neutral lead. In the “Y” scheme, the capacitor is connected from one or both of the incoming power lines to chassis ground, i.e., from the line lead to chassis ground and from the neutral lead to chassis ground. The safety risks of such capacitors are evident if one considers the capacitor failing in a shorted condition.
In the event of the “X” connected capacitor, this would create a direct short circuit across the incoming line cord, most likely blowing any fuse or tripping any circuit breaker that is hopefully present in the circuit. In those circuits without an overload protection device, the end result is a blown fuse or circuit in the service panel. In the event of the “Y” connected capacitor, failing shorted would most often result in a hot chassis, leading to an extreme shock hazard to the user of the equipment.
Nowadays, we have a device known as a “safety capacitor”, which is designed to fail open rather than shorted. These devices carry certain ratings that indicate the level of protection afforded by the capacitors.
Table 1 shows the rating values for “X” connected safety capacitors, while Table 2 shows similar rating values for “Y” connected safety capacitors. The safety capacitors that I typically use are 0.01µF X1-440V/Y2-300V ±20% Y5V-type ceramic disc safety capacitors. The capacitors originally installed in the Ameco PT Preamplifier were 0.01µF 150VAC/1400VDC Z5U-type ceramic discs, and there were as already mentioned two of them, connected in the “Y” configuration from each of the AC line leads to chassis ground. As these capacitors are not safety types, and are therefore just as likely to fail shorted as they are to fail open, they needed to go.
|
Once the new safety capacitors were installed (Figure 4), the unit was tested for proper operation one more time, and then the job was considered finished. I put the cover back onto the chassis and tied up the connected cables for return to Darrell. So...what lessons can be learned from this repair? Once again, it is the capacitors that |
almost always seem to be the earliest failure items in most electronic circuits. In a way, that makes sense, as thecapacitors are the only components that have internal materials or structures that are guaranteed to deteriorate over time. Now, I am speaking about the electrolytics here, of course. But, if one looks back at my last dozen or so At The Repair Bench articles, how many of them came down to capacitor failures? I think that you will get the point.
See you next month!
See you next month!
Heathkit® IT-3121 Semiconductor Curve Tracer Redux
May 2025
|
Back in February of this year, I reported on a Heathkit® IT-3121 Semiconductor Curve Tracer (Figure 1) that had come in for repair. That turned out to be a simple matter of shorted electrolytic capacitors in the low-voltage power supplies. I repaired it and shipped it back to its owner, and collected my fee.
Here we are, three months later, and another IT-3121 has landed on my bench for repair, from a different owner, but one who was referred to me by the owner of the first IT-3121 that I reported on back in February. This unit |
had a different apparent condition. It was blowing fuses as soon as it was powered on, without even a flicker of the panel-mounted neon pilot lamp. Tracking down a problem like this can be extremely difficult, as there are no working voltages to be measured, and all diagnosis must therefore be done without reference to voltages. Instead, we tend to look towards resistances in these situations.
So… how and where to start? The Heathkit® IT-3121 Assembly and Operation Manual provides a starting point in that the manual offers some “Initial Checks” which are to be performed by the individual assembling this instrument, prior to the first power-up of the unit. These checks are located in the Tests and Adjustments section of the manual, and they call for resistance measurements at specific points in the power supplies, measuring from those points to chassis ground in the form of the black banana jack on the instrument’s rear panel.
So… how and where to start? The Heathkit® IT-3121 Assembly and Operation Manual provides a starting point in that the manual offers some “Initial Checks” which are to be performed by the individual assembling this instrument, prior to the first power-up of the unit. These checks are located in the Tests and Adjustments section of the manual, and they call for resistance measurements at specific points in the power supplies, measuring from those points to chassis ground in the form of the black banana jack on the instrument’s rear panel.
The first measurement is from a point identified as “Point 1”, which is in essence the input to the positive-going low-voltage supplies, at the DC side of the full-wave bridge rectifier formed by diodes D5 through D8 (Figure 2), which is common to the positive side of a 200µF/50V electrolytic filter capacitor C5. The specified resistance is to be at least 10kΩ from that point to chassis ground, with the positive probe of the ohmmeter at Point 1. The reading taken was 15.6kΩ, meeting the provided specification.
Next is the measurement taken at “Point 3”, which is at the DC side of the full-wave bridge rectifier comprised of diodes D1, D2, D15, and D16 (Figure 3). The resistance between Point 3 and chassis ground, measured with the positive probe of the ohmmeter on Point 3, is to be at least 100kΩ. It measured 221.5kΩ, again within specified limits.
The third resistance measurement was to be taken with the probes reversed, placing the positive probe on chassis ground and the negative probe on “Point 2”. This point is located at the negative output of the low-voltage supply’s full-wave bridge rectifier (the same rectifier used when measuring Point 1 above). This point is then effectively at the negative end of the 200µF/50V electrolytic capacitor C8 (Figure 4), and it too called for a minimum of 10kΩ between that point and chassis ground. The actual reading was 17.3kΩ, making this one compliant as well.
These tests are designed to locate any direct short circuits present in the power supplies of the IT-3121, and all of the tests showed proper and normal conditions to exist. So… what’s next? I decided to isolate the power transformer, to verify that the problem was not a shorted primary in the transformer. To do this, I de-soldered and removed all of the transformer secondary leads from the printed circuit board (PCB). Upon power-up, the unit showed life in that the pilot lamp would now illuminate and the fuse would not blow. This meant that the transformer primary winding was not shorted and therefore not the cause of the problem.
In order to narrow down the location of the problem to a specific area of the unit, I decided to re-connect the transformer secondaries one circuit at a time. I first connected the low-voltage power supply input leads, a pair of blue wires and a blue with white tracer. The two blue leads were the two ends of that secondary winding, while the blue/white wire was the winding center tap, going to chassis ground. When powered up now, the low-voltage power supplies were all operational and the unit remained on. No problem there.
This caused me to take a good look at the sweep circuits and their associated transformer secondary leads. Starting out, I wanted to eliminate the supply to the sweep circuit FWBR, which were the green, the white, and the green with white tracer wires (Figure 4). I reconnected those three wires and powered the unit up. Once again, the unit held, with outwardly normal indications. That left, by process of elimination, the remaining wire pair, the red and yellow wires, which are connected to the two extreme ends of the sweep supply secondary winding.
These tests are designed to locate any direct short circuits present in the power supplies of the IT-3121, and all of the tests showed proper and normal conditions to exist. So… what’s next? I decided to isolate the power transformer, to verify that the problem was not a shorted primary in the transformer. To do this, I de-soldered and removed all of the transformer secondary leads from the printed circuit board (PCB). Upon power-up, the unit showed life in that the pilot lamp would now illuminate and the fuse would not blow. This meant that the transformer primary winding was not shorted and therefore not the cause of the problem.
In order to narrow down the location of the problem to a specific area of the unit, I decided to re-connect the transformer secondaries one circuit at a time. I first connected the low-voltage power supply input leads, a pair of blue wires and a blue with white tracer. The two blue leads were the two ends of that secondary winding, while the blue/white wire was the winding center tap, going to chassis ground. When powered up now, the low-voltage power supplies were all operational and the unit remained on. No problem there.
This caused me to take a good look at the sweep circuits and their associated transformer secondary leads. Starting out, I wanted to eliminate the supply to the sweep circuit FWBR, which were the green, the white, and the green with white tracer wires (Figure 4). I reconnected those three wires and powered the unit up. Once again, the unit held, with outwardly normal indications. That left, by process of elimination, the remaining wire pair, the red and yellow wires, which are connected to the two extreme ends of the sweep supply secondary winding.
Knowing that the problem had to be in the circuit fed by those wires, I left them disconnected and went to work with the ohmmeter. The red and green wires supply incoming AC current to a half-wave rectifier comprised of diodes D3 and D4. According to the schematic, a 0.22µF capacitor C3 (Figure 5) is placed in shunt across this rectifier assembly as a filter device. A look at the PCB in the unit showed that somebody had been in here working on the board. This was very obvious because the 0.22µF capacitor was not there, but instead there was a pair of 0.1µF/100V metallized polyester film capacitors placed together in parallel. With the secondary leads disconnected, I should have been able to measure the capacitance of that parallel pair, and it should have showed an initially low resistance, immediately climbing high to an open circuit condition. What actually happened, however, is that the capacitance meter errored out, and the ohmmeter showed a direct short circuit when placed across the capacitor pair. I removed the two capacitors and separated them for individual testing, and found what I expected to find at that point. One of the two capacitors tested out normally, while the other one was shorted. A new 0.22µF Mylar™ capacitor, rated at 630 volts, solved the problem. With the new capacitor in place and the secondary leads reconnected, the unit powered up and almost worked properly.
It turned out that someone, possibly the same person, had also replaced an “Offset” trimmer potentiometer (Figure 6) that is mounted to the foil side of the PCB. The original trimpot there was a four-legged horizontal-mount 0.688” single-turn 10kΩ pot, but that had been replaced by an enclosed trim pot with a 0.375” square body and short wire leads. These leads had been extended, and only one of them was actually still connected. Two of the three leads had broken free of their apparent cold-solder joinery. This trimpot is used as a null-offset balance control for balancing the input voltages on a 741 operational amplifier IC. Without this control in place and properly adjusted, the output from the curve tracer is unpredictable at best. I happened to have a Bourns 3352U-1-103 trimpot in stock, which just so happens to be the same size, value, and type as the factory part for this application. Needless to say, that component went in as a replacement for the improperly-installed trimpot that was there. This restored proper operation of the op-amp circuit and thus the curve tracer in general.
Because of the early 1980’s date codes on the electrolytic capacitors in this unit, I decided to replace them as a precautionary measure while I had it on the bench. This involved the replacement of nine capacitors, five of the radial type, and four axial devices. They were all in-stock parts as well.
Total time on the bench for this repair was about an hour. It seemed as if it might be a dog of a repair at first look, but in reality, it turned out to be a simple and straight-forward diagnosis and repair. Once again, it was a simple matter of thinking through the problem, studying the schematic, and understanding the circuits involved. In this manner, only those parts that have actually failed - or can be expected to fail in the near future - are replaced as a part of the repair.
See you next month!
Because of the early 1980’s date codes on the electrolytic capacitors in this unit, I decided to replace them as a precautionary measure while I had it on the bench. This involved the replacement of nine capacitors, five of the radial type, and four axial devices. They were all in-stock parts as well.
Total time on the bench for this repair was about an hour. It seemed as if it might be a dog of a repair at first look, but in reality, it turned out to be a simple and straight-forward diagnosis and repair. Once again, it was a simple matter of thinking through the problem, studying the schematic, and understanding the circuits involved. In this manner, only those parts that have actually failed - or can be expected to fail in the near future - are replaced as a part of the repair.
See you next month!
Yaesu CD-41 Lithium-Ion Battery Rapid Charge Cradle
April 2025
|
A while back, one of my fellow Club members John O’Connell K2QA brought a unit to me for repair of a strange condition. The unit was a Yaesu CD-41 lithium-ion battery rapid charge cradle (Figure 1). John has a couple of these devices, which are used to charge the batteries on several different Yaesu handheld transceiver models, including the FT-2 and FT-3 radio families. The problem that was exhibited by one of his charging cradles was that under any operating conditions at all, the green Fully Charged indicator LED would remain illuminated, and the cradle would fail to charge any battery placed into it.
|
This charging cradle uses a three-contact system for monitoring and charging the battery. One of the three contacts connects to the battery positive terminal, one connects to the battery negative terminal, and the third contact connects to a battery monitor terminal. This third contact is key to the charging process, as it transmits the battery condition to the charger, allowing the charger to decide if and how to flow a charge current into the connected battery.
Not having any factory service or support documentation for the CD-41, I followed my normal routine of first drawing out a schematic diagram of the unit (Figure 2). Then, using the new schematic, I was easily able to break the complete unit down into its functional blocks, which include :
Let’s take a quick look at just what each of these individual sections or blocks actually does in the overall circuit, starting with the power input section. The power input area provides a convenient connection point to the printed circuit board (PCB) for the current from the regulated “wall-wart” type of power supply, which is critical to the operation of the CD-41. Of the two cradles that John left with me, the specification labels are marked slightly differently. One of them (the operational one) is labeled as Input : DC 12 (10.5) - 16V 600mA and as Output: DC 8.4V 600mA. The second (failed) unit was labeled as Input : DC 12 - 16V 600mA and as Output: DC 8.4V 600mA. What makes this something that I would discuss is the fact that the operational unit is paired with a regulated power supply (Yaesu Model SAD-25) rated at 10.5V 1.0A for its output, while the failed unit is paired with a different regulated power supply (Yaesu Model SAD-24) rated at 12.0V 0.5A for its output.
The next functional block is the output regulation and isolation section. This consists largely of a 4.7Ω 3W wirewound resistor, a 2SA2183 PNP silicon power transistor, and a DD1031 isolation diode. The transistor controls the current flow into the battery when it is turned on, with the flow depending upon the degree to which the transistor is biased “on”. The diode prevents draining the battery back into the charging circuit if the battery is left on the charger after charging.
Next up is the annunciator section. This section consists of two LED’s, one red and the other green, a pair of transistors to switch the LED’s on or off, some resistors, and a 470µF electrolytic capacitor. The green LED is supposed to illuminate gradually, as the 470µF capacitor charges up, once the battery has reached full charge and the charge current is switched off. The red LED is meant to illuminate while the battery is charging, with its steady-on state changing over to a flashing state as the battery nears full charge.
The over-voltage protection circuit includes two transistors configured to form a Darlington pair, as well as a 12V Zener diode and several resistors. Its job is to prevent overcharge of the battery and over-current and over-voltage conditions throughout the charger.
Finally, we come to the battery sensing circuit. This section includes a P-channel enhancement-mode MOSFET, some more resistors, and a 6V Zener diode. The task set for this circuit is to measure and monitor the battery voltage, and then to trigger the series pass 2SA2183 transistor in response to battery conditions. It is this circuit that is the Achilles’ heel of this charger.
The MOSFET, which is an extremely static-sensitive device, is installed in such a manner that the user can come into contact with the MOSFET source terminal quite easily, thus imparting an electrostatic discharge from the user directly into the MOSFET. Such ESD will very easily pierce the insulating oxide layer within the MOSFET, causing immediate failure of that device.
- A power input section
- An output regulation and isolation section
- An annunciator section
- An over-voltage protection section
- A state-of-charge monitoring section
Let’s take a quick look at just what each of these individual sections or blocks actually does in the overall circuit, starting with the power input section. The power input area provides a convenient connection point to the printed circuit board (PCB) for the current from the regulated “wall-wart” type of power supply, which is critical to the operation of the CD-41. Of the two cradles that John left with me, the specification labels are marked slightly differently. One of them (the operational one) is labeled as Input : DC 12 (10.5) - 16V 600mA and as Output: DC 8.4V 600mA. The second (failed) unit was labeled as Input : DC 12 - 16V 600mA and as Output: DC 8.4V 600mA. What makes this something that I would discuss is the fact that the operational unit is paired with a regulated power supply (Yaesu Model SAD-25) rated at 10.5V 1.0A for its output, while the failed unit is paired with a different regulated power supply (Yaesu Model SAD-24) rated at 12.0V 0.5A for its output.
The next functional block is the output regulation and isolation section. This consists largely of a 4.7Ω 3W wirewound resistor, a 2SA2183 PNP silicon power transistor, and a DD1031 isolation diode. The transistor controls the current flow into the battery when it is turned on, with the flow depending upon the degree to which the transistor is biased “on”. The diode prevents draining the battery back into the charging circuit if the battery is left on the charger after charging.
Next up is the annunciator section. This section consists of two LED’s, one red and the other green, a pair of transistors to switch the LED’s on or off, some resistors, and a 470µF electrolytic capacitor. The green LED is supposed to illuminate gradually, as the 470µF capacitor charges up, once the battery has reached full charge and the charge current is switched off. The red LED is meant to illuminate while the battery is charging, with its steady-on state changing over to a flashing state as the battery nears full charge.
The over-voltage protection circuit includes two transistors configured to form a Darlington pair, as well as a 12V Zener diode and several resistors. Its job is to prevent overcharge of the battery and over-current and over-voltage conditions throughout the charger.
Finally, we come to the battery sensing circuit. This section includes a P-channel enhancement-mode MOSFET, some more resistors, and a 6V Zener diode. The task set for this circuit is to measure and monitor the battery voltage, and then to trigger the series pass 2SA2183 transistor in response to battery conditions. It is this circuit that is the Achilles’ heel of this charger.
The MOSFET, which is an extremely static-sensitive device, is installed in such a manner that the user can come into contact with the MOSFET source terminal quite easily, thus imparting an electrostatic discharge from the user directly into the MOSFET. Such ESD will very easily pierce the insulating oxide layer within the MOSFET, causing immediate failure of that device.
It did not take very long to isolate and identify the MOSFET as the failed component in this situation, circled in red in the Figure 3 illustration of the charger PCB. Some basic voltage and resistance measurements at various points around the overall circuit was all that it took. When all voltages in the other functional blocks turned out to be as expected, the problem was quickly narrowed down to the state-of-charge monitoring section of the circuit, and then to the MOSFET.
Interestingly enough, this was apparently a problem that became known to the engineers at Yaesu, as the second CD-41 that John left with me used a different part number for the MOSFET, which may or may not be meaningful. However, something that was very meaningful was the fact that that second CD-41 also had a P6KE18A transient voltage suppressor (TVS) diode connected across the MOSFET, from the battery sensing contact to the ground contact, for the purpose of ESD protection.
Ultimately, the repair of this charger involved replacement of the failed MOSFET, which I did by installing an IRLML6402TRPBF P-channel enhancement-mode MOSFET in place of the original 2SJ204 type, which is no longer available. The second CD-41 uses an STJ828K device, but I had the 6402 on hand and its specs were right, so I did not even attempt to source the STJ828K. Of course, no proper repair fails to include a fix for the underlying problem, so I made sure to install a P6KE18A diode across the MOSFET, circled in yellow in the Figure 3 illustration, thus providing the same level of ESD protection that the second CD-41 had from the factory.
Post-repair, the cradle successfully charges the battery, and the annunciator LED’s work as expected, but only to a certain limit, which I attribute to the difference between the original MOSFET used and the replacement device that I installed. While the red LED glows during charging, and blinks or flickers as the battery nears full charge, and the green LED illuminates at the fully charged point, the green LED nonetheless turns off after a certain period of time. From testing that I performed, I believe that this new MOSFET provides the proper charge current, but shuts down the charging circuit completely when the charge state is full, thus turning off the LED. The original MOSFET maintained a “holding” charge current after full charge was reached.
The upshot of this job is that it illustrates how sometimes, failure is designed into a piece of equipment, and a proper repair will correct for the poor design as well as replace the failed component parts.
See you next month!
Interestingly enough, this was apparently a problem that became known to the engineers at Yaesu, as the second CD-41 that John left with me used a different part number for the MOSFET, which may or may not be meaningful. However, something that was very meaningful was the fact that that second CD-41 also had a P6KE18A transient voltage suppressor (TVS) diode connected across the MOSFET, from the battery sensing contact to the ground contact, for the purpose of ESD protection.
Ultimately, the repair of this charger involved replacement of the failed MOSFET, which I did by installing an IRLML6402TRPBF P-channel enhancement-mode MOSFET in place of the original 2SJ204 type, which is no longer available. The second CD-41 uses an STJ828K device, but I had the 6402 on hand and its specs were right, so I did not even attempt to source the STJ828K. Of course, no proper repair fails to include a fix for the underlying problem, so I made sure to install a P6KE18A diode across the MOSFET, circled in yellow in the Figure 3 illustration, thus providing the same level of ESD protection that the second CD-41 had from the factory.
Post-repair, the cradle successfully charges the battery, and the annunciator LED’s work as expected, but only to a certain limit, which I attribute to the difference between the original MOSFET used and the replacement device that I installed. While the red LED glows during charging, and blinks or flickers as the battery nears full charge, and the green LED illuminates at the fully charged point, the green LED nonetheless turns off after a certain period of time. From testing that I performed, I believe that this new MOSFET provides the proper charge current, but shuts down the charging circuit completely when the charge state is full, thus turning off the LED. The original MOSFET maintained a “holding” charge current after full charge was reached.
The upshot of this job is that it illustrates how sometimes, failure is designed into a piece of equipment, and a proper repair will correct for the poor design as well as replace the failed component parts.
See you next month!
Yaesu FT-65 HT Dual-Band Transceiver - March 2025
|
Sometimes, repairs will come in that are not actually “repairs” at all, although they seem to be to the owner of the equipment of concern. That was exactly the situation with a recent “repair” to a Yaesu FT-65 Handheld Dual-Band Transceiver (Figure 1).
The unit was brought to me during the 2024 Hamfest, and its owner demonstrated that the transceiver would apparently not transmit when the PTT switch was activated. There is some history of these radios losing microphone connectivity, especially after being dropped, so I agreed to take a look at the unit. When I put it on the bench, I attempted to verify the complaint, as I normally do. The radio was tuned to 147.180MHz, and it was set in the automatic repeater mode with the correct offset, so when keyed, the display showed full power and a frequency of 147.780MHz. Further, the CTCSS tone was set to 131.8Hz, the correct value for the repeater to which the radio was tuned. Sure enough - although the radio showed full signal output on the LCD panel, nothing was received and passed on by the repeater. |
However, the fact that the repeater was not responding was not conclusive that there was no radio RF output… just that it was not making the trip through that repeater. I decided to experiment a bit, and I set the radio to transmit on a separate simplex frequency outside of the normal repeater frequency range. Immediately, the signal was received by a nearby receiver tuned to the same simplex frequency. This conclusively showed that the radio did in fact produce an RF output and put it on the air.
That fact caused me to look more deeply into the various settings in the repeater configurations of the radio. The first thing that I did was to connect the radio to a PC via a programming cable and back up the existing configuration. Then, I took a look at what was shown in the downloaded data from the radio. What I found was surprisingly simple… the squelch mode was set to “OFF”.
I disconnected the radio from the PC and went into the menu system to make some changes manually. As soon as I set the squelch mode to “TSQL” (tone squelch), the unit came up as expected on the repeater.
I tested a bit further by programming in some additional repeaters and testing them. All, of course, worked properly and the signal was successfully received and repeated by each of the test repeaters so programmed. I then cable-connected the radio again and did some programming via the PC… enough to once again verify proper operation of the radio on both the VHF and the UHF bands.
To finish up after all of the testing was complete, I reset the radio to factory settings and then re-programmed the frequencies that were in memory when I received the unit by restoring the backed-up configuration to the radio. Finally, I once again manually set the TSQL value again, and the job was done.
This was a case of simple mis-configuration of the radio. Interestingly enough, the owner, in a subsequent conversation, informed me that he had just obtained a programming cable for the radio, and would be programming the set via his computer when he got the radio back. Had the original programming been done via the computer instead of being done manually, where each separate step must be accomplished individually, the problem most likely would not have occurred. Setting the squelch mode is a routine component of the computerized programming process.
So then… what is the primary “take-away” from this story? If anything, it is that the devil is in the details, and that we cannot assume a malfunction just because we do not immediately get the results that we anticipate. When things do not seem to work properly, go back to basics and check everything, especially all modes of operation that are available. It may well turn out that there is no actual failure.
Heathkit® IT-3121 Curve Tracer - February 2025
|
Every now and then, a piece of equipment comes in as an unsolicited repair job, wherein the owner has been directed to me either by a friend, another ham, or via my website, www.ad2cs.com. This was one of those cases, where a friend of a friend sent this guy to me. He shipped an older (circa 1980) Heathkit® IT-3121 Semiconductor Curve Tracer for repair if possible. I sort of chuckled at that last caveat - “if possible” - because to my way of thinking, anything is repairable, but it may not always be practical or cost-effective to do so. There is almost always a method by which an older piece of equipment can be made operational again, if the owner wants to spend the “do-re-mi” that it would take. |
In the situation at hand, this was a piece of test apparatus that would not operate as intended. The specific complaint was that although the pilot light would illuminate, there was no output from this unit when connected to an oscilloscope.
A brief explanation is called for here. This tester is actually a curve tracer adapter rather than a full curve tracer in its own right. This device is designed to apply the operational voltages and current to the semiconductor device under test (DUT), and then to process the output into usable input signals for display on an oscilloscope. The oscilloscope connections for both X and Y (horizontal and vertical) are on the rear panel of the IT-3121. The owner’s complaint was that he was getting no output to the oscilloscope when the DUT was installed to the banana jacks used as the test jacks on this unit.
A quick look at the schematic revealed that the IT-3121 has two separate internal power supplies, one of which is identified as the low-voltage supply, leaving the technician to assume that the opposite supply (the sweep supply) is a high-voltage supply. In fact, that supply provides output voltages as high as 200 volts. It also supplies AC to the neon lamp used as the pilot lamp, which tells part of the story of this unit.
The fact that the pilot lamp was working simply meant that the incoming line voltage, the power switch, the main fuse, and the transformer primary winding were all intact, and it indicated that the HV supply secondary was also intact. This shifted my focus to the low-voltage power supply in the search for the problem. Some voltage measurements showed that there were definitely some problems in the low-voltage supply. Specifically, the +5VDC, +15.5VDC, and -16.1VDC supplies were all missing. In fact, the only low-voltage supply that seemed to be present was the -15.5VDC supply.
A look at the schematic in this area (Figure 2) showed some likely candidates, so I set about taking some more measurements. The positive output of the full-wave bridge rectifier (or the collector of transistor Q13) should have measured about +22 volts, but this point in fact measured zero volts, meaning it was grounded. The most likely candidate here was the 200µF/25V axial electrolytic capacitor C5, whose job is to smooth the pulsating rectifier output somewhat. I opened this capacitor circuit, and voltage was restored at the Q13 collector. Replacing that shorted capacitor restored both the +15.5VDC and the +5VDC supplies. I used a 50-volt rated capacitor as the replacement - more about why shortly.
Now for the -16.1VDC supply. In this case, I began by measuring the voltage at the collector of transistor Q15, and once again found it to be 0VDC, indicating that it was grounded and that Zener diode D18 was effectively bypassed. Once again, we were looking at a shorted capacitor, in this case, the culprit was the 50µF/25V axial electrolytic capacitor C9. As before, replacing the shorted capacitor resulted in the -16.1VDC supply coming back to life.
This entire unit uses only nine polarized capacitors, all aluminum electrolytics. There are four 10µF/25V radial types (C11, C12, C13, and C14) - all in the step generator circuit. There are two of the 200µF/25V axial types, one in each of the two low-voltage power supply sections, the positive supply and the negative supply. There are two of the 50µF/25V axial types, again one in each of the two low-voltage power supply sections, and finally one rated 100µF/35V, placed in the +5VDC part of the positive low-voltage power supply. Based on the age of this unit and therefore the associated ages of these electrolytic capacitors, I decided that it was worth replacing all of them with new.
Note that the 200µF capacitors were rated 25V, and are used in ±22VDC circuits. Depending upon specific component tolerances and actual line voltage levels, these capacitors may have been operated at a point in excess of their rated voltage limits. For this reason, I elected to upgrade these capacitors to 50-volt types instead of the original 25-volt rating. In fact, in all cases, the working voltages of the capacitors were increased, partly due to smaller modern component sizes and my desire to keep to the components of the same approximate physical size so that they fit the PCB placements properly.
With all of the capacitors replaced, I did a quick clean-up of the unit, and then I put it through some actual-use testing to verify its functionality. All was as it should have been, so I called this job “done!”
This was one of those simple jobs that come in occasionally, and it is one that was extremely easy to diagnose so long as one thinks through the conditions. What works? What doesn’t work? How is that condition verified? Then, finally, what could cause that problem? Think it through, evaluate the schematic, check your thinking with a multimeter, and it’s all over.
Now for the -16.1VDC supply. In this case, I began by measuring the voltage at the collector of transistor Q15, and once again found it to be 0VDC, indicating that it was grounded and that Zener diode D18 was effectively bypassed. Once again, we were looking at a shorted capacitor, in this case, the culprit was the 50µF/25V axial electrolytic capacitor C9. As before, replacing the shorted capacitor resulted in the -16.1VDC supply coming back to life.
This entire unit uses only nine polarized capacitors, all aluminum electrolytics. There are four 10µF/25V radial types (C11, C12, C13, and C14) - all in the step generator circuit. There are two of the 200µF/25V axial types, one in each of the two low-voltage power supply sections, the positive supply and the negative supply. There are two of the 50µF/25V axial types, again one in each of the two low-voltage power supply sections, and finally one rated 100µF/35V, placed in the +5VDC part of the positive low-voltage power supply. Based on the age of this unit and therefore the associated ages of these electrolytic capacitors, I decided that it was worth replacing all of them with new.
Note that the 200µF capacitors were rated 25V, and are used in ±22VDC circuits. Depending upon specific component tolerances and actual line voltage levels, these capacitors may have been operated at a point in excess of their rated voltage limits. For this reason, I elected to upgrade these capacitors to 50-volt types instead of the original 25-volt rating. In fact, in all cases, the working voltages of the capacitors were increased, partly due to smaller modern component sizes and my desire to keep to the components of the same approximate physical size so that they fit the PCB placements properly.
With all of the capacitors replaced, I did a quick clean-up of the unit, and then I put it through some actual-use testing to verify its functionality. All was as it should have been, so I called this job “done!”
This was one of those simple jobs that come in occasionally, and it is one that was extremely easy to diagnose so long as one thinks through the conditions. What works? What doesn’t work? How is that condition verified? Then, finally, what could cause that problem? Think it through, evaluate the schematic, check your thinking with a multimeter, and it’s all over.
Icom IC-746 PRO Transceiver - January 2025
|
Recently, I wrote about the repair of an Icom IC-756 PRO, wherein I replaced the VFO encoder. I had no sooner returned that radio to its owner when that individual presented me with another radio for repair. This time, it was an Icom IC-746 PRO (Figure 1), and the failure was in the realm of a lack of output signal from the radio as a whole. |
The IC-746 PRO is a 160m to 6m plus 2m all-mode transceiver. When tested for output, it was found that the transmit power was nil on all bands and in all modes. The internet is full of stories about such or similar failures on this family of Icom transceivers. There are some similarities among these web reports, with the most common cause being related to the failure of a component identified by Icom as IC151 and referenced in the Service Manual as the wide-band YGR Amplifier. The conventional wisdom holds that this IC, which is an MMIC device, typically fails due to excessive heat being experienced by the IC. Investigation of this unit showed that the failures in this case went beyond the YGR amplifier, and affected the pre-driver transistor and both driver transistors.
|
The YGR amplifier, as already mentioned, is a surface-mount MMIC device carrying a part number of µPC1678G (Figure 2). The pre-driver is a silicon NPN power transistor in a TO-220 case. This transistor, a type 2SC1971, is obsolete and is extremely difficult to find. Fortunately, there is a suitable replacement still available, though in very limited quantities. The NTE-342 transistor is a good match and will serve nicely in place of the original 2SC1971 transistor. One of the factors that makes for difficulty in finding a suitable replacement for the 2SC1971 is not the operating voltages of the device; instead, it is the fact that this |
device has an unusual physical arrangement in that the center pin and tab are emitter-connected rather than the much more common collector-connected tab arrangement.
The driver transistors are a pair of 2SK2975 surface-mount N-channel enhancement-mode power MOSFET’s. These transistors are mounted to a small daughter board that is equipped with a large heat-sinking metal base, directly to which the source connection is made through holes in the daughter board. The gate and drain connections are made to SMT pads on the top side of this board. We will discuss replacement of these transistors a bit more later on.
Replacement of the YGR amplifier IC is best done with the board on which it is installed having been removed from the chassis. This is the board identified by Icom as the RF Unit, and the IC is installed in the vicinity of the mounting hole identified as Hole 4, near one corner of the board.
Removal of this IC is most easily done simply by first cutting two three-eighths-inch-long pieces of bare 22 AWG wire. Lay each of these wire lengths across the IC leads on each side of the device, and solder them freely to the leads. Then, apply the heat of the soldering iron to the wire lengths, one at a time, and heat the wire until the solder all along the wire has melted. At that point, gently lift that side of the IC using the tip of a pick or a fine tweezer. Lift it carefully, and just enough to keep it free of the solder puddle. Repeat the heat-and-lift operation on the opposite side of the IC, and the part will be free. Clean up the pads with some solder wick and then with some 99.9% isopropyl alcohol (IPA). After the clean-up is done, tin the pads lightly with some fresh solder, in preparation for the placement of the new IC. This removal method is a useful trick for removing many multi-pin devices from a PCB, and can be used with a wide variety of device types.
|
After installation of the new IC, a solid copper machined heatsink was attached to the IC (Figure 3) to protect it against heat during future operation of the radio. Next to be replaced was the Pre-driver Transistor (Figure 4). This was a straight-forward component replacement, except that in this installation, the transistor leads are not passed through the PCB, but instead are clipped short and are soldered to pads on the PCB top surface. The mounting tab of this transistor is secured directly to the radio chassis through a hole in the PCB, a design feature intended to remove heat from the transistor. However, as the chassis is beneath the transistor and heat naturally moves upward, the cooling efficiency is not as great as it could be. To that end, a heatsink identical to the one installed to the YGR amplifier IC was installed to the body of the Pre-driver Transistor (Figure 5) after the new transistor was installed. Replacement of the driver transistors on their Daughter Board (Figure 6) required removal of the board from the chassis. This was a simple matter of desoldering four sets of four pins and removing two screws. While the transistors were the only items needing replacement on this board, it was actually easier to clear the board of all components and to start with a clean board. This board holds a total of twelve surface-mount passive devices. These included (2) 100Ω 0805 resistors, (4) 1Ω 0805 resistors, (1) 150Ω 0805 resistor, (2) 68Ω 2512 resistors, (2) 0.1µF 0805 capacitors, and (1) 22pF 0805 capacitor. The reason that it was best to wipe the board clean was because of the high heat developed in the heatsink first in removing and then in installing the driver |
transistors. The heat of removal was sufficient to “float” the nearby components.
Once the board was stripped and cleaned, paste solder and liquid flux were applied to the board and heatsink, after which the driver transistors, one at a time, were installed, soldering them in place via the application of focused hot air. Then, it was a simple matter to replace the passives, using the hot tweezers to install each of those devices.
With all of the failed parts replaced, it was time for the post-repair testing of the radio, followed by an alignment and tweaking job to ensure maximum performance. On delivery back to its owner, the radio performed flawlessly, making for a very satisfied customer.
Repairs of this nature can be time-consuming, but what really took the most time on this one was locating the correct replacement parts. Many of the components used in radios of this period are now obsolete and are quite difficult to source. I was very lucky, and as such, I brought in sufficient quantities to permit repair of several more radios of this type.
Take the time to research the parts carefully, and then only buy when you are sure that you are buying the right items. Then check those parts carefully against their datasheets to ensure that you have received what you expected to get. For example, I actually received and returned a set of bogus 2SC1971 transistors that had their pin assignments different from what the real 2SC1971 should have been.
Persistence and perseverance will carry the day. See you next month.
Yaesu G-2700XDS Azimuth Rotator System - December 2024
|
As my regular readers are well aware, I enjoy taking on the oddball repairs and the repairs that other shops will not or cannot handle. Sometimes that penchant for the unusual will bite me, but for the most part, it has led to some interesting repair case histories. This one is no different.
I was asked by a regular customer to take a look at his Yaesu G-2700XDS Azimuth Rotator System (Figure 1) due to the fact that there is no motion indication on the panel meter of the controller. |
He brought me the motion unit, the G-2700 controller, and a second G-1000 controller. He had experimented with the second controller, and had gotten a limited response on the meter of that controller, about a 90° swing, but it only occurred one time and he could not get it to repeat the behavior.
It must be understood that the positional display on the panel meter of the Yaesu rotators (and many others as well) is a co-operative effort between components inside the controller and components inside the motion unit. In a nutshell, there is a potentiometer inside the motion unit that is driven through a gearing arrangement that is connected through to the motor and its driven gear. There are multiple levels of reduction in both directions before we ever get to the potentiometer drive gear, and the gearing must be such to allow the full amount of rotator motion within a single swing of the potentiometer from one limit to the other. This is very important with some models of rotator, especially with those that have a turn and a quarter (450°) or a turn and a half or 540° of motion from limit switch to limit switch. The entire amount of that degree of rotation must occur within - and actually less than - a single rotation of the potentiometer, which in and of itself does not have a full 360° of rotational range between its stops.
The relationship between the potentiometer drive and the position of the rotating element is established through the various gears used in the drive system. There are a couple of important points to understand when assembling one of these units, however, that are related to the potentiometer. The first is that we must determine where the center-point of the unit rotational travel will be and position the unit in alignment with that center point when installing it. The second is that we must also determine where the mid-point of the potentiometer’s rotational range is located and position the potentiometer at that mid-point for the assembly of the unit. It is only when both the motion system and the potentiometer are oriented at the centers of their rotational ranges that we can be assured of proper timing between the motion unit and the potentiometer.
As a result of all of this, a varying voltage signal is available on one of the wire leads from the motion unit to the controller. The harness cable between the two units generally contains six wires, distributed as below :
The potentiometer wiper lead is where we will find the varying voltage that indicates the relative position of the motion unit between its limits of motion. A nominal 6VDC is supplied to the potentiometer, being connected to one end of the potentiometer, while the opposite end of the potentiometer is connected to the system ground. The voltage on the potentiometer wiper will vary as the potentiometer rotates with the rotation of the motion unit, and that varying voltage is the input signal to the controller for driving the meter.
With this in mind, it should make sense that if we monitor that wiper lead while the motion unit rotates, we would expect to find a varying voltage available there. If there is no voltage, we have either a failed supply to the potentiometer, a failed (open) potentiometer, or an open circuit in one or more of the potentiometer’s leads. If we measure a fixed voltage there while the motion unit rotates, we have a potentiometer that is either not being driven due to a failure in the drive system, or we have a seized potentiometer that cannot rotate.
In most of the Yaesu rotators, the potentiometer drive gear is a nylon gear that is fastened to the potentiometer shaft by way of a set-screw installed into the gear hub. In many units, this nylon gear is directly driven by one of the motion system gears. However, in the G-2700, there is a different arrangement for driving the potentiometer gear. In this design, the unit gearing drives a stamped steel gear that is mounted to a short shaft. That shaft extends through the motor mounting plate into the lower area of the rotator housing, where the potentiometer is installed. The lower end of that shaft has a small quill gear secured to the shaft, and it is that quill gear that in turn drives the potentiometer gear. As a result, when first opening up the motion unit, the potentiometer and its drive gear are hidden, out of sight below the motor mounting plate.
It must be understood that the positional display on the panel meter of the Yaesu rotators (and many others as well) is a co-operative effort between components inside the controller and components inside the motion unit. In a nutshell, there is a potentiometer inside the motion unit that is driven through a gearing arrangement that is connected through to the motor and its driven gear. There are multiple levels of reduction in both directions before we ever get to the potentiometer drive gear, and the gearing must be such to allow the full amount of rotator motion within a single swing of the potentiometer from one limit to the other. This is very important with some models of rotator, especially with those that have a turn and a quarter (450°) or a turn and a half or 540° of motion from limit switch to limit switch. The entire amount of that degree of rotation must occur within - and actually less than - a single rotation of the potentiometer, which in and of itself does not have a full 360° of rotational range between its stops.
The relationship between the potentiometer drive and the position of the rotating element is established through the various gears used in the drive system. There are a couple of important points to understand when assembling one of these units, however, that are related to the potentiometer. The first is that we must determine where the center-point of the unit rotational travel will be and position the unit in alignment with that center point when installing it. The second is that we must also determine where the mid-point of the potentiometer’s rotational range is located and position the potentiometer at that mid-point for the assembly of the unit. It is only when both the motion system and the potentiometer are oriented at the centers of their rotational ranges that we can be assured of proper timing between the motion unit and the potentiometer.
As a result of all of this, a varying voltage signal is available on one of the wire leads from the motion unit to the controller. The harness cable between the two units generally contains six wires, distributed as below :
- Motor Common
- Motor Clockwise
- Motor Counter-Clockwise
- Potentiometer Supply
- Potentiometer Wiper
- Potentiometer Ground
The potentiometer wiper lead is where we will find the varying voltage that indicates the relative position of the motion unit between its limits of motion. A nominal 6VDC is supplied to the potentiometer, being connected to one end of the potentiometer, while the opposite end of the potentiometer is connected to the system ground. The voltage on the potentiometer wiper will vary as the potentiometer rotates with the rotation of the motion unit, and that varying voltage is the input signal to the controller for driving the meter.
With this in mind, it should make sense that if we monitor that wiper lead while the motion unit rotates, we would expect to find a varying voltage available there. If there is no voltage, we have either a failed supply to the potentiometer, a failed (open) potentiometer, or an open circuit in one or more of the potentiometer’s leads. If we measure a fixed voltage there while the motion unit rotates, we have a potentiometer that is either not being driven due to a failure in the drive system, or we have a seized potentiometer that cannot rotate.
In most of the Yaesu rotators, the potentiometer drive gear is a nylon gear that is fastened to the potentiometer shaft by way of a set-screw installed into the gear hub. In many units, this nylon gear is directly driven by one of the motion system gears. However, in the G-2700, there is a different arrangement for driving the potentiometer gear. In this design, the unit gearing drives a stamped steel gear that is mounted to a short shaft. That shaft extends through the motor mounting plate into the lower area of the rotator housing, where the potentiometer is installed. The lower end of that shaft has a small quill gear secured to the shaft, and it is that quill gear that in turn drives the potentiometer gear. As a result, when first opening up the motion unit, the potentiometer and its drive gear are hidden, out of sight below the motor mounting plate.
When I opened up this particular motion unit, I found plenty of indication of water entry into the housing, in the form of heavy corrosion on most of the internal parts (Figure 2). This included the stamped steel gear that drives the shaft that in turn drives quill gear that drives the potentiometer gear (Figure 3). In this illustration, it is quite difficult to see the drive gear - note the set-screw in the gear hub and then move out from there. The drive gear is the piece with all of the red corrosion on it.
I removed the cap screws that secure the motor mounting plate to the housing, and lifted the motor unit up and out so as to get to the potentiometer and gear. Next, I removed the stamped steel drive gear and the drive shaft by loosening the set-screw in the small quill gear at the lower end of the drive shaft. Once the shaft was out, I could remove that quill gear and had an isolated potentiometer and its drive gear. A quick check of the potentiometer gear for the ability to rotate showed that the potentiometer was seized. It only took a couple of minutes to remove the potentiometer gear and then the potentiometer itself from the unit (Figure 4).
I thought that it might just be a matter of replacing the potentiometer with a new one, but as it turned out, the seizure of the potentiometer caused damage to the hub of the gear. To start with, the gear hub, which like the gear is made of nylon, had fractured longitudinally along the length of the hub, in two diametrically-opposed locations. This meant that tightening the set-screw would not secure the gear to the potentiometer shaft, but would only serve to spread the fractures wider apart. I cured this by first cleaning the hub thoroughly with residue-free solvents. Then, I did some plastic-welding of the cracks in the hub, using the soldering iron. Finally, using some safety wire, I made a couple of wraps of wire around the hub and then twisted the ends tight, so as to form a clamp around the hub. This clamp would keep the hub from spreading as the set-screw was tightened.
The second manner in which the gear hub was damaged was that the hub bore was badly worn on the side opposite the set-screw. This is an apparent result of the gear rotating on the potentiometer shaft rather than turning the shaft. In any event, this wear caused the gear to be pulled off-square when the set-screw was tightened on the new potentiometer, leaving the gear to “wobble” on the shaft and causing changes in its mesh with the quill gear. I resolved this issue by building up the potentiometer shaft slightly, using two different lengths of copper tape applied to the potentiometer shaft opposite the point where the set-screw would touch the shaft. I first laid down a slightly longer strip of copper tape, and then applied a somewhat shorter length at the direct opposite point from the set-screw. This tape took up the slack in the bore of the gear hub, causing the gear to tighten securely and as squarely as possible.
The leads for the potentiometer were very short, making it extremely difficult to manipulate or maneuver the potentiometer in the housing to any extent. To aid in the installation of the new potentiometer, I extended the three leads, using 22AWG stranded wire of the same colors, and covering the soldered splices with heat-shrink tube insulation. When replacing this potentiometer, be sure to place the mylar sheet back in place under the body of the potentiometer, as it serves to ensure that there is no shorting of the potentiometer leads to the frame of the motion unit. I added four inches of wire to each lead.
I spent a lot of time cleaning the corrosion and contaminated lubricant out of the motion unit. The two rows of ball bearings required special attention as they had fine coatings of rust on many of the balls. The ball tracks in the housing halves were thoroughly cleaned, as was the remainder of the motion unit gearing and motor assembly. See Figure 5.
Next, I reassembled the potentiometer and its drive system, positioning the potentiometer at the midpoint of its rotational range. I then lubricated the ball tracks and installed the cleaned ball bearings, replacing those that merited replacement. The balls were coated with lubricant as they were installed into their tracks, and then the installed row of balls had some additional lubricant applied to them for good measure. The lubricating grease on these ball bearings is the only water barrier present on this motion unit, so it is important to have adequate coverage of the lubricating grease on these ball bearings.
The motion system housing half was installed, positioning it in such a manner that the cast boss that operates the limit switches was aligned directly across the unit from the limit switch pair. This effectively sets the motion unit to the center point of its rotational range, and thus times it to the potentiometer.
The lower track of ball bearings was lifted into place against the housing, and then the entire unit was inverted so as to allow the installation of the cap screws that secure the housing halves to each other. Once the assembly of the motion unit was complete, it was tested operationally by connecting it to a known good controller and checking its operation throughout its full range of motion.
Next, it was time to test the G-2700 controller with the motion unit. The controller drove the unit successfully, but there was no meter indication of the motion of the rotator. I discussed the situation with the owner of the system, and he decided to use the second controller with this motion unit and not to spend any money on the G-2700 controller.
I assembled a test cable for the G-1000 controller to connect it to the G-2700 motion unit, and then checked the operation of that controller and its meter, to find that all was working as it should. The owner decided to leave those units paired, and said that he would bring me a length of cable for installation of the correct connectors at a later date.
This was a repair that brought some unexpected circumstances, but that turned out well in spite of that. It illustrates the point that with some ingenuity, most problems can be overcome. When a strange condition turns up, stop and think it through. Consider all of your options, and then choose that option which has the best odds of success. Properly executed, your work should turn out as you want it to.
See you next month!
Icom IC-703 QRP Transceiver - November 2024
|
Once in a while, a job will come in that is simple and straightforward, but is still a pain in the behind to complete. This is one of those situations. In this case, the job is the replacement of the output transistors in an Icom IC-703 QRP Transceiver. This unit came to me with a diagnosis report from an authorized Icom repair facility. The owner had, at the time that the radio was evaluated, not wanted to spend the money that the repair |
facility quoted to repair the radio. Now, five years later, the radio ends up on my bench because the owner decided to go ahead and have the repairs made.
According to the Bench Report from the Icom facility, transistors Q200 and Q201, the power amplifier transistors, had failed and were in need of replacement. The repair quote that was provided to me with the radio showed an estimated $457 repair cost to the owner, and as I said earlier, that was five years ago. I believed that I could and would do better than that on the price, and I told the owner so.
The Icom repair facility had done the heavy lifting as far as diagnosis was concerned. While it is not my policy to blindly accept such findings, I also consider the source. Then, I attempt to duplicate or verify the diagnosis. In this case, I was able to readily verify that the power amplifier transistors had both failed. This took a minimum of time, but I considered it to be a necessary investment, as I did not want to replace these parts blindly and then find that something else was really wrong with the radio.
The transmit signal was present at healthy levels through the pre-driver Q101, a 2SK3074, and the driver Q150, an RD01MUS1 type, both of which are N-channel power MOSFETS. The signal, however, was lost through the power amplifier transistors. This was a simple matter of tracing the signal through the radio using an oscilloscope.
According to the Bench Report from the Icom facility, transistors Q200 and Q201, the power amplifier transistors, had failed and were in need of replacement. The repair quote that was provided to me with the radio showed an estimated $457 repair cost to the owner, and as I said earlier, that was five years ago. I believed that I could and would do better than that on the price, and I told the owner so.
The Icom repair facility had done the heavy lifting as far as diagnosis was concerned. While it is not my policy to blindly accept such findings, I also consider the source. Then, I attempt to duplicate or verify the diagnosis. In this case, I was able to readily verify that the power amplifier transistors had both failed. This took a minimum of time, but I considered it to be a necessary investment, as I did not want to replace these parts blindly and then find that something else was really wrong with the radio.
The transmit signal was present at healthy levels through the pre-driver Q101, a 2SK3074, and the driver Q150, an RD01MUS1 type, both of which are N-channel power MOSFETS. The signal, however, was lost through the power amplifier transistors. This was a simple matter of tracing the signal through the radio using an oscilloscope.
The biggest problem was actually in sourcing the transistors. These transistors, commonly referred to as “final” or “output” transistors, are in fact the last stage of RF amplification before the output RF signal is directed to the antenna for transmission. They are RD07MVS1 devices, and are N-channel enhancement-mode power MOSFETS made by Mitsubishi. The only sources of these transistors appeared to be in China, and there was therefore, as always, the question of whether or not the received parts would be genuine parts or counterfeits.
I decided to purchase the transistors from a vendor that I have dealt with in the past. Jotrin Inc. (https://www.jotrin.com) is a supplier of surplus electronics parts to the repair industry, and I have always obtained viable parts from them in the past. I put in my request to my representative there and waited for a reply.
Eventually, three weeks later, she sent me an email saying that they had located the parts, but that the price would be considerably higher than originally anticipated. I discussed the situation with the owner of the radio, and we made the decision to go ahead and order the transistors.
Another month went by before the package containing the transistors showed up in my mailbox. Imagine my surprise when the package turned out not to contain two transistors, but to contain twenty of the little buggers. Now I know why the cost was so high. Somehow, we got our wires crossed as to quantity, I thought. I reached out to Elle at Jotrin and found that she was aware of the quantity difference, and that the quantity shipped was the minimum purchase from the source from which she had obtained the parts.
OK - so I now had eighteen spare transistors to fit the Icom IC-703 radios, and I could also extend a lower price to my customer. All that I had to do now was to replace the transistors and test and align the radio.
Replacement of the transistors involved the use of focused hot air to de-solder the original transistors. I then used some solder wick to clean up the excess solder on the traces on the board, and cleaned the area afterwards with some 99.9% IPA. The board was now ready for the installation of the new transistors.
I applied some low-temperature CHIPQUICK® paste solder to the pads, and then applied plenty of liquid flux to the area, working with one of the transistor locations at a time. After positioning the transistor on the pads, I applied heat via the focused hot air again. This caused the solder to flow and to bond the transistor to the board. I repeated the process with the second transistor, and then cleaned up the excess flux with the IPA after the board had cooled.
Testing of the radio with a Bird 43 directional wattmeter into a dummy load showed that the output power was right where it should be, peaking at about 9.8 watts in CW mode, and easily reaching 9.5 watts in USB with a continuous 10kHz moderately loud audio tone into the microphone.
I spent some time going through a full alignment of the radio, but it really was very close to correct alignment to begin with. I made some very minor adjustments, but as I said, it was just about right to start with.
I did notice that the cone of the speaker in the radio was cracked in two spots. After some discussion with the radio owner, I made a repair to the speaker cone mostly to prevent further cracking of the cone. Such repairs are easily made with rubber cement brushed lightly onto both sides of the cone material over the cracks. A light coating of the rubber cement will remain pliable enough so as to not hinder movement of the cone as the speaker operates, but will hold the paper edges together nicely and prevent rattling. I extended the coat of cement around the cone in line with the cracks, as that was where the stress on the cone had been. I was not too concerned with the speaker performance either way, as the owner stated that his intent was to use an external speaker or headphones with the radio. He did not want to spend the money for a replacement speaker, though it would not have been very expensive.
This was one of those repairs that did not call for any real diagnosis - that part of the job had already been done by a reputable vendor. My policy in a case like that is to accept, but verify, which I did. In the long run, this was simply a mechanical repair, with no real brain work required, but nonetheless, it made sense to investigate all aspects of the problem.
The radio was returned to its owner, who was happy to have it back on the air after many years of sitting in a box in his basement. I enjoyed the repair, and ended up with eighteen spare transistors for this type of radio. All in all, not a bad job.
See you next month!
MFJ-407D Keyer - October 2024
|
Last month, I wrote about an Astron power supply unit that had come in for repair. The ham who owns the Astron brought an MFJ-407D Electronic Keyer (Figure 1) to me at the same time, with the complaint that the keyer had no keying output. The customer suspected the output transistor, which did in fact turn out to have been in a failed condition. However, what the customer |
did not suspect is why the transistor had failed, nor were intermittent operation and power drop-outs mentioned at all. These two last conditions were conditions that I noted during test and repair operations. Of course, the unit would not be repaired until those problems were cured as well.
Replacement of the failed output transistor, Q1 in the schematic (Figure 2), an enhancement-mode MOSFET, was straight-forward. The transistor in question is a 2N7002 surface-mount device in an SOT-23-3 package. This transistor is one of the few components in the direct output path for the keyer. There is a selectable parallel path designed for use in grid-block or tube-type systems rather than in solid-state systems. The grid-block path has considerably more components, but they are all moot because this keyer was configured for use in the Direct mode of operation.
Selection of the output mode is made through a pair of three-pin headers with a shunt cap on each header (Figure 4). Selection of the Direct mode requires placement of both shunt caps on the center and D pins of each of the respective pin headers. It is at these pin headers that the problem arose which apparently led to the failure of the 2N7002 transistor. Specifically, the problem was on the foil side of the PCB, where the pin headers are soldered through the board.
A short-circuit path had been formed at each of the pin headers between the D pin and the ground plane. The green corrosion formed there was conductive and led to a condition wherein both the gate and the drain of the MOSFET were shorted to ground. It is unclear exactly what the failure mechanism of the MOSFET was, but there is no doubt that it showed itself to be failed when the transistor was tested under both in-circuit and out of circuit conditions. The corrosion was completely removed from the board and the cleaned areas were sealed with clear enamel.
A short-circuit path had been formed at each of the pin headers between the D pin and the ground plane. The green corrosion formed there was conductive and led to a condition wherein both the gate and the drain of the MOSFET were shorted to ground. It is unclear exactly what the failure mechanism of the MOSFET was, but there is no doubt that it showed itself to be failed when the transistor was tested under both in-circuit and out of circuit conditions. The corrosion was completely removed from the board and the cleaned areas were sealed with clear enamel.
|
I set out next to cure the intermittent problems that this unit exhibited. I noted that I could affect the intermittency by putting pressure on the board in various spots, which led me to look closely at all of the solder joints on the board. As this is largely a surface-mount construction, most of these joints were on the component side of the board. Ultimately, I found and repaired cold solder joints at the IC socket pin rows for the microcontroller (µC or µController), a PIC16C72 device (Figure 5).
|
Reflowing the joints along this IC socket cured the intermittency problems that had existed. As it turned out, one of the indications of power drop-out that I mentioned earlier was the fact that the front panel LED would intermittently go out. It happens that the LED ground is made through the µC, and that the LED’s behavior was part of the larger cold solder joint intermittency issue.
Although I do whatever I can to keep my repair pricing reasonable and affordable to most hams, this particular customer made the statement that I was too expensive and I could no longer be afforded. While I know that I keep the costs as low as I can, I have to admit that sometimes, repairing a unit is not economically feasible. Take this repair as an example. The repair bill for this job came in at about $120. A brand new MFJ-407E is available for about ten dollars more, plus tax and shipping. It is very easy to have a repair cost more than a replacement, as parts prices are higher than ever before, without even considering any labor costs. Of course, with MFJ now having gone defunct, that keyer option is no longer available.
This repair was interesting, and locating the intermittent was a challenge that was necessary for a complete repair. I hope that this keyer lasts a good long while and that the customer gets a lot of future use out of it.
See you next month!
Astron VS-35M Power Supply - September 2024
|
Not too long ago, I was asked to take a look at an Astron VS-35M Power Supply that was exhibiting current drop-out under high-current demand periods. The PSU would drop out and then simply reset itself, with no blown fuses or other indications of excessive current draw. There is a single SCR used in the PSU, and the owner suspected that the SCR may have been the cause of the problem, but in reality, the SCR is in the crowbar overvoltage protective circuit. If the crowbar circuit were to be |
activated, the fuse should blow, as the effect is that of dropping a crowbar across the output, creating a dead short across the PSU output.
I tested the operation of the unit and found it to be as described. When I tried to draw as little as ten amperes from the supply, it would drop out and reset itself. I quickly eliminated the pass transistors as the cause of the problem, both by thermal evaluation and by static testing of the easily-removed TO-3 devices. I further tested the driver transistor for the pass network, and it too tested OK. At this point, I suspected that the culprit was the LM723 voltage regulator IC. For the sake of being able to answer the owner’s anticipated questions, I took a few minutes and tested each of the semiconductor devices used in the PSU, largely by desoldering one end of each diode, and by removing the transistors and SCR for out-of-circuit testing. All semiconductor devices tested out OK except for the crowbar SCR! A viable SCR should latch in its conducting mode if the gate and anode are shorted momentarily. In this case, the SCR went into conduction, but failed to latch in that state. Needless to say, I replaced the SCR, though it clearly was not the cause of the specific reported problem.
Among the various Astron schematics available online is a pair of VS-35M schematics, both of which provide similar if not exact listings of the “normal” voltages for the LM-723 regulator. Under initial testing, all of the IC voltages checked out OK, but as I ramped up the load on the power supply, the voltages started to go awry.
I tested the operation of the unit and found it to be as described. When I tried to draw as little as ten amperes from the supply, it would drop out and reset itself. I quickly eliminated the pass transistors as the cause of the problem, both by thermal evaluation and by static testing of the easily-removed TO-3 devices. I further tested the driver transistor for the pass network, and it too tested OK. At this point, I suspected that the culprit was the LM723 voltage regulator IC. For the sake of being able to answer the owner’s anticipated questions, I took a few minutes and tested each of the semiconductor devices used in the PSU, largely by desoldering one end of each diode, and by removing the transistors and SCR for out-of-circuit testing. All semiconductor devices tested out OK except for the crowbar SCR! A viable SCR should latch in its conducting mode if the gate and anode are shorted momentarily. In this case, the SCR went into conduction, but failed to latch in that state. Needless to say, I replaced the SCR, though it clearly was not the cause of the specific reported problem.
Among the various Astron schematics available online is a pair of VS-35M schematics, both of which provide similar if not exact listings of the “normal” voltages for the LM-723 regulator. Under initial testing, all of the IC voltages checked out OK, but as I ramped up the load on the power supply, the voltages started to go awry.
On the LM723, Pin 3 is the “current sense” pin, which is tied to the PSU output, and should range between 13.87VDC (no-load) and 13.7VDC (full load). Pin 2 is the “current limit” pin, and is tied in a roundabout manner to the crowbar circuit, and it should range between 13.1VDC (no load) and 14.0VDC (full load). Pin 10 is the regulator output pin, which drives the TIP-29 pass transistor driver. It should range between 14.8VDC (no-load) and 16.5VDC (full load). While the current sense and current limit voltages were basically where they belonged, as the load went up, the output voltage on Pin 10 would sag way down, eventually dropping to 1.5VDC when a full load was initially applied, and then the PSU dropped out. The cure was a replacement of the LM723 voltage regulator IC.
|
Along the way, I discovered that the 2200µF 16V electrolytic capacitor across the output (See Figure 4) was also very leaky. I replaced that capacitor as well as the other small electrolytics that were on the PCB. The 64,000µF main filter capacitor tested OK, and so was left alone. In post repair testing, the PSU performed flawlessly, so I put this one to bed as a job well done. Using an electronic load test unit, I was able to draw 30 amperes successfully for a thirty-minute period following a 50% duty-cycle pattern. The PSU is rated at 25 amperes at a 100% duty cycle and 35 amperes at a 100% duty cycle. I repeatedly ran the load up to 35 amperes with no drop-out noted. |
One final note. The schematic diagram (See Figure 5), as drawn by the factory, looks strange at first glance, until the technician realizes that the supply side is nothing more than a pair of nested supplies fed through full-wave rectifier circuits. It just looks odd because we are accustomed to seeing separate secondary windings rather than nested winding pairs. It is nonetheless a straightforward pair of full-wave circuits, one inside the other in the diagram.
See you next month!
Para Dynamics PDC-50DL Dummy Load - August 2024
The complaint was that the owner smelled a “burnt electronics” odor from the dummy load, and when he measured the through-resistance of the load, it was no longer 50.1 ohms as it had been. Instead, it was closer to 54 ohms, and he wanted the unit repaired.
When I put it on the bench, the first thing that I did was to measure the through-resistance of the load, which came in at 53.8 ohms. Now this is clearly not fifty ohms as the load was labeled, but it was not terribly far from it. I decided to open it up and see what was what inside the unit.
When I put it on the bench, the first thing that I did was to measure the through-resistance of the load, which came in at 53.8 ohms. Now this is clearly not fifty ohms as the load was labeled, but it was not terribly far from it. I decided to open it up and see what was what inside the unit.
Upon removal of the cover, I discovered that the architecture of the unit was a set of forty-eight 270-ohm 2W resistors configured as sixteen parallel sets of three resistors each, with each group of three resistors set up as individual series strings. Thus, we had 16 parallel resistances of 810 ohms each. Some simple mathematics shows that the total resistance would be 50.625 ohms (810 divided by 16). However, the resistors were 5% types, meaning that each series string could have been anywhere from 769.5 ohms to 850.5 ohms. Taken at the high end, and assuming all were the same, we would now have 850.5 divided by 16, or a potential high resistance of 53.15625 ohms. I wondered just what his concern was until I looked at the other side of the PCB sandwich that comprised the body of the dummy load. There, it was obvious that a resistor had gotten very hot, as the board was charred.
I attacked the unit with the soldering iron, first removing the dummy load body from its enclosure, and then removing the three resistors in the series string that was centered at the charred spot. What I found was that all three of these resistors had failed catastrophically, and that that particular series string was in fact not in circuit at all, but was fully open.
I attacked the unit with the soldering iron, first removing the dummy load body from its enclosure, and then removing the three resistors in the series string that was centered at the charred spot. What I found was that all three of these resistors had failed catastrophically, and that that particular series string was in fact not in circuit at all, but was fully open.
I had the same type and value resistors in stock, so it was a simple job to install three new resistors at that location in the array. I did so, and then I reassembled the dummy load. Now when measured with the ohmmeter, the resistance showed as 50.1 ohms from the SO-239 center pin to the body of the dummy load.
So… why did these three resistors fail, and why did they fail in the manner in which they did? I cannot answer that with any degree of certainty. I can make the assumption, however, that excessive power was input into the load and that this failure was the result. Maybe they were the “weak link” in the resistor chain. Maybe the soldering at those resistors was poor and heat developed as a result. “Maybe” is a big and powerful word, because it can mean so much and so little at the same time. All that I know for sure is that the dummy load is now back to its nominal fifty-ohm value, though in reality it was never very far off from that value, and was just barely outside of the tolerance range for the components used in its construction. Finally, I would like to mention that the 100-watt rating is a bit hopeful, as on its best day, two watts each at forty-eight resistors only provides for sinking 96 watts. What a slippery slope.
See you next month.
So… why did these three resistors fail, and why did they fail in the manner in which they did? I cannot answer that with any degree of certainty. I can make the assumption, however, that excessive power was input into the load and that this failure was the result. Maybe they were the “weak link” in the resistor chain. Maybe the soldering at those resistors was poor and heat developed as a result. “Maybe” is a big and powerful word, because it can mean so much and so little at the same time. All that I know for sure is that the dummy load is now back to its nominal fifty-ohm value, though in reality it was never very far off from that value, and was just barely outside of the tolerance range for the components used in its construction. Finally, I would like to mention that the 100-watt rating is a bit hopeful, as on its best day, two watts each at forty-eight resistors only provides for sinking 96 watts. What a slippery slope.
See you next month.
MFJ-941E Versa Tuner II - July 2024
A short while ago, one of our fellow GCARC Club members asked me about making a repair to his MFJ antenna tuner, a model 941E Versa Tuner II (Figure 1). It seems that he had grown tired of having to shine a flashlight on the panel meter to read the crossed needles at night. Apparently, the factory illumination for the panel meter, a 12V incandescent lamp, had failed, as they are prone to doing. I decided to make a far more permanent repair by fitting a white LED in place of the incandescent lamp. I also noted that one of the four rubber bumper “feet” for the unit was missing.
I opened up the unit - a total of eight screws, with three on each side and two across the top front of the cover - and checked to make sure that the lamp had actually failed and that there was not some other problem. With 13.8V supplied to the rear panel power inlet for the lamp, and with the lamp switch in its “ON” position, I had the full 13.8V across the (dead) lamp. Lamp failure was confirmed.
I opened up the unit - a total of eight screws, with three on each side and two across the top front of the cover - and checked to make sure that the lamp had actually failed and that there was not some other problem. With 13.8V supplied to the rear panel power inlet for the lamp, and with the lamp switch in its “ON” position, I had the full 13.8V across the (dead) lamp. Lamp failure was confirmed.
|
I removed the lamp holder from its place in the meter housing (Figure 2), and then set about removing the lamp from the holder. That took a little bit of doing because of the manner in which the lamp’s bare wire leads had been fed through the holder and wrapped around the socket terminals of the holder. In addition, there is a 0.01µF ceramic disc capacitor across the lamp, and that had to be dealt with as well. I worked at it, and eventually had the holder completely stripped and disassembled.
|
Disassembly of the holder was necessary in order to make a provision for the LED leads to pass through the holder base alongside the socket terminals. The LED leads are much heavier than were the lamp wire leads, and I needed to make holes for the leads to run through. That was simple enough, using a “T” pin and a pair of long-nose pliers to push the pin through the plastic alongside the terminal contacts.
I gathered up the necessary parts - a white 5mm LED, a 510Ω 250mW 5% resistor for current limiting, and a replacement for the 0.01µF capacitor that was unavoidably damaged in removal. The LED fit perfectly into the lamp holder, and I wrapped the LED leads around the terminal contacts. I then added the resistor to the cathode terminal, after which I installed the capacitor across the LED.
I soldered the components in place and formed a small hook on the opposite end of the resistor, so as to facilitate connection of the cathode lead there. Finally, I soldered the lamp circuit wires to the lamp holder terminal (anode) and to the resistor (cathode), cleaning up the excess lead lengths.
I gathered up the necessary parts - a white 5mm LED, a 510Ω 250mW 5% resistor for current limiting, and a replacement for the 0.01µF capacitor that was unavoidably damaged in removal. The LED fit perfectly into the lamp holder, and I wrapped the LED leads around the terminal contacts. I then added the resistor to the cathode terminal, after which I installed the capacitor across the LED.
I soldered the components in place and formed a small hook on the opposite end of the resistor, so as to facilitate connection of the cathode lead there. Finally, I soldered the lamp circuit wires to the lamp holder terminal (anode) and to the resistor (cathode), cleaning up the excess lead lengths.
|
The incandescent lamp and the LED emit light in different patterns. The incandescent lamp emits its light in a diffuse pattern all around the lamp envelope without any particular focus. The LED, on the other hand, emits most of its light in the forward direction off the end of the LED envelope. This caused an objectionable “white spot” to appear in the center of the meter when the LED was powered up. I resolved that issue by applying a dome cap of copper tape (Figure 3) to the very end of the LED envelope, blocking most if not all of the light in the immediate forward direction. As a result, the
|
illumination of the meter is now more diffuse while still being sufficiently bright for reading the meter under any ambient light level. I installed the cover and gave the unit a final look-over.
At that point, I remembered the missing rubber bumper “foot” on the unit. I removed the remaining three bumpers, which were barely holding on, and cleaned the surface thoroughly with some 99.9% IPA. Then, I installed a matched set of four new bumpers to the bottom of the unit. Job done.
Sometimes, repairs can make a piece of equipment better than the factory design level. I am not sure, in today’s electronic world, why MFJ chose to use incandescent illumination other than maybe the fact that it made diffusion of the produced light a non-issue and therefore cut some minor expense. However, it also built in some planned failures, which could easily have been avoided. This unit should never suffer another panel meter illumination failure.
See you next month!
At that point, I remembered the missing rubber bumper “foot” on the unit. I removed the remaining three bumpers, which were barely holding on, and cleaned the surface thoroughly with some 99.9% IPA. Then, I installed a matched set of four new bumpers to the bottom of the unit. Job done.
Sometimes, repairs can make a piece of equipment better than the factory design level. I am not sure, in today’s electronic world, why MFJ chose to use incandescent illumination other than maybe the fact that it made diffusion of the produced light a non-issue and therefore cut some minor expense. However, it also built in some planned failures, which could easily have been avoided. This unit should never suffer another panel meter illumination failure.
See you next month!
Icom IC-756 PRO Transceiver - June 2024
|
One of my fellow GCARC members called me one day because he was having some difficulties with his Icom IC-756 PRO (Figure 1), particularly in tuning the set via the VFO. While I helped him to determine that his biggest problem was the fact that the VFO was locked, I could not account for all of the behavior of the radio. He asked me to put it on the bench and give it a good once-over. |
I found that almost everything was normal with the set, with one glaring exception. The VFO worked very intermittently. It the dial was turned very slowly, it would tune, but it would skip for one half of the revolution of the VFO knob. If the knob was spun rapidly, it would not tune at all.
A quick look at the IC-756 PRO schematic showed that the VFO utilizes a magnetic encoder as its control device. Removal of the front panel, and partial disassembly of that panel, was necessary to access the encoder in its installed location. I quickly determined that the encoder has suffered some sort of a mechanical failure in that a black powdery substance was coming out of the encoder body along the encoder shaft. I attempted a cleaning of the encoder, but to no avail. The encoder still behaved badly, so I determined that a replacement encoder was required.
A quick look at the IC-756 PRO schematic showed that the VFO utilizes a magnetic encoder as its control device. Removal of the front panel, and partial disassembly of that panel, was necessary to access the encoder in its installed location. I quickly determined that the encoder has suffered some sort of a mechanical failure in that a black powdery substance was coming out of the encoder body along the encoder shaft. I attempted a cleaning of the encoder, but to no avail. The encoder still behaved badly, so I determined that a replacement encoder was required.
|
The encoder (Figure 2) has a part number on it (RMS20-250-201P), which turned out to be a Nidec magnetic encoder having 250 pulses per revolution and designed for operation on 5VDC, with “A” and “B” square wave outputs in quadrature. I ordered in a replacement encoder from one of my standard suppliers, knowing that the received encoder would not have the four-pin plug on it, being terminated as wire leads instead. It took only a couple of days to receive that encoder, but when it came in, I discovered that the encoder used by Icom in this case, while carrying that part number, was in fact a custom variation of that part, having a shaft that is approximately 15mm longer than the shaft on the standard part. Obviously, this encoder was not going to fit properly in the radio, in that the shaft would not extend far enough through the front panel for the knob to mount on it properly. |
I ended up locating another encoder, this one having the correct length shaft and the pre-installed four-pin plug. It carried an Icom part number of 6910011090. I was fortunate in being able to obtain this part at a price somewhat reduced from the normal Icom asking price for the part, which was quite expensive.
When the Icom encoder came in, I installed it and tested the operation of the radio. All worked as it was intended to, and the tuning was, of course, back on track. I put the radio through its paces with the full array of test equipment connected, and all was well. The radio was ready to go back to its owner.
When the Icom encoder came in, I installed it and tested the operation of the radio. All worked as it was intended to, and the tuning was, of course, back on track. I put the radio through its paces with the full array of test equipment connected, and all was well. The radio was ready to go back to its owner.
The lesson learned in this repair is that even when a part carries a part number that matches up with a manufacturer’s standard parts offerings, it may still be a customized and therefore a proprietary part. This makes sourcing a replacement part somewhat more difficult, and can severely limit the cost-savings effect of purchasing a standard off-the-shelf part for a repair.
|
As a final point, I had done some research into Icom IC-756-series encoder (Figure 3) issues and I found that this is a quite common failure, in most cases with the encoder going out of alignment or failing due to the failure of one or both halves of the dual comparator IC that is integrated into the encoder assembly. There is information on the web about repairing these encoders from a realignment standpoint and also from a replacement of the IC standpoint. It turns out that an ubiquitous LM393 dual comparator IC in its SMT form factor will do the job nicely. |
The reason that I opted for replacement of the encoder is two-fold : (1) while the price of the LM393 comparator is minute, the time that it takes to disassemble the encoder and replace the IC would cost the owner more than the cost of the replacement encoder, and (2) the fact that the black powdery substance was coming out of the encoder tells me that there was physical damage internal to the encoder as well as whatever electronic damage existed.
Had the radio been my own radio, I may have experimented with repairing the encoder. With the radio belonging to a customer, I chose to err on the side of caution, as I would have to stand behind my work. Oh yeah - one other thing. There is also a case documented online about a ham who used one of the standard encoders in an Icom IC-756 and extended the shaft length via the use of a coupling collar and a cut-off shaft from a potentiometer. It turns out that as an idea, that is not half bad. The problem is that there is not much room for any kind of standard 1/4" coupler to fit in there, so instead, I have discussed having custom single-piece extenders turned from aluminum rods. I have provided a fellow GCARC member with a drawing of what I would like the extender to look like, and as of this writing, he has made a small quantity of these shaft extenders for my use. I have also had a few shaft extenders manufactured for me via the 3-D print process. As it turns out, I have now installed both types of shaft extenders. When the metallic type is installed, I have found it advantageous to also install a copper leaf spring contact that maintains a positive connection to the knob and shaft, and which is connected to the radio chassis. This provides an effective ground path for the static electricity that may find its way onto the shaft from the operator’s touch.
It also turns out that Icom uses the same encoder with the standard (shorter) shaft in other radio models, including the IC-718, where it seems to see frequent failures, presumably due to static discharge through the encoder knob and circuit to ground. I will hang onto the standard encoder, as it will probably find a use at some point in the future.
See you next month!
Had the radio been my own radio, I may have experimented with repairing the encoder. With the radio belonging to a customer, I chose to err on the side of caution, as I would have to stand behind my work. Oh yeah - one other thing. There is also a case documented online about a ham who used one of the standard encoders in an Icom IC-756 and extended the shaft length via the use of a coupling collar and a cut-off shaft from a potentiometer. It turns out that as an idea, that is not half bad. The problem is that there is not much room for any kind of standard 1/4" coupler to fit in there, so instead, I have discussed having custom single-piece extenders turned from aluminum rods. I have provided a fellow GCARC member with a drawing of what I would like the extender to look like, and as of this writing, he has made a small quantity of these shaft extenders for my use. I have also had a few shaft extenders manufactured for me via the 3-D print process. As it turns out, I have now installed both types of shaft extenders. When the metallic type is installed, I have found it advantageous to also install a copper leaf spring contact that maintains a positive connection to the knob and shaft, and which is connected to the radio chassis. This provides an effective ground path for the static electricity that may find its way onto the shaft from the operator’s touch.
It also turns out that Icom uses the same encoder with the standard (shorter) shaft in other radio models, including the IC-718, where it seems to see frequent failures, presumably due to static discharge through the encoder knob and circuit to ground. I will hang onto the standard encoder, as it will probably find a use at some point in the future.
See you next month!
Yaesu FTM-400XDR Transceiver - May 2024
|
Sometimes, a repair does not only involve schematics, components, and solder. That was the case recently when a Yaesu FTM-400XDR (Figure 1) came in for repair. The FTM-400XDR is a dual-band 2m/70cm mobile radio with digital, data, APRS, and Bluetooth capability in addition to the usual analog modes.
The radio’s owner brought it to me, saying that it would not allow him to reach the Club’s repeater at 147.180 MHz. He and I, several weeks prior, had spent some time noodling |
around with the radio for the same complaint, and I found then that it worked quite well in simplex mode, and that when I entered the correct CTCSS frequency and set the radio for automatic repeater offset operation and proper squelch mode, it worked well on the repeater as well. I told him to go through the programming of the radio and at that point I believed that the problem was resolved.
Fast-forward a few weeks, and the radio is back, this time having been replaced by an FTM-500 series unit out of frustration (and probably a little bit of desire). The more features any given radio offers, the more complex the operation and therefore the setup or programming of that radio will be. This is what turned out to be at the root of this failure, but I am getting ahead of myself.
Having the previous history in mind, the first thing that I looked at was the programming of the memories in the radio. What I found surprised me. There were no stations programmed other than the Club’s 2-meter repeater, and that one had an incorrect CTCSS frequency entered. The tone was set to 100.0 Hz rather than to the correct 131.8 Hz. Further, I found that the Squelch Mode setting was set to Noise rather than to either Tone or Tone Squelch. This meant that that the radio was generating a 100 Hz sub audible noise signal instead of the clear 131.8 Hz sub audible sine wave tone required to allow access to the repeater.
Funny thing… I remembered additional memory channels having been populated when I looked at the radio previously. I couldn’t see the owner deleting all of the other channels, including the “Home” channels, so I began to wonder about the memory of the radio. I programmed in three each VHF and UHF repeaters manually, and then I set the radio aside for a few days. When I came back to the radio, the memory slots were not empty, but neither were the stored values the same as I had entered. For example, the text strings assigned to the memory slots had been corrupted, and the CTCSS tone frequencies had changed. In addition, the Squelch Mode settings for each of the memory slots had also reverted to Noise. At that point, I believed that I had narrowed the problem down to a failed memory battery in the radio. This is reinforced by the fact that the date and time stored in the radio, which I had reset, were also incorrect.
Investigation of the radio service manual showed that the radio actually uses two batteries, which are actually coin cells - one each in the Front Panel Module (Figure 2) and the Main Module (Figure 3). In both locations, the cell is an industry standard ML614R-TT31 cell carrying a Yaesu replacement part number of Q9000895. This is a lithium-ion secondary cell with a 3.0V 2.5mAh rating and an anticipated life of five years, and is designed for a discharge rate of 0.005mA. The specifications for these cells are shown in Figure 4. The specification list for the M614R-TT31 shows that it was designed for only a 10% discharge depth, with a charge/discharge cycle count of around 300 cycles.
Fast-forward a few weeks, and the radio is back, this time having been replaced by an FTM-500 series unit out of frustration (and probably a little bit of desire). The more features any given radio offers, the more complex the operation and therefore the setup or programming of that radio will be. This is what turned out to be at the root of this failure, but I am getting ahead of myself.
Having the previous history in mind, the first thing that I looked at was the programming of the memories in the radio. What I found surprised me. There were no stations programmed other than the Club’s 2-meter repeater, and that one had an incorrect CTCSS frequency entered. The tone was set to 100.0 Hz rather than to the correct 131.8 Hz. Further, I found that the Squelch Mode setting was set to Noise rather than to either Tone or Tone Squelch. This meant that that the radio was generating a 100 Hz sub audible noise signal instead of the clear 131.8 Hz sub audible sine wave tone required to allow access to the repeater.
Funny thing… I remembered additional memory channels having been populated when I looked at the radio previously. I couldn’t see the owner deleting all of the other channels, including the “Home” channels, so I began to wonder about the memory of the radio. I programmed in three each VHF and UHF repeaters manually, and then I set the radio aside for a few days. When I came back to the radio, the memory slots were not empty, but neither were the stored values the same as I had entered. For example, the text strings assigned to the memory slots had been corrupted, and the CTCSS tone frequencies had changed. In addition, the Squelch Mode settings for each of the memory slots had also reverted to Noise. At that point, I believed that I had narrowed the problem down to a failed memory battery in the radio. This is reinforced by the fact that the date and time stored in the radio, which I had reset, were also incorrect.
Investigation of the radio service manual showed that the radio actually uses two batteries, which are actually coin cells - one each in the Front Panel Module (Figure 2) and the Main Module (Figure 3). In both locations, the cell is an industry standard ML614R-TT31 cell carrying a Yaesu replacement part number of Q9000895. This is a lithium-ion secondary cell with a 3.0V 2.5mAh rating and an anticipated life of five years, and is designed for a discharge rate of 0.005mA. The specifications for these cells are shown in Figure 4. The specification list for the M614R-TT31 shows that it was designed for only a 10% discharge depth, with a charge/discharge cycle count of around 300 cycles.
|
According to the serial number of the radio at hand, it was produced in September of 2020. Making the coin cells almost three years of age in use, but there is no real way of knowing how much of their shelf lives had expired at the time of installation. It is not unreasonable to find these cells to be failing at three years of radio life. Upon opening the radio’s Main module and measuring the mainboard cell, I found it to be at 2.58V. Next, I opened up the Front Panel module and measured that cell. The Front Panel module cell measured out at a very low 0.612V. It was obvious at this point that replacement of both of the cells was necessary, so I ordered them in. As it turned out, even though the FTM-400 uses two of these cells, Yaesu’s USA service center Standard Horizon stocks only one of these cells. They get $1.49 for each cell and about $11.00 for the shipping, and said that the second cell would have to come from Asia and would entail additional shipping charges. Instead, I ordered a set of ten cells from an Asian supplier at a reasonable cost and with less than a two-dollar shipping fee. The only rub is that the cells, ordered in the middle of May, are not projected |
to arrive until almost the end of July, about the same lead time that Yaesu had offered.
You would think that a consumable item with a finite life cycle such as these lithium-ion cells, which also have a relatively low expected charge/discharge cycle count before failure, would be more readily available here, where so many of these radios have been sold. The Yaesu parts counterman said that he only gets orders for these cells one at a time. That may well be, as other models use the same cell but in a single cell scheme. The FTM-400, however, uses two of these cells, and the manufacturer should be ready to support the radios as these cells fail. The failure of these cells is inevitable and should therefore be anticipated, with an accompanying adjustment in stocking levels. This looks like poor planning, if you ask me.
OK - the batteries - or cells, to be more accurate - have arrived and have been installed. Now the voltages measured are as follows: 2.98V on the mainboard, and 3.02V on the front panel board. Hopefully, this repair will keep the memories in this radio operational for several years. These cells are lithium-ion secondary cells, which are rechargeable, and they do receive a charging current during radio operation. However, there is a finite limit to the number of discharge/charge cycles which the battery can experience before it will fail to accept additional charging. It is safe to assume that between the relatively short “shelf” life and the limited “cycle” life of these cells, they have simply met their limits and needed replacement.
Replacement of the cells was straight-forward. I used my SMT soldering tweezer to heat both tabs of each original cell at the same time, simply lifting the cell clear once the solder flowed. The soldering tweezer was not used to install the new cell, as I did not want to place a short across a new cell. I simply placed each cell into its proper position onto the pre-tinned pads on its respective board, and then soldered it in place with my pencil iron. To simplify the installation, I pre-tinned the solder tabs and the PCB pads before placing the cells on their boards. Having done that, the final step was a simple reflow of the tinning solder.
Following the installation of the cells, it was time for the radio to be programmed and tested. I used the RT software and cable provided by the radio owner for the programming steps. Once that was completed, I took the radio to an antenna, feeding the output through my trusty Bird 43 directional wattmeter with an appropriate element in place.
All operational testing of the radio went as expected. The output power level on the 2-meter band measured a nice 49.2 watts on the High Power setting, 19 watts on the Medium Power setting, and 4.75 watts on the Low Power setting. The 70-centimeter band did not fare quite as well, measuring 46.5 watts on the High Power setting, 18.25 watts on the Medium Power setting, and 4.5 watts on the Low Power setting. While all of these power levels are somewhat lower than the advertised maximums for this radio, they are none the less within reasonable limits for each of the individual power level settings, and were therefore accepted as being “normal”.
It must be noted that Yaesu does not publish an output power range for each band in their service manual for this radio, choosing instead to publish only the maximum power levels expected. The technician must then make a decision as to whether or not a given measured output is acceptable. I considered 10% to be a reasonable lower limit for the various power levels, therefore giving us lower limits of 45 watts, 18 watts, and 4.5 watts respectively for the three power levels offered in this model - high, medium, and low. All of the power measurements were either above or right at these lower-level limits, and were therefore accepted as being within “normal” operating power ranges.
All that was left now was to reassemble the radio, do a final after-reassembly test, back up the programming to the onboard micro-SD card, and get the radio back to its owner. As a convenience to the owner, I printed off a copy of the service manual, so that he would have one for any future needs.
In summary, it can safely be said that this family of radios is coming of age to the point where they will begin requiring lithium-ion cell replacements, as these cells are about at the anticipated extent of their life spans. This means that more of these radios will be coming in for coin cell swaps, and the repair shops should be prepared to service these units. I have now got sufficient inventory on these cells and I am therefore quite prepared. I hope that other repair facilities follow suit and get themselves ready for the rush, as quite a lot of these radios have been sold.
See you next month!
You would think that a consumable item with a finite life cycle such as these lithium-ion cells, which also have a relatively low expected charge/discharge cycle count before failure, would be more readily available here, where so many of these radios have been sold. The Yaesu parts counterman said that he only gets orders for these cells one at a time. That may well be, as other models use the same cell but in a single cell scheme. The FTM-400, however, uses two of these cells, and the manufacturer should be ready to support the radios as these cells fail. The failure of these cells is inevitable and should therefore be anticipated, with an accompanying adjustment in stocking levels. This looks like poor planning, if you ask me.
OK - the batteries - or cells, to be more accurate - have arrived and have been installed. Now the voltages measured are as follows: 2.98V on the mainboard, and 3.02V on the front panel board. Hopefully, this repair will keep the memories in this radio operational for several years. These cells are lithium-ion secondary cells, which are rechargeable, and they do receive a charging current during radio operation. However, there is a finite limit to the number of discharge/charge cycles which the battery can experience before it will fail to accept additional charging. It is safe to assume that between the relatively short “shelf” life and the limited “cycle” life of these cells, they have simply met their limits and needed replacement.
Replacement of the cells was straight-forward. I used my SMT soldering tweezer to heat both tabs of each original cell at the same time, simply lifting the cell clear once the solder flowed. The soldering tweezer was not used to install the new cell, as I did not want to place a short across a new cell. I simply placed each cell into its proper position onto the pre-tinned pads on its respective board, and then soldered it in place with my pencil iron. To simplify the installation, I pre-tinned the solder tabs and the PCB pads before placing the cells on their boards. Having done that, the final step was a simple reflow of the tinning solder.
Following the installation of the cells, it was time for the radio to be programmed and tested. I used the RT software and cable provided by the radio owner for the programming steps. Once that was completed, I took the radio to an antenna, feeding the output through my trusty Bird 43 directional wattmeter with an appropriate element in place.
All operational testing of the radio went as expected. The output power level on the 2-meter band measured a nice 49.2 watts on the High Power setting, 19 watts on the Medium Power setting, and 4.75 watts on the Low Power setting. The 70-centimeter band did not fare quite as well, measuring 46.5 watts on the High Power setting, 18.25 watts on the Medium Power setting, and 4.5 watts on the Low Power setting. While all of these power levels are somewhat lower than the advertised maximums for this radio, they are none the less within reasonable limits for each of the individual power level settings, and were therefore accepted as being “normal”.
It must be noted that Yaesu does not publish an output power range for each band in their service manual for this radio, choosing instead to publish only the maximum power levels expected. The technician must then make a decision as to whether or not a given measured output is acceptable. I considered 10% to be a reasonable lower limit for the various power levels, therefore giving us lower limits of 45 watts, 18 watts, and 4.5 watts respectively for the three power levels offered in this model - high, medium, and low. All of the power measurements were either above or right at these lower-level limits, and were therefore accepted as being within “normal” operating power ranges.
All that was left now was to reassemble the radio, do a final after-reassembly test, back up the programming to the onboard micro-SD card, and get the radio back to its owner. As a convenience to the owner, I printed off a copy of the service manual, so that he would have one for any future needs.
In summary, it can safely be said that this family of radios is coming of age to the point where they will begin requiring lithium-ion cell replacements, as these cells are about at the anticipated extent of their life spans. This means that more of these radios will be coming in for coin cell swaps, and the repair shops should be prepared to service these units. I have now got sufficient inventory on these cells and I am therefore quite prepared. I hope that other repair facilities follow suit and get themselves ready for the rush, as quite a lot of these radios have been sold.
See you next month!
Conar Model 231 Tuned Signal Tracer - April 2024
|
Back in August of 2023, a customer asked me for some help in making his late 1970’s-vintage Conar Model 231 Tuned Signal Tracer (Figure 1) operational for him. A little bit of history is called for here. Conar Instruments was the electronic equipment division of National Radio Institute (NRI). National Radio Institute - McGraw Hill Continuing Education Center was a private, postsecondary, for-profit correspondence school based in Washington
DC, from 1914 to 2002. NRI launched the Conar division in the fall of 1961 and began selling test equipment (and other items) to |
their students primarily in kit form in early 1962, some of which were assembled as a part of the home study program. Other items were simply made available for purchase, assembly, and use by the students in their new electronics repair trade. The Conar 231 Tuned Signal Tracer was released around 1978, and several hundred were sold.
The 231 is an easy-to-use, all solid-state tuned signal tracer. It is called a tuned signal tracer because it has three selectable ceramic filter controlled tuned inputs covering the standard broadcast IF frequencies of 262kHz, 455kHz, and 10.7MHz. These tuned circuits eliminate the need for manual tuning as was required when using some other signal tracing units. This design simplifies the operating setup, allowing the technician to spend his or her work time where it counts - locating and repairing the defect. The Model 231 also provides two untuned input selections, an RF option and an AUDIO option. The unit schematic is shown in Figure 2. This schematic was derived from the unit itself and was drawn in the ExpressSchematic software that I like to use.
The 231 is an easy-to-use, all solid-state tuned signal tracer. It is called a tuned signal tracer because it has three selectable ceramic filter controlled tuned inputs covering the standard broadcast IF frequencies of 262kHz, 455kHz, and 10.7MHz. These tuned circuits eliminate the need for manual tuning as was required when using some other signal tracing units. This design simplifies the operating setup, allowing the technician to spend his or her work time where it counts - locating and repairing the defect. The Model 231 also provides two untuned input selections, an RF option and an AUDIO option. The unit schematic is shown in Figure 2. This schematic was derived from the unit itself and was drawn in the ExpressSchematic software that I like to use.
The unit came in to my shop as an inoperative piece of equipment that was also missing its test probe and ground connector. Those two items are actually the subject of one of my build articles previously published at this point, as I designed and built a replacement active amplifying probe with the high input impedance necessary to avoid loading of the circuit under test and therefore obtaining undistorted waveform samples. The subject of this article is the actual repair of the Conar 231 main unit.
|
This model is powered by 117VAC line current into a step-down transformer with a center-tapped secondary, which then produces two operating voltages, a +15VDC source and a +12VDC source (Figure 3). The +15VDC is taken directly off the rectified and filtered output of the power transformer, while the +12VDC output is tapped off the full wave rectifier and regulated down to twelve volts via a 2N2124 transistor and a 1N5242B 12V Zener diode. The +15VDC source is filtered by capacitor C220, a 1000µF/25V axial aluminum electrolytic capacitor, and the +12VDC
source is further filtered by capacitor C221, a 330µF/16V radial aluminum electrolytic capacitor. |
On power-up, the +15VDC supply was found to be varying from about +6VDC up to about +19VDC, most likely as a result of heavy ripple imposed upon the source. The only possible cause of this ripple was the 1000µF filter capacitor C220. At the same time, the +12VDC supply was found to be dead. As a starting point, I removed and tested capacitor C220 and also C221 (the 330µF filter for the +12VDC source). The 1000µF capacitor turned out to be extremely leaky, while the 330µF capacitor was shorted. I replaced these two capacitors and went back to my testing routine. Now the +15VDC source was as it should have been, but the +12VDC supply was still dead. Voltage measurements at the 2N4124 pass transistor Q201 showed that the transistor was shorted, as was the 1N5242B 12V Zener diode. Replacement of both of these components restored the +12VDC source to proper operation.
At this point, I thought that I had the problems solved, but it turned out that there was still another problem. In testing the operation of the signal tracer, I found that there was no audio from the speaker at all, and no activity at all on the front panel signal strength meter. It was obviously time for some more tests to be made.
I fired up my signal generator and set it for a 1kHz sine wave output at about a half of a volt amplitude. I then injected that signal at the input of the LM380 audio amplifier, IC103 (Figure 4). There was no signal throughput to the speaker at this point. I checked all of the IC voltage readings and they were all right on the money, where they were supposed to be. That led me to the most likely culprit being C218, a 1µF/35V tantalum capacitor in a shunt position across the speaker. I removed and tested that capacitor and found it to be shorted. Replacement of the tantalum capacitor restored the audio operation to normal.
With three failed polarized capacitors in this unit so far, and considering the age of the unit and therefore its capacitors, I elected to go proactive and replace the remaining polarized capacitors, which included a pair of 100µF/25V axial electrolytics, a second 330µF/16V radial electrolytic, and a single 220µF/35V radial electrolytic. It was good repair practice to replace all of these capacitors based upon the rate of failure already seen and the overall age of the parts involved.
This is a fairly well-designed signal tracer, and in spite of the screwy component numbering scheme used, it is not at all difficult to work on. The single PCB is retained in a modular fashion to the chassis by a set of four nylon retaining stand-offs, setting down onto a pair of ten-position pin connecter strips. The PCB itself has receiver sockets that mate with the pins in the connector strips.
As a footnote, one of the things that I noticed was that the red paint had all come off the needle of the front panel signal strength meter, and was sitting in pieces on the floor of the meter shell. I removed and disassembled the meter, cleaning out the paint particles. I then masked the meter face and re-painted the needle with some red color. After re-assembly, it looked as good as new.
All in all, a fairly easy repair, though there were multiple failures to be tracked down and corrected. The moral of this story is that it’s not done until it is all done. I packed the unit up together with the new probe and ground lead that I had fabricated, and shipped it back to its owner.
See you next month!
With three failed polarized capacitors in this unit so far, and considering the age of the unit and therefore its capacitors, I elected to go proactive and replace the remaining polarized capacitors, which included a pair of 100µF/25V axial electrolytics, a second 330µF/16V radial electrolytic, and a single 220µF/35V radial electrolytic. It was good repair practice to replace all of these capacitors based upon the rate of failure already seen and the overall age of the parts involved.
This is a fairly well-designed signal tracer, and in spite of the screwy component numbering scheme used, it is not at all difficult to work on. The single PCB is retained in a modular fashion to the chassis by a set of four nylon retaining stand-offs, setting down onto a pair of ten-position pin connecter strips. The PCB itself has receiver sockets that mate with the pins in the connector strips.
As a footnote, one of the things that I noticed was that the red paint had all come off the needle of the front panel signal strength meter, and was sitting in pieces on the floor of the meter shell. I removed and disassembled the meter, cleaning out the paint particles. I then masked the meter face and re-painted the needle with some red color. After re-assembly, it looked as good as new.
All in all, a fairly easy repair, though there were multiple failures to be tracked down and corrected. The moral of this story is that it’s not done until it is all done. I packed the unit up together with the new probe and ground lead that I had fabricated, and shipped it back to its owner.
See you next month!
Heathkit® IT-5283 Signal Tracer - March 2024
|
As is well-known by now, I have a tendency to take on unusual projects, especially those that others cannot seem to repair. This was the case recently with a Heathkit® IT-5283 Signal Tracer (Figure 1) that came in for repair. It was shipped to me in “inoperative” condition, with no other information except that the owner purchased it on ebay.com and was disappointed when he was not able to get it to work at all. He is a hobbyist, but is not much of a repair technician, though he did say that he took voltage measurements with a fresh pair of batteries, but could not find any operating voltages anywhere on the main (and only) circuit board. |
The IT-5283 is one of a five-piece test equipment family of about an early- to mid-1970’s vintage. The family includes a multimeter, an audio signal generator, an RF signal generator, an RLC bridge, and this signal tracer. All five units share a common design as regards form factor and appearance, residing in two-piece plastic enclosures. The kit builder had the option of powering the units either from a pair of nine-volt snap-top batteries, or from a specialized five-output power supply that offered ±9VDC to each of its five output cables. The power supply, Heathkit® model IPA-5280-1, is very hard to come by today, but it is not very hard to duplicate. Each of the five output cables was terminated with a Molex® three-pin 0.093” connector. If the kit builder chose to power the kit from the power supply, there were five sets of parts that came with the power supply kit and that were used to modify each of the 5200-series test units to accept power from the power supply. I mention all of this because it is an important point in the repair of this unit.
When the power supply conversion was made to the test equipment, regardless of which specific model it was, a removable blocking panel gets taken out of the back of the enclosure, and a replacement panel got installed in its place. The new panel (Figure 2) held a slide switch used to select between battery power (for portability) and the line power from the power supply. In addition, this panel also held the mating Molex® three-pin connector so that the power supply cable could be tied in to the unit. OK - more about this later… just remember this detail.
When I received this unit for repair, there were no batteries installed, so I put a fresh set of nine- volt batteries into the snap connectors, got out the voltmeter and my signal generator, and set out to test the unit. I set the signal generator for a one-volt peak-to-peak signal at one kilohertz, connected its output to the signal tracer input, and turned it on. Needless to say, there was nothing - not even static or noise - from the signal tracer. So far, my findings matched what the owner told me - no operation.
I opened up the housing to access the circuit board, and got out a schematic of the unit (Figure 3) from my Heathkit® library, and started to check for voltages on the printed circuit board (PCB). Once again, the owner was correct in that there was absolutely nothing alive on the PCB. Knowing that I had a pair of good batteries, I went to the power switch, which is a section of the rotary function selector switch on the front panel. The switch was badly oxidized, so I cleaned it up with some DeoxIT®, but that was not the problem, as I was not even getting power to the switch. The only thing between the batteries and the power switches (there are actually two power switch sections in the selector switch, one for +9VDC and one for -9VDC) is the PCB, the power source selector switch on the back panel, and the wiring between them. A quick look at the power source selector slide switch showed that it was installed (or wired) backwards, so that the “BATTERY” position was actually indexed to the “LINE” indication on the panel. A simple fix for this one, I thought. Simply dismount the switch, rotate it 180°, and remount it. Once I saw that problem, I simply moved the switch to the correct position (I would turn it around later) and continued with my testing.
When the power switch was turned on, I now had power to the PCB at both voltage levels as appropriate for the function selector switch position. However, as I quickly discovered when I powered up the signal generator again, there was still no output at all from the signal tracer speaker - not even static or noise - the same as earlier.
I started probing the PCB (Figure 4) for actual voltages in accordance with the schematic, and I quickly found that the operating voltages for transistors Q6, Q7, and Q8 were very low, with no voltage present at all on Q8. According to the schematic, there is a 250µF electrolytic capacitor (C11) that is connected to the collectors of Q6 and Q7, and if shorted or very leaky, would drag those terminals, and by extension Q8, right down to low levels. I removed that capacitor and tested it. It turned out to be extremely leaky, testing out more like a 98Ω resistor than like a capacitor. I replaced it with a 220µF 25V electrolytic from my inventory, and the unit came alive.
I was not finished there, however, as although it was alive, it was extremely noisy when the level (gain) potentiometer was rotated, and from time to time there was a loud “pop” in the speaker as well. Some more investigation turned up another failed capacitor, this one a 10µF electrolytic in the level control circuit. I replaced it with a like 10µF 16V electrolytic capacitor from my inventory, and the “pop” was gone. Some DeoxIT® spray took care of the noisy level potentiometer as well.
With two of the seven electrolytic capacitors in this unit having failed, I opted to replace all of the electrolytics, three (total) 250µF (replaced by 220µF), two 50µF (replaced by 47µF), and two (total) 10µF capacitors. Once that was completed, I went over the rest of the unit to check for any other problems, and I found one wire in the “LINE” power circuit that was not soldered to the PCB. It was in the hole in the PCB, and because it was solid rather than stranded wire, it stayed in place, but the circuit would have been problematic at best, if it worked at all. Of course, I soldered this wire in place properly. I then remounted the power source selector switch in its proper orientation, gave the unit a good cleaning, and buttoned it up. Finished!
Truth be told, I have to wonder if the original builder of this unit ever got it to work at all, or if the builder just never noticed that the power source selector switch was backwards. While that individual may have known and not cared that it was backwards, that little problem sure caused some grief for at least one later owner of the unit. It is a safe bet that the current owner never noticed the backwards switch, as he was lost as to why there was no incoming supply voltage to the PCB.
It takes a systematic approach to any problem if you want to find a solution to the problem. It certainly does not pay to just go jumping from place to place, and guessing or assuming anything. Know what you have, and know what you expect to find. Then, when you don’t find what you expected to find, look for the reason why the result is different. With a logical and systematic approach, you will find the answer.
See you next month!
LF&C Survey Meter - February 2024
Not long ago, I wrote in this column about a geiger counter repair that I was asked to take on. As you may (or may not) recall, I wrote at that time that the Club member for whom I was making these repairs actually brought two “geiger counters” in for repair. The previous article described the operation and repair of a Victoreen CD V-700 Model 6A Radiological Survey Meter. Now, I am telling the rest of the story, as Paul Harvey used to say. This month, I am describing the operation of and repairs to a Landers, Frary & Clark CD V-715 Model 1A Radiological Survey Meter (Figure 1).
As I explained in the previous article, these geiger counters and radiological survey meters were manufactured under the auspices of the federal Civil Defense program, each being made to a specific standard for its CD type designation, but with the specific circuitry and operational design left up to the individual manufacturers of the equipment. Thus, there were several different makers of the CD type V-715 meter. Landers, Frary & Clark (LF&C) was just one of those manufacturers.
While the V-700 meter described in the earlier article is a geiger tube instrument, the V-715 utilizes an ionization chamber as the sensing element instead of a geiger tube. As a result, the V-715 is not really a “geiger counter”, though that term has been loosely used to describe meters of this type as well.
One thing that sets this type of instrument apart from the others is that it uses some resistors having extremely high through resistances. Connected to the range switch in this unit (refer to Figure 2 and Figure 4) are resistors having the following values, all of which are specified as 500mW 20% metal film types as below :
- 2 pieces, series connected, of 1 x 1011 ohms (100,000,000,000Ω) each;
- 1 piece of 2 x 1010 ohms (20,000,000,000Ω);
- 1 piece of 2 x 109 ohms (2,000,000,000Ω); and
- 1 piece of 2 x 108 ohms (200,000,000Ω).
The lowest of these values is 200 megohms, well above the capability of most ohmmeters to measure. This poses a bit of a problem when attempting to validate the condition of such a resistor. One method of determining the resistance would be to apply a fixed voltage source to the resistor and then to measure the current flowing through it. But, at 200 megohms, a testing voltage of 100V will cause only 500 nanoamperes (0.0000005A) to flow - well below the measurement range of most typical ammeters. So… how is the resistance measured? One method that often works is to first isolate the resistor under test, and then to place a resistor of known value in parallel with the resistor under test. Measure the parallel resistance and work the arithmetic backwards to determine the value of the resistor under test. However, even this method is not useful in this circumstance due to the sheer magnitude of the resistances of the resistors to be tested. Placing a 1MΩ 0.1% tolerance resistor in parallel with the smallest of these high-value resistors, the 200,000,000Ω one, gave me a measured resistance of 994,130Ω. This value is outside the tolerance range of the 1MΩ 0.1% resistor (100,100,000Ω to 999,000Ω), but would be a resultant value that is well within the tolerance range of the 200,000,000Ω 20% resistor (240,000,000Ω to 160,000,000Ω) and 1MΩ resistor placed in parallel, so the arithmetic would be meaningless in determining the actual value of the high-value resistor. It should be noted that the 994,130Ω reading obtained is pretty close to what would be expected with a 200MΩ and a 1MΩ resistor of close tolerances in parallel with each other - (200,000,000 x 1,000,000) / (200,000,000 + 1,000,000) = 995,025Ω.
My everyday RLC bridge is capable of only 10 megohms, while my HP4284A laboratory RLC bridge tops out at 99.99 megohms in its resistance mode, well beneath the lowest value used in the range selector section of this unit. I decided that I could not measure these resistors by any practical method, so I would have to assume that they were acceptable until some operating condition of the unit showed me otherwise. In reality, based upon the resistor types in place and the age of the unit, I would have to believe that these resistors were replaced at some point in the history of this unit, which belief is reinforced by the fact that one range position (the x 0.1 position) that called for two series resistors now has a single wire-wound tubular glass device instead.
OK - on to the general description of the unit. This meter is powered by a single standard “D” cell at 1.5VDC, but generates a maximum potential of -60V from the secondary of the power transformer. The primary of that transformer is in the oscillator circuit, which includes a GI 1459 PNP germanium transistor (more about this later).
As mentioned previously, the sensing element is a hermetically sealed plated steel ionization chamber. This chamber (Figure 3) consists of a shell and an insulated center electrode called a collector, which is mounted to a high-resistance insulated feed-through connector. A strong voltage potential is applied to the collector and ionization chamber shell, which makes the shell (with respect to electrical common) negative by about a sixty-volt differential. This negative charge attracts the positively-charged ions that are formed by gamma radiation passing through the air that is contained within the ionization chamber. The ions striking the ionization chamber shell cause a current to flow in the collector. This current is proportional to the number of ions striking the shell, and therefore proportional to the strength of the radiation field. What appears to be a date (June of 2011) is penciled on the top of the ionization chamber. It is a possible surmise that this is an historical replacement date for the ionization chamber.
Depending upon which range has been selected by the range selector switch, this very small collector current flows through and develops a measurable voltage across one of the extremely high value resistors discussed earlier and clearly visible, attached to the range switch in the Figure 4 photo. This voltage is applied to the grid of the triode-connected 5886 Electrometer Tube, causing a small current to flow in the grid circuit. To give some idea of just how small this grid current really is, I took a quick look at the Tung-Sol 5886 Pentode Electrometer Vacuum Tube Datasheet. The maximum grid current, in accordance with the datasheet limitations, is 2.5 x 10-13 amperes when the tube is used as a triode, as it is in this circuit. Written in another form, this current we are talking about measures a mere 0.00000000000025 amperes! The grid current causes a proportional plate current to flow in the tube, with any change in the plate current being shown on the 0-50µA meter movement that is the user’s indication of a detected radiation source.
In this unit, there is a transformer that has a pair of primary windings, one of which has a through resistance of 1.4Ω while the other has a through resistance of 60Ω. The secondary's are also isolated, having through resistances of 890Ω and 85Ω, with the 890Ω secondary paired with the 1.4Ω primary and the 890Ω secondary paired with the 60Ω primary. Used as a step-up transformer, the 1.4Ω primary has a 1:635.7 turns ratio, yielding a very high-voltage output pulse compared to the input pulse voltage in that winding pair.
The remainder of the circuitry uses a handful (seven to be exact) of 500mW resistors of common standard values, easily tested and sourced for replacement, all but one of which are 5% tolerance types. I found one difference between the schematic and parts list and the physical unit, in that R16, a bleeder resistor for capacitor C1, a 5µF electrolytic type, was installed as a 4.7MΩ resistor while the documentation called for R16 to be a of 1MΩ value. Due to the fact that these seven resistors were all of a type - carbon composition - known to exhibit resistance changes over extended time and use, I decided to isolate and measure each of these resistors. In doing so, I found that several of them had varied by well more that their labeled tolerances.
For example, one of the 1KΩ resistors was down to about 400 ohms, while the other was higher than its nominal value, measuring out at 1345 ohms. At 5% tolerance, these resistors should have been no less than 950Ω nor more than 1050Ω. I had all of the required values in stock as modern carbon film 5% tolerance 500mW rated types, so I replaced all of these resistors with new ones, maintaining the 4.7MΩ value as installed for R16.
Next up were the capacitors. Both of the ceramic capacitors tested out as being within specifications and were therefore usable, so they were left in place. The sole electrolytic, on the other hand, had an ESR that was off the top end of the meter scale on my ESR meter, and measured out as about 31.25µF instead of its nominal 5µF as regards capacitance. The top of the ESR meter scale is five ohms, so that capacitor was at least somewhat leaky. It is this leakiness that leads to a higher-than-normal capacitance measurement, as current continues to flow into the capacitor long after it should have stopped if the capacitor had been in good condition. Left alone long enough, that capacitance meter reading would have increased even more - I stopped the test at that point as it was obvious that the capacitor was non-suitable for use. It was replaced with a modern 4.7µF 50V 5% 105°C axial aluminum electrolytic capacitor. Such tight tolerance was not really necessary in this capacitor used as a filtering device, but that is what I had on hand, so I used it. The 4.7µF 50V capacitor is an acceptable replacement for the original 5µF 25V component.
The LC&F meter circuit uses three semiconductor devices - one transistor (mentioned earlier) and two rectifier diodes. The only information provided about the rectifier diodes is that they were “rectifiers”, meaning that they were intended for use in a power supply to convert the AC into DC, and that one had a 50V PIV rating, while the other had a 100V PIV rating. It is unclear why two different diodes were chosen here, as the 100PIV diode should have worked in either location. The original diodes had heavy oxidation on their leads, compromising the lead integrity to the point where they both broke off easily when moved slightly during de-soldering. Through test measurements, I was able to determine that they were both of silicon composition, so I replaced them with a 1N5400 50V PIV 3A diode and a 1N5401 100V PIV 3A diode, both of which were in stock. These rectifier diodes are visible in the Figure 4 photo at the bottom right corner of the PCB.
The transistor was a different story. It was obviously defunct, as it failed each and every test to which I submitted it. I could not make any determinations as to type or specifications from the transistor itself other than the fact that it had gold leads, and its markings were of no help at all. The schematic showed it to be a PNP type. However, what I did find, in the LF&C manual for the unit, was that the original transistor supplier was General Instruments, and that it was a GI part number 1459 device. You might think that having a manufacturer’s name and his part number for the transistor would make it easy to obtain more information about it, right? Not so much, as it turns out. I could not find anything resembling specifications for this transistor anywhere on the internet. I then had a brainstorm and turned to my NTE Electronics QUICKCross™ cross-reference software, where the first item turned up in a text search using “1459” as the search string was the NTE-102 transistor. The datasheet for this device showed it to be a PNP germanium type rated as below :
- Collector-Base Voltage (VCBO)25V
- Continuous Collector Current (IC)150mA
- Collector-Emitter Voltage (VCES)24V
- Emitter Current (IE)100mA
- Emitter-Base Voltage (VEBO)12V
- Total Device Dissipation (PD)150mW
This looked like a good possibility. I mentioned the gold leads because germanium transistors most often have gold leads. I went looking to see who might have stock on this transistor, and I found that Digikey (www.digikey.com) had availability of a direct-ship from NTE with about a five-day lead time. On a whim, I punched “NTE102” into an Amazon search box, and to my surprise, Amazon not only had it, but they had it at about half of the Digikey price. To clinch the deal, the Amazon item order page said that I would have it the next day! What a no-brainer! I ordered it in from Amazon and set everything aside overnight.
OK - so the next day came and with it came the transistor, as promised. Of course, as this point, I really had nothing to go by, that is, nothing saying that this was the correct part other than the NTE cross-reference. On the other hand, I have found the QUICKCross™ software to be quite accurate and reliable with its interchange information. As expected, the leads on the new transistor were in fact gold, and also as expected, based on the datasheet information, was the fact that the transistor was in the same case type, a TO-39 metal can with a tab on its circumference. So far, so good…
Working from the orientation of the original transistor in the PCB and the schematic diagram, the transistor pinout was also correct. The “pinout” is the assignment of specific terminals of the transistor to specific pins on the physical device. In the schematic, the emitter is connected directly to the “D” cell positive terminal. The base is connected to one end of the 1.4Ω transformer primary winding, while the collector is connected to the opposite end of the transformer 60Ω primary winding. Having this connection information, it is easily seen which pin of the original transistor was which terminal of the transistor, which then easily translated to a match with the terminal versus pin assignments of the new transistor. Seeing that everything matched up, I was very confident that I had located a proper replacement for the failed transistor in this unit. I went ahead and installed the new transistor, which can be seen at the lower left area of the PCB in the Figure 4 photo, just to the right of the meter “zero” control potentiometer.
Figure 5 shows a close-up view of the 5886 Pentode Electrometer vacuum tube. I illustrate this tube simply for its curiosity value, as it is somewhat different from those devices that we customarily recognize as vacuum tubes. None the less, it is a vacuum tube. Earlier in this article, reference was made to the fact that the current from the collector of the ionization chamber is directed to both the high-value resistors) via the range selector switch and to the (control) grid of the triode-connected vacuum tube. Note the bare wire lead from the vacuum tube, from the right side of the tube as shown in the Figure 5 photo. This lead ties directly to the common terminal of one deck of the range selector switch, and then also connects directly to the collector lead of the ionization chamber. Note that apart from that one wire, which is soldered, the vacuum tube is connected into the circuit by use of a vacuum tube base socket as are most vacuum tubes. A quick look at the schematic in Figure 2 shows that the cathode is directly heated, and that the cathode is tied directly to the emitter of the transistor.
Once the repairs were made and all operational checks were made in accordance with the manual and the schematic diagram voltage callouts, it was time to button this one up. Field calibration is not really feasible – or even possible in most cases - due to the fact that calibration requires the use of a calibrated radioactive field into which the unit is placed. Then, based upon the strength of the calibrated RA field, the unit is placed into its each of its various operating ranges in turn and each successive calibration potentiometer, one for each range, is adjusted to bring the meter reading into agreement with the known field strength. This requires the use of some equipment not generally available to the field user or maintainer of this device. The manual does indicate which potentiometer is related to which range switch position for actually making the calibration adjustments, but the complete adjustment process requires the use of an X-ray or gamma ray field.
One of the more important factors in the successful operation of this radiological survey meter is the fact that it is sensitive to moisture, including local air humidity. Humidity can and will affect the values of the high-resistance resistors used in the range selection stage as well as the operation of the ionization chamber’s center collector assembly. The high value resistors, the vacuum tube, and the collector assembly are all also subject to problems from handling, as skin oil contamination on the surfaces of these components can cause leakage currents to flow across the component surfaces. When handled, these components must be properly cleaned of all skin oil residue through the use of residue-free alcohol and a soft cloth or cotton swab. To aid in the moisture reduction inside the closed unit, a bag of dry desiccant granules is placed in the bottom of the lower enclosure, which is sealed to the upper body assembly via the use of a rubberized gasket under the cover and O-rings on the control shafts. A rubber cushion is installed in the lower enclosure in the proper location to aid in keeping the “D” cell in its holder. When the unit is assembled, the “D” cell rests on this rubber pad, keeping the cell securely in place.
To close, a few quick words about the manual are actually overdue. I found two different copies of the factory user and maintenance manual for this unit online with a little bit of searching, one more easily readable than the other. The only catch is that care must be taken to ensure that the manual matches the device at hand. Bear in mind that there were multiple manufacturers who produced V-715 radiological survey meters, and each manufacturer may have produced multiple versions of their device. Just make sure that the manual selected is the correct manual for the device at hand, by manufacturer and by specific model number.
All things considered, this was a pretty typical repair of an unusual device. Apart from the fact that the high-value resistors can not easily be measured, the remainder of this repair was pretty straight-forward and required nothing out of the ordinary in either skills or equipment. This was a repair that any reasonably-skilled technician should, be able to handle with ease.
See you next month!
MFJ-259B HF/VHF SWR Analyzer - January 2024
|
I just (at the time of writing this, in early August of 2023) completed the repair of an MFJ-259B SWR Analyzer. The item belongs to one of the GCARC Club members, but had been donated for long-term use to the GCARC Clubhouse. I came across the unit when it was discovered that it would sometimes operate from an AC power adapter, but would not operate at all from its internal battery. What specifically would happen is that the meters came alive, but the LCD panel did not.
The AC power supply for this unit is a 12VDC 1000mA wall-wart type supply. The internal battery is a bank of ten 1.5VDC “AA” cells. The unit is designed to use either regular disposable alkaline cells, or it can use rechargeable Ni-Cad cells. If the Ni-Cad cells are used, a jumper on the MFJ-259B main circuit board must be moved to the “CHARGER ON” position; otherwise, the jumper should remain in the “CHARGER OFF” position. Of course, this is necessary so that the integrated battery charger can recharge the Ni-Cad cells when AC power is provided. |
What I found when I opened up the case was a mess. The alkaline cells that had been installed were obviously flat, and had leaked considerably inside the unit. I spent about an hour cleaning the corrosion out of the battery box and the surrounding area. I then replaced the “AA” cells with fresh alkaline cells and tried the unit, to no avail. It would not operate from the battery. Interestingly enough, it also would no longer operate from the external power supply. The same behavior - active meters but dead LCD panel - was exhibited.
This unit was made to the RoHS Directive standard, using lead-free solder throughout. This was evident by the appearance of the solder joints, with their characteristic flat grey appearance so indicative of lead-free solder use. Lead-free solder joints are prone to early failure due to stresses placed on the board and joints, and I also noted several cold joints in various spots on the main board. I went over the board carefully, re-flowing every joint and removing the solder from any that were suspect in appearance. I re-soldered those joints, and again tested the unit. No luck - it was still inoperative in the same manner as before.
This unit has two five-volt DC supplies internally, one of which is used for the oscillator circuit, and the other of which is used for the logic and display circuits. I was getting intermittent five-volt power to the microprocessor and the LCD panel. One of the areas that had cold joints was the power switch on the main board, which is a DPDT latching push-button switch. The two separate sides of this switch provide current to each of the two five-volt supplies. I wanted to validate the power switch, so I removed the switch and tested it out of circuit, where it tested fine. However, after re-installing the switch, the five-volt supply to the microprocessor and the LCD panel came alive. Progress, but not enough. The LCD panel was still dead.
I next took a look at the ground side of the LCD panel. Pin #1 of the LCD harness is the ground wire, while Pin #2 is the +5VDC lead. When I measure the voltage between these two points, I got no voltage reading at all. When I measured Pin #2 to chassis ground, the +5VDC was present. I next placed a temporary jumper wire from Pin #1 of the LCD panel to chassis ground, and the panel came alive and worked normally.
OK - was there an open in the harness to the LCD panel? Or was the problem elsewhere? I moved the jumper wire from the LCD panel to the Pin #1 wire connect point on the main board, and the panel remained operational. This told me that the wire harness was OK, but that the connection point on the main board had lost its ground connection somehow. I re-flowed that joint again, but that still did not solve the problem.
Ultimately, I resolved the issue by soldering in a jumper wire from the Pin #1 connection on the main board to another chassis ground point on the main board. Problem solved.
The mystery still remains as to how and why that particular pad on the PCB lost its connection to the ground plane, but it was not worth digging any further. The intent was to make the unit operational, which I did. The stresses that contribute to the early failure of lead-free solder joints can be thermal stresses, electrical stresses, or physical stresses. It is for this reason that lead-free solder use is prohibited in mission-critical applications like aerospace, military, or medical applications.
What is interesting about this unit, and something that I believe led to the failure of the PCB connection, is the fact that the battery holder for this unit is mounted directly to the PCB, at two points that span the area of the LCD panel connection to the main board. It is likely that the stresses imposed by removing and re-securing the battery compartment caused some flexing of the printed circuit board, resulting in the failure.
Whereas I am not a big proponent of willy-nilly soldering in jumper wires, in this case it was the best solution to the problem at hand. I do not recommend this approach for every open-circuit problem, as there may be another underlying problem that could worsen if not tracked down. In this case, though, I am fairly confident that the problem is related to the lead-free stress failures, possibly internal in the circuit board. So, in this case I used the jumper wire solution to the problem.
See you next month!
This unit was made to the RoHS Directive standard, using lead-free solder throughout. This was evident by the appearance of the solder joints, with their characteristic flat grey appearance so indicative of lead-free solder use. Lead-free solder joints are prone to early failure due to stresses placed on the board and joints, and I also noted several cold joints in various spots on the main board. I went over the board carefully, re-flowing every joint and removing the solder from any that were suspect in appearance. I re-soldered those joints, and again tested the unit. No luck - it was still inoperative in the same manner as before.
This unit has two five-volt DC supplies internally, one of which is used for the oscillator circuit, and the other of which is used for the logic and display circuits. I was getting intermittent five-volt power to the microprocessor and the LCD panel. One of the areas that had cold joints was the power switch on the main board, which is a DPDT latching push-button switch. The two separate sides of this switch provide current to each of the two five-volt supplies. I wanted to validate the power switch, so I removed the switch and tested it out of circuit, where it tested fine. However, after re-installing the switch, the five-volt supply to the microprocessor and the LCD panel came alive. Progress, but not enough. The LCD panel was still dead.
I next took a look at the ground side of the LCD panel. Pin #1 of the LCD harness is the ground wire, while Pin #2 is the +5VDC lead. When I measure the voltage between these two points, I got no voltage reading at all. When I measured Pin #2 to chassis ground, the +5VDC was present. I next placed a temporary jumper wire from Pin #1 of the LCD panel to chassis ground, and the panel came alive and worked normally.
OK - was there an open in the harness to the LCD panel? Or was the problem elsewhere? I moved the jumper wire from the LCD panel to the Pin #1 wire connect point on the main board, and the panel remained operational. This told me that the wire harness was OK, but that the connection point on the main board had lost its ground connection somehow. I re-flowed that joint again, but that still did not solve the problem.
Ultimately, I resolved the issue by soldering in a jumper wire from the Pin #1 connection on the main board to another chassis ground point on the main board. Problem solved.
The mystery still remains as to how and why that particular pad on the PCB lost its connection to the ground plane, but it was not worth digging any further. The intent was to make the unit operational, which I did. The stresses that contribute to the early failure of lead-free solder joints can be thermal stresses, electrical stresses, or physical stresses. It is for this reason that lead-free solder use is prohibited in mission-critical applications like aerospace, military, or medical applications.
What is interesting about this unit, and something that I believe led to the failure of the PCB connection, is the fact that the battery holder for this unit is mounted directly to the PCB, at two points that span the area of the LCD panel connection to the main board. It is likely that the stresses imposed by removing and re-securing the battery compartment caused some flexing of the printed circuit board, resulting in the failure.
Whereas I am not a big proponent of willy-nilly soldering in jumper wires, in this case it was the best solution to the problem at hand. I do not recommend this approach for every open-circuit problem, as there may be another underlying problem that could worsen if not tracked down. In this case, though, I am fairly confident that the problem is related to the lead-free stress failures, possibly internal in the circuit board. So, in this case I used the jumper wire solution to the problem.
See you next month!
Antenna Rotator Controller - December 2023
Back around the end of May, Al KB2AYU came to me and told me that the antenna rotator controller (Figure 1) that I had built and given to the Club for use in the VHF room was “hosed”. A quick look at it showed that he was correct - the display, which should have been showing azimuthal readings between zero degrees and three hundred and sixty degrees, was displaying values way up into the four- and five-digit area (Figure 2), as well as blanking out some of the letters in the word “Azimuth”, which should have been displayed as well.
This controller consists of some very basic parts… (1) an H-bridge motor driver to handle the output current to the rotator motor, including directional (polarity) control, (2) a simple five-volt voltage regulator that drops the incoming 24VDC down to the 5VDC required by the brains of the unit, and (3) an Arduino Mega2560 microprocessor board. A plain Mega2560 shield was built up to bring out the necessary pin connections as well as serve as the PCB for a low-pass filter that is a crucial part of the circuit.
When I say “to bring out the necessary pin connections”, it must be understood that there are many more +5VDC connections and ground connections made back to the Arduino than there are native pins on the Arduino to handle. As a result, a row of eight or nine pins of each type - +5VDC and ground - are set up on the shield. In addition to the LPF already mentioned, the shield also carries the contrast control for the front panel display, which is a blue and white backlit LCD panel with 16 x 2 character capability.
The shield also carries the interface pins for the other controls on the front panel, which include directional motion switches (CW and CCW), preset, park, and speed controls, as well as the bulk of the front panel display connections. This shield board, of course, simply plugs piggy-back style onto the Arduino Mega2560.
I initially thought that maybe a quick reload of the program on the Arduino might solve the problem, in that it may have somehow gotten corrupted. Deciding to try that on the spot, I brought my laptop and a USB-A to USB-B cable into the VHF room, hooked it up to the controller, fired up the Arduino IDE software, and uploaded the program into the Arduino. No joy - the problem remained. I decided then that I would bring the unit home for repair, and I would swap it out with a second controller that I had already built for my own use, but was sitting idle. Originally, I was going to bring the replacement controller to the Clubhouse on Tuesday evening when I went there to teach the General class (Monday was a holiday, and the Technician class was cancelled for that evening). The way things worked out, I was able to bring the fully repaired controller back to the Clubhouse on Tuesday evening instead. Here is what I found…
I began by verifying the operation of the +5VDC voltage regulator, because if that voltage was screwy, the Arduino operation would also be wonky if it worked at all. The five-volt regulator was fine, with a steady output under load of 4.996 volts. No problem there.
Now, as I have already explained in describing the controller, this thing is actually quite simple with a limited number of places for a problem to crop up. Those problems, discounting a wire connection issue, are limited to the voltage regulator, the H-bridge, the display, and the Arduino. The voltage regulator has already been cleared, and the display was evidently operational, as it displayed information - just not the correct information. Simply in an effort to be thorough, I disconnected the plug the carries control signals from the Arduino to the H-bridge, and rebooted the controller, only to find that the same condition existed. Three out of four of the possibilities have now been eliminated, leaving only the Arduino as the culpable component.
Knowing that the programming had already been uploaded to the Arduino once since this problem began, and also knowing that the upload did not resolve the issue, I was left with the base Arduino as the fault source. Now… the Arduino obviously operated, as it was sending data to the H-bridge and the display, even if that data was incorrect. My reasoning told me to try to recover the Arduino and restore its proper operation.
There is a piece of software embedded on the Arduino called the bootloader which basically sets up the operating condition of the Arduino in use. That is the only thing, apart from a possible hardware failure, that determines how the Arduino behaves. Because of the fact that this is a piece of embedded software, the possibility exists that this software could have become corrupted. I decided to erase the Arduino and to burn a new bootloader into place on the board.
Burning the bootloader can be done in a couple of ways. One way is to use a second Arduino as a programming interface. Another way is to use a dedicated programming device that is compatible with the type of Arduino at hand. In this case, with the Arduino being a Mega2560, I would be able to burn the bootloader using a device known as a USBasp (USB Atmel Serial Programmer). The USBasp (Figure 3) simply plugs into a USB port on the host PC, and then connects to the ICSP (in circuit serial programming) header on the Arduino board. Easily enough done, this procedure does require removal of the shield board in order to access the ICSP header, which in turn requires disconnection of all of the myriad pin connections made on the shield board. Note that the intermediate board in the data cable of the USBasp in the Figure 3 photo is an adapter interface, changing the ten-pin output of the USBasp to six pins so that it can be connected to a six-pin ICSP header such as that used in the Mega2560.
The USBasp works seamlessly, provided that two preliminary steps are taken. First is to set the on-board Slow SCK jumper on the USBasp to its closed (active) position. This introduces some wait states in the data stream so as to enable successful communications with the Mega2560. Second is to install the correct driver for the USBasp under your operating system. I am using Windows 10, and this step was a simple as running the ZADIG software and installing the driver from within ZADIG. Once the driver is installed, launch the Arduino IDE (if it is not already running), go to the Tools > Programmer menu item and select USBasp as the programmer in use. Then, with the USBasp connected to both the PC and the Arduino, go to Tools > Burn Bootloader and let the software do its job.
I did all of this, and then I re-uploaded the operational program to the Arduino again. Next, I completely re-assembled the controller (without its cover), including installing the shield board and re-connecting all of the pin connections. Finally, I connected up the 24VDC power supply to the controller and turned it on. Voilá! It worked normally, as it should have done. Note that the “damaged” digit in the Figure 4 image is a digit that was in the process of changing when the photo was snapped.
Finally, I installed the top cover, and the job was complete. I connected it up to a Yaesu rotator motor I have on hand here, and it worked flawlessly. Thus, it was able to go back to the Clubhouse that evening.
The moral of the story here is that when everything else has been eliminated, what remains must be the problem, regardless how unlikely it may seem. I would have expected the operational program to become corrupted before I would expect that to happen to the bootloader. However, the proof is in the repair, and the bootloader was certainly at fault here.
See you next month!
Sunbeam PM-0001 Plasma Lamp - November 2023
|
A little while ago, one of our fellow Club members came to me to ask if I would look at an inoperative novelty item that belongs to his son. I agreed, as I am often likely to do, and so began one of the more unusual repair episodes that I have undertaken.
Don’t get me wrong. The repair itself was relatively easy. It is just that this item is so far removed from my usual type of repair that I found it to be intriguing. The item was a Plasma Lamp (Figure 1), and it had just up and quit working. Back in March, when the owner first came to me, we took a quick look at it and found a fractured capacitor, a radial film type rated 0.001µF at 1.2kV, with a 5% tolerance. |
The first step was to source a suitable replacement for this capacitor, though I doubted at the time that the capacitor was the only problem. I had noted a slight indentation in a plastic cover on the circuit board, and that indentation was aligned with and shaped like the body of the diode that was sitting right next to that cover. This was a sure sign of heat, which is why I was not sure that the capacitor was the only problem.
I located a replacement capacitor easily enough, with the exception that the replacement was a 2kV rated device. Time went by, and I had forgotten all about the whole thing until I was asked if the capacitor had come in. I brought the replacement capacitor to the Clubhouse on a Saturday morning, but I ended up bringing the unit home with me to make the repairs instead of doing it there at the Clubhouse. One of the reasons that I wanted to get it home was that I wanted to explore the circuit so that I could understand the working of the lamp, and I also wanted to draw up a working schematic of the unit.
When I started on it at home, I began by disconnecting the circuit board from its incoming power wires coming from the lamp base so that I could have better access to both sides of the circuit board. Then, I began to trace out the circuit and put down into a schematic diagram what I was seeing. I typically use ExpressSchematic (part of the ExpressPCB package) to draw my schematics, and I did so here. The circuit (See Figure 2) basically consisted of a full wave rectifier for the incoming AC, an oscillator, a chopper or switching transistor, and a multi-section transformer. The transformer has a winding that is part of the oscillator circuit, but largely serves as a flyback transformer to produce the high potential output needed to drive the plasma stream.
I located a replacement capacitor easily enough, with the exception that the replacement was a 2kV rated device. Time went by, and I had forgotten all about the whole thing until I was asked if the capacitor had come in. I brought the replacement capacitor to the Clubhouse on a Saturday morning, but I ended up bringing the unit home with me to make the repairs instead of doing it there at the Clubhouse. One of the reasons that I wanted to get it home was that I wanted to explore the circuit so that I could understand the working of the lamp, and I also wanted to draw up a working schematic of the unit.
When I started on it at home, I began by disconnecting the circuit board from its incoming power wires coming from the lamp base so that I could have better access to both sides of the circuit board. Then, I began to trace out the circuit and put down into a schematic diagram what I was seeing. I typically use ExpressSchematic (part of the ExpressPCB package) to draw my schematics, and I did so here. The circuit (See Figure 2) basically consisted of a full wave rectifier for the incoming AC, an oscillator, a chopper or switching transistor, and a multi-section transformer. The transformer has a winding that is part of the oscillator circuit, but largely serves as a flyback transformer to produce the high potential output needed to drive the plasma stream.
The plastic cover that I mentioned earlier is the housing of the transformer, and the diode that had melted a groove into the housing was one of the full wave rectifier set. There are two transistors used, one for the oscillator itself, and the other for the high-frequency switching necessary to create the pulse train input for the transformer. Testing revealed that the oscillator transistor had failed, and the switching transistor was severely past its “best by” date. While this transistor did operate, it was extremely below peak frequency and its hFE or beta tested out to be a mere 2.5 instead of the normal 200-plus value of a serviceable transistor.
Further testing showed that the diodes used in the unit, seven in all, were all also below spec in performance, although they were still operational. The biggest problem was that one of the diodes, an FR107 fast-recovery type, was not fast at all, having recovery time measured in the 875mS realm instead of the 500nS that it should have been. Voltage drops on the diodes in the full-wave rectifier proved to be quite variable, with one as low as 350mV and another as high as 935mV. The norm is around 535mV for these 1N4007 diodes.
Also indicative of high heat levels in this unit was the condition of the 4.7µF 250V aluminum electrolytic capacitor. This capacitor was quite leaky, acting more like a resistor than a capacitor. The equivalent series resistance (ESR) measured out at just under 5Ω. It should have been down near zero ohms. The transformer, as near as I could tell using an ohmmeter and LRC meter, seemed to be in serviceable condition, as were the resistors, the 18pF 3kV ceramic capacitor and the 1.5A fuse.
Repairs to this unit, then, included replacement of all of the diodes with like types (1N4007 x 6 and FR107 x 1), replacement of both ST13003 transistors, replacement of the 4.7µF 250V and the 22µF 25V electrolytic capacitors, and installation of the new 0.001µF 2kV film capacitor.
It was not a surprise that the unit worked after the repair… after all, that was the intent. I was happy, though, that I could make a little boy happy by getting one of his favorite items back to him in working condition. I don’t know how long the unit lasted on its factory parts set, but it is a safe bet that it will most likely fail again at some point in the future, as no substantial design changes or parts improvements were implemented.
The upshot of this repair is that even when something is out of our comfort zone, and even if we have absolutely no documentation, we can still often achieve a successful repair just through common sense and perseverance. It was necessary in this case to almost completely disassemble the unit in order to correctly draw up a schematic and to get to some of the components for testing. In fact, there is a diode and a resistor underneath the transformer housing that cannot be seen or identified until the transformer is removed. Just keep after it and you should make it through.
See you next month…
Further testing showed that the diodes used in the unit, seven in all, were all also below spec in performance, although they were still operational. The biggest problem was that one of the diodes, an FR107 fast-recovery type, was not fast at all, having recovery time measured in the 875mS realm instead of the 500nS that it should have been. Voltage drops on the diodes in the full-wave rectifier proved to be quite variable, with one as low as 350mV and another as high as 935mV. The norm is around 535mV for these 1N4007 diodes.
Also indicative of high heat levels in this unit was the condition of the 4.7µF 250V aluminum electrolytic capacitor. This capacitor was quite leaky, acting more like a resistor than a capacitor. The equivalent series resistance (ESR) measured out at just under 5Ω. It should have been down near zero ohms. The transformer, as near as I could tell using an ohmmeter and LRC meter, seemed to be in serviceable condition, as were the resistors, the 18pF 3kV ceramic capacitor and the 1.5A fuse.
Repairs to this unit, then, included replacement of all of the diodes with like types (1N4007 x 6 and FR107 x 1), replacement of both ST13003 transistors, replacement of the 4.7µF 250V and the 22µF 25V electrolytic capacitors, and installation of the new 0.001µF 2kV film capacitor.
It was not a surprise that the unit worked after the repair… after all, that was the intent. I was happy, though, that I could make a little boy happy by getting one of his favorite items back to him in working condition. I don’t know how long the unit lasted on its factory parts set, but it is a safe bet that it will most likely fail again at some point in the future, as no substantial design changes or parts improvements were implemented.
The upshot of this repair is that even when something is out of our comfort zone, and even if we have absolutely no documentation, we can still often achieve a successful repair just through common sense and perseverance. It was necessary in this case to almost completely disassemble the unit in order to correctly draw up a schematic and to get to some of the components for testing. In fact, there is a diode and a resistor underneath the transformer housing that cannot be seen or identified until the transformer is removed. Just keep after it and you should make it through.
See you next month…
Honorary Donation As Payment?
|
A while back, in early February of this year, I received an e-mail from a Pitman resident who has a passing interest in ham and short-wave radio. I believe that he was sent to me by Jim Clark KA2OSV, but I am not one hundred percent sure about that. Anyway, his main SWL radio had developed a problem and was unusable for him. Now, he is an older shut-in gentleman whose only real contact with the wider world is via his short-wave listening hobby, so the SWL radio being inoperable was a big deal to him. |
In his e-mail, he described the problem with the radio. It sounded fairly simple, so I told him that I would take a look at it for him. He had the radio dropped off to me by an ex-wife, and I went to work on it. The fix was relatively simple once I got the radio’s case open without doing any damage to it. What I needed to do was to re-secure the telescopic whip antenna to the RF input point in the circuit, and then re-mount the base of the antenna to its mounting boss inside the case. The whole repair, including tightening the antenna pivot point, putting a fresh set of batteries, in and testing the radio, probably took me ten minutes. I called him and told him that his radio was ready for pickup, and I did not charge him a penny for the job. His ex-wife again came to my house, this time to pick up the radio, which I had packaged up into its factory carton (he had sent the carton with the radio), just like a new radio.
He was quite happy to get his radio back, as it is his daily companion and window on the world. He called me and said that it worked like it did when it was brand new. The biggest visible difference, apart from the fact that the antenna was back where it belonged, is that the antenna no longer flopped around loosely. Because I had tightened the pivot point screw, the aerial now stayed where it was placed. I felt good about doing a favor for a senior citizen, and that was the end of it as far as I was concerned.
That was then… and I have not thought much about it since… until today, that is. You see, today I received a letter from the ARRL that relates to this repair. I am attaching a copy of the letter to this article for your reading pleasure, but the gist of it all is that he went and made a donation to the League in my honor, and the League was writing to tell me so.
It is funny how one random act of kindness turns into another act that reaches farther and impacts more people. I have no idea how much was donated, and it really does not matter. It is the thought process behind the donation that encourages me, and that is the reason that I am writing this… to share that encouragement.
Keep on doing good deeds. The good that we do is returned when we least expect it and often in ways that we would never have imagined. Read the letter below.
He was quite happy to get his radio back, as it is his daily companion and window on the world. He called me and said that it worked like it did when it was brand new. The biggest visible difference, apart from the fact that the antenna was back where it belonged, is that the antenna no longer flopped around loosely. Because I had tightened the pivot point screw, the aerial now stayed where it was placed. I felt good about doing a favor for a senior citizen, and that was the end of it as far as I was concerned.
That was then… and I have not thought much about it since… until today, that is. You see, today I received a letter from the ARRL that relates to this repair. I am attaching a copy of the letter to this article for your reading pleasure, but the gist of it all is that he went and made a donation to the League in my honor, and the League was writing to tell me so.
It is funny how one random act of kindness turns into another act that reaches farther and impacts more people. I have no idea how much was donated, and it really does not matter. It is the thought process behind the donation that encourages me, and that is the reason that I am writing this… to share that encouragement.
Keep on doing good deeds. The good that we do is returned when we least expect it and often in ways that we would never have imagined. Read the letter below.
Heathkit IM-5284 & IPA-5280-1 - October 2023
At this year’s GCARC Hamfest, I picked up a pair of items for a very low price - a Heathkit® IM-5824 multimeter and a Heathkit® IPA-5280-1 power supply for the 5280-series test instruments. I never checked at all to determine the condition of these items - the price was right regardless the condition, and I was confident that I could repair anything that may have been wrong with the two items. It turns out that I was not wrong, but the challenge ended up being quite considerable.
Let’s talk about condition first. The power supply was plugged in to the multimeter and could not be unplugged. It turned out that the -9VDC wire in the connector body had overheated and melted the connection together, leaving cutting the wires as the only means of removing the power supply from the multimeter. More about the power supply later.
The multimeter was a mess. This unit has two front-panel wafer-type rotary switches and two front panel potentiometers. All four of these controls were seized and would not turn at all. On the rear panel of the enclosure is the connector to which the power supply cable connects, which we already discussed, and also a slide switch that is used to select between the power supply as a power source and the internal battery bank as the power source. This switch was also seized and would not slide at all. When I opened up the enclosure, I found more damage. While the two nine-volt battery snaps were unpopulated, they were none the less severely corroded, beyond saving. There was a leaking “C” cell in the holder for the ohmmeter power source. The alkali from this cell had leaked all over the inside of the enclosure, coating the bottom of the enclosure and soaking into the paint on the front panel. Several wires had corroded off their attachment points, and the battery contacts for the “C” cell were corroded beyond use, with one of them actually broken into two pieces and the other corroded so badly that there were holes through the metal.
I began by completely disassembling the unit and starting the clean-up of the various pieces. That was when I discovered that the alkali had damaged the front panel paint to the point where the paint all the way across the lower edge of the front panel washed off when I rinsed the panel under cold running water. I cleaned the enclosure sections with warm water and dish soap, removing all traces of the alkali and the corrosion. I cleaned the front panel the same way. Fortunately, the damage to the paint remained below the portion of the panel where there were markings for the various controls, so it turned out to be an easy fix with a rattle-can of the right color paint, first masking out the lettering on the panel to avoid overspray damage there.
The rotary wafer switches required complete disassembly in order to free up the moving parts and to clean the wafers properly. I did this for both of the switches, restoring them to working condition. Next, I disassembled the two front panel potentiometers and cleaned and lubricated them in the same manner. DeoxIT is the best choice for cleaning and lubricating these components.
The next thing that I tackled was the rear panel slide switch, removing the original one and installing a new replacement switch in its place. Then I set about repairing the damaged wiring, including replacing the two nine-volt battery snap connectors. Once all of the damaged wiring was repaired, I had to fabricate two new battery contacts for the “C” cell position. This was done by cutting some 24-gauge copper sheet metal to the correct size, and then making two cuts in the bottom edge of each new contact, reaching up about three-quarters of the way to the top of each contact. The center strip, between the cuts, was bent forward to form a spring contact that projects forward from the plane of the contact. I soldered the contacts to their wire leads, and then slid them down into their proper locations in the “C” cell battery compartment.
Once the multimeter was fully assembled, I went through the calibration steps as detailed in the factory manual for this unit, successfully calibrating the multimeter. To complete the job, I made up a set of probe leads for the multimeter and put them into the storage compartment built into the upper enclosure half. Job done… and now it was time to turn to the power supply.
When tested, the power supply was dead. I opened it up and found that the fuse was blown. Digging deeper, I discovered that one of the full-wave rectifier diodes was shorted as was one of the 500µF filter capacitors. I replaced the failed diode and all of the polarized capacitors in the unit - two of the 500µF capacitors and a pair of 10µF capacitors at the outputs of the voltage regulator IC’s. I then replaced the fuse and tested the unit. It came right up and operated correctly, so I placed it under a load to verify the voltage regulation. The unit held rock steady at +9VDC and -9VDC at the two outputs. I assembled the power supply enclosure and replaced the cut-off plug that was melted when connected to the multimeter, and the power supply was as good as new.
Ultimately, I listed the two units on eBay, and the multimeter sold within two days at my full asking price. The power supply, as of this writing, is still available there.
It may seem like a reckless thing to do, to purchase some equipment on a whim without knowing anything about the condition of the equipment. It may actually be foolish. However, as I said earlier, I didn’t care what condition the items were in, as I was confident that I could restore them, and I did. Not only did I restore both items, I sold one of the two for considerably more than I paid for both of them together, and when the second item sells, as it will (it is a very rare piece of equipment), I will be that much further ahead. When you are sure of your abilities, and when you have the skills to overcome most problems, you can go out on a limb and take chances like this one was. And, when you are not so sure of your skills and abilities, there is no better way to learn and to build those skills than by trying.
Let’s talk about condition first. The power supply was plugged in to the multimeter and could not be unplugged. It turned out that the -9VDC wire in the connector body had overheated and melted the connection together, leaving cutting the wires as the only means of removing the power supply from the multimeter. More about the power supply later.
The multimeter was a mess. This unit has two front-panel wafer-type rotary switches and two front panel potentiometers. All four of these controls were seized and would not turn at all. On the rear panel of the enclosure is the connector to which the power supply cable connects, which we already discussed, and also a slide switch that is used to select between the power supply as a power source and the internal battery bank as the power source. This switch was also seized and would not slide at all. When I opened up the enclosure, I found more damage. While the two nine-volt battery snaps were unpopulated, they were none the less severely corroded, beyond saving. There was a leaking “C” cell in the holder for the ohmmeter power source. The alkali from this cell had leaked all over the inside of the enclosure, coating the bottom of the enclosure and soaking into the paint on the front panel. Several wires had corroded off their attachment points, and the battery contacts for the “C” cell were corroded beyond use, with one of them actually broken into two pieces and the other corroded so badly that there were holes through the metal.
I began by completely disassembling the unit and starting the clean-up of the various pieces. That was when I discovered that the alkali had damaged the front panel paint to the point where the paint all the way across the lower edge of the front panel washed off when I rinsed the panel under cold running water. I cleaned the enclosure sections with warm water and dish soap, removing all traces of the alkali and the corrosion. I cleaned the front panel the same way. Fortunately, the damage to the paint remained below the portion of the panel where there were markings for the various controls, so it turned out to be an easy fix with a rattle-can of the right color paint, first masking out the lettering on the panel to avoid overspray damage there.
The rotary wafer switches required complete disassembly in order to free up the moving parts and to clean the wafers properly. I did this for both of the switches, restoring them to working condition. Next, I disassembled the two front panel potentiometers and cleaned and lubricated them in the same manner. DeoxIT is the best choice for cleaning and lubricating these components.
The next thing that I tackled was the rear panel slide switch, removing the original one and installing a new replacement switch in its place. Then I set about repairing the damaged wiring, including replacing the two nine-volt battery snap connectors. Once all of the damaged wiring was repaired, I had to fabricate two new battery contacts for the “C” cell position. This was done by cutting some 24-gauge copper sheet metal to the correct size, and then making two cuts in the bottom edge of each new contact, reaching up about three-quarters of the way to the top of each contact. The center strip, between the cuts, was bent forward to form a spring contact that projects forward from the plane of the contact. I soldered the contacts to their wire leads, and then slid them down into their proper locations in the “C” cell battery compartment.
Once the multimeter was fully assembled, I went through the calibration steps as detailed in the factory manual for this unit, successfully calibrating the multimeter. To complete the job, I made up a set of probe leads for the multimeter and put them into the storage compartment built into the upper enclosure half. Job done… and now it was time to turn to the power supply.
When tested, the power supply was dead. I opened it up and found that the fuse was blown. Digging deeper, I discovered that one of the full-wave rectifier diodes was shorted as was one of the 500µF filter capacitors. I replaced the failed diode and all of the polarized capacitors in the unit - two of the 500µF capacitors and a pair of 10µF capacitors at the outputs of the voltage regulator IC’s. I then replaced the fuse and tested the unit. It came right up and operated correctly, so I placed it under a load to verify the voltage regulation. The unit held rock steady at +9VDC and -9VDC at the two outputs. I assembled the power supply enclosure and replaced the cut-off plug that was melted when connected to the multimeter, and the power supply was as good as new.
Ultimately, I listed the two units on eBay, and the multimeter sold within two days at my full asking price. The power supply, as of this writing, is still available there.
It may seem like a reckless thing to do, to purchase some equipment on a whim without knowing anything about the condition of the equipment. It may actually be foolish. However, as I said earlier, I didn’t care what condition the items were in, as I was confident that I could restore them, and I did. Not only did I restore both items, I sold one of the two for considerably more than I paid for both of them together, and when the second item sells, as it will (it is a very rare piece of equipment), I will be that much further ahead. When you are sure of your abilities, and when you have the skills to overcome most problems, you can go out on a limb and take chances like this one was. And, when you are not so sure of your skills and abilities, there is no better way to learn and to build those skills than by trying.
Heathkit IP-2718 Power Supply - September 2023
|
Last month (in July 2023), I received an e-mail from a ham in Presque Isle, Maine, asking me if I would be interested in taking a look at an older Heathkit® IP-2718 Tri-Power Supply (Figure 1) that was not operating properly. I agreed to give it a shot, and had the owner ship the PSU to me. A rather compact power |
supply that weighs in at a mere ten pounds, the IP-2718 is a three-output unit, having a 5VDC fixed output and a pair of identical 0V to 20VDC adjustable outputs. The two 20-volt outputs can be operated independently, or they can be set so that the “A” output tracks the “B” output. The 5VDC output is at 1500mA, while the 20VDC outputs are at 500mA each. The three outputs are all individually floating outputs which can be connected together in a wide variety of methods, whether in series, in parallel, or in any one of a number of series/parallel combinations. As a result, it is possible for example to achieve a developed output of -5VDC to -45VDC at a maximum output current of 500mA.
Figure 2 illustrates one of the many configurations possible. In this configuration, the +5V terminal is referenced to ground, and each of the 0 to +20V supplies are referenced to -5 volts. In this manner, each of the positive-going 20-volt supplies can be varied from -5VDC to +15VDC, or an overall span of 20 volts. Output currents for each of the three supplies are as shown in the Figure 2 diagram.
In another example, shown in Figure 3, we see the three outputs connected in series with the ground reference made at the high end of the series circuit string. In this circuit, the output voltage is adjustable from -5VDC to -45VDC, while the maximum output current is limited by the maximum current outputs of the “A” and “B” supplies to 500mA.
A third example can help to bring home the concept of multiple configurations yielding multiple outputs. In this example, shown at Figure 4, the supplies are connected in such a manner as to produce three separate outputs, a fixed +5VDC output at 0-1500mA current, the “A” 20-volt supply provides an output that is adjustable from 0V to +20VDC at 500mA, and the “B” 20-volt supply outputs an adjustable 0V to -20VDC also at 500mA.
Note that the polarity of these three outputs is dependent upon which terminal of each supply is connected to the green ground terminal. A careful look at Figure 4 will show that J2 and J4 - both negative terminals - are connected to ground, thus referencing those two supplies as positive-going outputs, but in the “B” supply, terminal J7 - a positive terminal - is connected to the ground point, thus referencing that output as a negative-going output.
Let’s take a look at yet another arrangement, in which we take the two 20-volt supplies out in parallel, thus allowing the currents of these two supplies to effectively add together, resulting in a nominal 1000mA output from the parallel pair. In Figure 5, we can see that a pair of current-sharing or equalizing resistors of 0.5Ω each is connected in series with each of the two 20-volt supplies’ positive terminals feeding the positive side of the load. The total output voltage is reduced by the voltage drops of these two resistors. The actual amount of those voltage drops will be determined by the spontaneous current draw of the circuit, as calculated via the Ohm’s Law formula of E = I x R. For example, if the circuit current draw is 946mA and if it were to be drawn exactly evenly from each of the two supplies (an unlikely circumstance), the voltage drop across each resistor would be (0.946/2) x 0.5, or 0.2365V. This would mean that the total voltage dropped across the two resistors would be 0.473V, or just under a half of a volt. That is the amount by which the total output voltage would be reduced in this configuration and at that specific current draw value. Of course, due to component tolerances and other related factors, the likelihood of having exactly half of the current provided by each of the 20-volt supplies is very slim, and is in fact almost impossible. However, the difference will be small enough that it should not have any meaningful impact on the circuit.
In one final example (Figure 6), we will look at the circumstance wherein we have one of the two 20-volt supplies tracking the other as to output voltage. In this particular power supply, the “A” output will track the “B” output when the unit is placed in the “TRACKING” mode. Under these conditions, each of the outputs is floating. However, almost any combination of series-connected outputs can be utilized in the tracking mode. The main take-away here is that the two 20-volt supply outputs need not be adjusted independently, as in this mode, whatever output voltage level the “B” supply is producing, the “A” supply will do the same.
OK - enough about how this supply is intended to operate. Now let’s talk about what it was not doing, or was doing improperly. To start with, the 5-volt supply exhibited heavy ripple and low output voltage. In addition, the 20-volt “A” supply had no output voltage at all, and the 20-volt “B” supply exhibited an output voltage that was too high and could not be adjusted to its proper value.
Under the cover here, there are three separate power supplies that are integrated within this unit. The 5-volt supply consists mainly of an LM309K three-pin voltage regulator IC, a pair of 1N5403 silicon diodes forming a full-wave rectifier, and a 12,000µF 15V aluminum electrolytic capacitor. In this case, diagnosis was easily accomplished because there was so little that could go wrong. As it turned out, the capacitor was extremely leaky, causing the ripple and also causing the failure of one of the two diodes in the full-wave rectifier. It was a no-brainer that both diodes should be replaced, as they were both placed under the same stresses. This portion of the IP-2718 is constructed with point-to-point wired components (Figure 7), so replacement was extremely simple. The 12,000µF capacitor (C2) has a 220Ω one-watt bleeder resistor placed across its terminals, the edge of which is just barely visible in the Figure 7 photo. The rear panel of the enclosure has a terminal tie strip on which are the two diodes of the full-wave rectifier. Replacement of the capacitor and the two diodes resolved the issues with the 5-volt supply. I did have to do a little bit of customization, as the replacement capacitor has screw terminals rather than the solder lugs of the original device. That was handled by putting solder lugs onto each of the leads that needed to go onto the capacitor, and then simply putting those lugs under the screws and tightening them down in place.
Next up was the 20-volt “A” supply, which had no output voltage. The two 20-volt supplies are identical in design, each occupying one half of the printed circuit board (PCB) on which they are installed. As a result of this happy circumstance, it is very easy to compare the two sections as to voltage readings at various points across the PCB. Component numbering here is laid out following the rule that all “one-hundred” series components are in the “A” supply section, while the “two-hundred” components are in the “B” supply section. Thus, for example, Q101 and Q201 are the same part number and serve the same function at the same location in each of the two supply sections.
The input to the 20-volt power supply is through a pair of 1N4002 silicon diodes configured as a full-wave rectifier directly off the secondary winding of the power transformer (Figure 8). The output of the full-wave rectifier, according to the schematic diagram, should be a nominal 37.6VDC.
At the anode of D103, which is the same point as the cathodes of D101 and D102, the point just referenced as the output of the full-wave rectifier, the actual voltage measured there was 0.030VDC, essentially no voltage. Voltage was present at the anodes of D101 and D102, and the voltage drop across each of those diodes was just over 36 volts. It was obvious that these diodes were both open, and therefore in need of replacement.
Due to the age of this unit, the number of electrolytic capacitors, the level of heat developed by the large power transformer, and the already verified failure of the 12,000µF filter capacitor C2, I decided to replace all of the electrolytic capacitors on the PCB. This equated to a total of twelve capacitors, six in each 20-volt section of the power supply.
I replaced all of those capacitors, installed the replacements for diodes D101 and D102, and then I checked the operation of the unit. The 20-volt “A” supply was restored to proper operation, but the “B” section was still not right. As mentioned earlier, this section exhibited an output that was too high and was not able to be adjusted to its proper level. Some more diagnosis was called for.
Mounted to the rear panel of the enclosure are three semiconductor devices. One of them is the LM309K voltage regulator IC already discussed. The other two are the pass transistors for the voltage regulator circuits of the 20-volt supplies. These transistors are of the type MJ2841 and are identified as Q1 (supply section “A”) and Q2 (supply section “B”). The MJ2841 transistor is a high-power NPN silicon transistor rated at 80VCEO, 80VCB, 4VEB, a collector current (IC) of 10A and a base current (IB) of 4A. The rated power dissipation is 150 watts and the device is in a TO-3 steel case. All told, this is a very sturdy and capable transistor, bordering on overkill for the job it is being asked to do in this power supply. The schematic (Figure 9) calls for an in-circuit operational base voltage of 20.1VDC, an emitter voltage of 20.0VDC, and a collector voltage of 36.7VDC. The emitter is directly connected to the J7 positive output jack for the 20-volt “B” supply and is therefore the supply output voltage. The collector voltage is one diode-drop, in this case 0.9V, less than the input voltage of 37.6V as mentioned in the section “A” discussion above. This is evident, as the only component in series between the D201 and D202 cathodes and the Q2 collector is a single 1N4002 silicon diode, D203.
The actual voltage measured at the emitter of Q2 and at the positive output terminal of the power supply “B” section was 36.9VDC, the same voltage as that found on the collector of Q2. From that information, it was evident that transistor Q2 was shorted, and thus merited replacement.
The type MJ2841 transistor is very difficult to find now, as it is an obsolete part. I found a couple of surplus houses that claimed to have inventory, and I even found a couple of eBay vendors offering the original part, but at extremely exorbitant pricing. The best price that I found was just over twenty dollars plus shipping, but I also found pricing as high as sixty dollars plus shipping. When it comes to replacement of some older semiconductor devices, a usually-viable alternative is NTE Electronics of Bloomfield, New Jersey. I have found suitable replacements in their product line-up before, and this time was no different. A look at my NTE QUICKCROSS™ software turned up the NTE-130 as a suitable replacement for the MJ2841. Amazon had it in stock for next-day delivery at just over five dollars. Sold!
When the transistor came in, I installed it and tested the operation of the IP-2718. It now worked properly on all three of its outputs. I gave the unit a quick cosmetic clean-up, inside and out, and buttoned it up for shipment back to its owner. Start to finish, I had the unit here for three days, shipping it out again on the third day after I received it. The quick turn-around time on this one was aided by the fact that I had all of the capacitors in stock, as well as the diodes. The only part that I needed to source and have shipped in was the pass transistor that we just discussed.
The group of electrolytic capacitors that I changed out on the main PCB included four (4) 10µF/50V axials, four (4) 50µF/50V axials, two (2) 50µF /15V radials (which I replaced with 47µF/63V radials), and two (2) 2,200µF/40V axials, which I replaced with 2,200µF/50V axial devices.
The moral of this story is that no matter how difficult a job may seem at the onset, break it down to its constituent parts and you may find that one difficult large job has become two or three easy smaller jobs. That is exactly what happened here.
See you next month!
Figure 2 illustrates one of the many configurations possible. In this configuration, the +5V terminal is referenced to ground, and each of the 0 to +20V supplies are referenced to -5 volts. In this manner, each of the positive-going 20-volt supplies can be varied from -5VDC to +15VDC, or an overall span of 20 volts. Output currents for each of the three supplies are as shown in the Figure 2 diagram.
In another example, shown in Figure 3, we see the three outputs connected in series with the ground reference made at the high end of the series circuit string. In this circuit, the output voltage is adjustable from -5VDC to -45VDC, while the maximum output current is limited by the maximum current outputs of the “A” and “B” supplies to 500mA.
A third example can help to bring home the concept of multiple configurations yielding multiple outputs. In this example, shown at Figure 4, the supplies are connected in such a manner as to produce three separate outputs, a fixed +5VDC output at 0-1500mA current, the “A” 20-volt supply provides an output that is adjustable from 0V to +20VDC at 500mA, and the “B” 20-volt supply outputs an adjustable 0V to -20VDC also at 500mA.
Note that the polarity of these three outputs is dependent upon which terminal of each supply is connected to the green ground terminal. A careful look at Figure 4 will show that J2 and J4 - both negative terminals - are connected to ground, thus referencing those two supplies as positive-going outputs, but in the “B” supply, terminal J7 - a positive terminal - is connected to the ground point, thus referencing that output as a negative-going output.
Let’s take a look at yet another arrangement, in which we take the two 20-volt supplies out in parallel, thus allowing the currents of these two supplies to effectively add together, resulting in a nominal 1000mA output from the parallel pair. In Figure 5, we can see that a pair of current-sharing or equalizing resistors of 0.5Ω each is connected in series with each of the two 20-volt supplies’ positive terminals feeding the positive side of the load. The total output voltage is reduced by the voltage drops of these two resistors. The actual amount of those voltage drops will be determined by the spontaneous current draw of the circuit, as calculated via the Ohm’s Law formula of E = I x R. For example, if the circuit current draw is 946mA and if it were to be drawn exactly evenly from each of the two supplies (an unlikely circumstance), the voltage drop across each resistor would be (0.946/2) x 0.5, or 0.2365V. This would mean that the total voltage dropped across the two resistors would be 0.473V, or just under a half of a volt. That is the amount by which the total output voltage would be reduced in this configuration and at that specific current draw value. Of course, due to component tolerances and other related factors, the likelihood of having exactly half of the current provided by each of the 20-volt supplies is very slim, and is in fact almost impossible. However, the difference will be small enough that it should not have any meaningful impact on the circuit.
In one final example (Figure 6), we will look at the circumstance wherein we have one of the two 20-volt supplies tracking the other as to output voltage. In this particular power supply, the “A” output will track the “B” output when the unit is placed in the “TRACKING” mode. Under these conditions, each of the outputs is floating. However, almost any combination of series-connected outputs can be utilized in the tracking mode. The main take-away here is that the two 20-volt supply outputs need not be adjusted independently, as in this mode, whatever output voltage level the “B” supply is producing, the “A” supply will do the same.
OK - enough about how this supply is intended to operate. Now let’s talk about what it was not doing, or was doing improperly. To start with, the 5-volt supply exhibited heavy ripple and low output voltage. In addition, the 20-volt “A” supply had no output voltage at all, and the 20-volt “B” supply exhibited an output voltage that was too high and could not be adjusted to its proper value.
Under the cover here, there are three separate power supplies that are integrated within this unit. The 5-volt supply consists mainly of an LM309K three-pin voltage regulator IC, a pair of 1N5403 silicon diodes forming a full-wave rectifier, and a 12,000µF 15V aluminum electrolytic capacitor. In this case, diagnosis was easily accomplished because there was so little that could go wrong. As it turned out, the capacitor was extremely leaky, causing the ripple and also causing the failure of one of the two diodes in the full-wave rectifier. It was a no-brainer that both diodes should be replaced, as they were both placed under the same stresses. This portion of the IP-2718 is constructed with point-to-point wired components (Figure 7), so replacement was extremely simple. The 12,000µF capacitor (C2) has a 220Ω one-watt bleeder resistor placed across its terminals, the edge of which is just barely visible in the Figure 7 photo. The rear panel of the enclosure has a terminal tie strip on which are the two diodes of the full-wave rectifier. Replacement of the capacitor and the two diodes resolved the issues with the 5-volt supply. I did have to do a little bit of customization, as the replacement capacitor has screw terminals rather than the solder lugs of the original device. That was handled by putting solder lugs onto each of the leads that needed to go onto the capacitor, and then simply putting those lugs under the screws and tightening them down in place.
Next up was the 20-volt “A” supply, which had no output voltage. The two 20-volt supplies are identical in design, each occupying one half of the printed circuit board (PCB) on which they are installed. As a result of this happy circumstance, it is very easy to compare the two sections as to voltage readings at various points across the PCB. Component numbering here is laid out following the rule that all “one-hundred” series components are in the “A” supply section, while the “two-hundred” components are in the “B” supply section. Thus, for example, Q101 and Q201 are the same part number and serve the same function at the same location in each of the two supply sections.
The input to the 20-volt power supply is through a pair of 1N4002 silicon diodes configured as a full-wave rectifier directly off the secondary winding of the power transformer (Figure 8). The output of the full-wave rectifier, according to the schematic diagram, should be a nominal 37.6VDC.
At the anode of D103, which is the same point as the cathodes of D101 and D102, the point just referenced as the output of the full-wave rectifier, the actual voltage measured there was 0.030VDC, essentially no voltage. Voltage was present at the anodes of D101 and D102, and the voltage drop across each of those diodes was just over 36 volts. It was obvious that these diodes were both open, and therefore in need of replacement.
Due to the age of this unit, the number of electrolytic capacitors, the level of heat developed by the large power transformer, and the already verified failure of the 12,000µF filter capacitor C2, I decided to replace all of the electrolytic capacitors on the PCB. This equated to a total of twelve capacitors, six in each 20-volt section of the power supply.
I replaced all of those capacitors, installed the replacements for diodes D101 and D102, and then I checked the operation of the unit. The 20-volt “A” supply was restored to proper operation, but the “B” section was still not right. As mentioned earlier, this section exhibited an output that was too high and was not able to be adjusted to its proper level. Some more diagnosis was called for.
Mounted to the rear panel of the enclosure are three semiconductor devices. One of them is the LM309K voltage regulator IC already discussed. The other two are the pass transistors for the voltage regulator circuits of the 20-volt supplies. These transistors are of the type MJ2841 and are identified as Q1 (supply section “A”) and Q2 (supply section “B”). The MJ2841 transistor is a high-power NPN silicon transistor rated at 80VCEO, 80VCB, 4VEB, a collector current (IC) of 10A and a base current (IB) of 4A. The rated power dissipation is 150 watts and the device is in a TO-3 steel case. All told, this is a very sturdy and capable transistor, bordering on overkill for the job it is being asked to do in this power supply. The schematic (Figure 9) calls for an in-circuit operational base voltage of 20.1VDC, an emitter voltage of 20.0VDC, and a collector voltage of 36.7VDC. The emitter is directly connected to the J7 positive output jack for the 20-volt “B” supply and is therefore the supply output voltage. The collector voltage is one diode-drop, in this case 0.9V, less than the input voltage of 37.6V as mentioned in the section “A” discussion above. This is evident, as the only component in series between the D201 and D202 cathodes and the Q2 collector is a single 1N4002 silicon diode, D203.
The actual voltage measured at the emitter of Q2 and at the positive output terminal of the power supply “B” section was 36.9VDC, the same voltage as that found on the collector of Q2. From that information, it was evident that transistor Q2 was shorted, and thus merited replacement.
The type MJ2841 transistor is very difficult to find now, as it is an obsolete part. I found a couple of surplus houses that claimed to have inventory, and I even found a couple of eBay vendors offering the original part, but at extremely exorbitant pricing. The best price that I found was just over twenty dollars plus shipping, but I also found pricing as high as sixty dollars plus shipping. When it comes to replacement of some older semiconductor devices, a usually-viable alternative is NTE Electronics of Bloomfield, New Jersey. I have found suitable replacements in their product line-up before, and this time was no different. A look at my NTE QUICKCROSS™ software turned up the NTE-130 as a suitable replacement for the MJ2841. Amazon had it in stock for next-day delivery at just over five dollars. Sold!
When the transistor came in, I installed it and tested the operation of the IP-2718. It now worked properly on all three of its outputs. I gave the unit a quick cosmetic clean-up, inside and out, and buttoned it up for shipment back to its owner. Start to finish, I had the unit here for three days, shipping it out again on the third day after I received it. The quick turn-around time on this one was aided by the fact that I had all of the capacitors in stock, as well as the diodes. The only part that I needed to source and have shipped in was the pass transistor that we just discussed.
The group of electrolytic capacitors that I changed out on the main PCB included four (4) 10µF/50V axials, four (4) 50µF/50V axials, two (2) 50µF /15V radials (which I replaced with 47µF/63V radials), and two (2) 2,200µF/40V axials, which I replaced with 2,200µF/50V axial devices.
The moral of this story is that no matter how difficult a job may seem at the onset, break it down to its constituent parts and you may find that one difficult large job has become two or three easy smaller jobs. That is exactly what happened here.
See you next month!
Victoreen Geiger Counter - August 2023
|
A fellow club member recently brought some of the strangest repairs that I have seen so far… a pair of 1960’s vintage Geiger counters, neither of which was operational. The two devices were of different series, both of them Civil Defense standard survey units. One of them was a V-700 series unit while the other was a V-715 type.
|
Geiger counters, back in those days, were put out to a common specification for the basic outward design and operational standards, but were built by the various firms that got involved inoutward design and operational standards, but were built by the various firms that got involved in the program each to its own design, electronically. This meant that any V-700 unit would look and function just the same as any other V-700 unit, regardless of the actual manufacturers, but under the skin, each maker had its own proprietary circuit design.
To make matters even more curious, certain manufacturers built multiple different models or design levels of specific devices. For example, from one manufacturer, there was a CD V-700 Model 6, Model 6A, and Model 6B. The circuits in these different design levels were not identical, with each successive sub-model having some sort of design advantage over its previous counterpart.
Of the units that were brought to me for repair, this article will discuss the Victoreen CD V-700 Model 6A Radiological Survey Meter. This unit is a two-transistor design that uses a Geiger tube as the sensing element, and originally used a corona discharge regulator tube in the high voltage power supply, which operated at about 900 volts. The unit is powered by four standard “D” cells as found in most flashlights at that time. The Geiger tube is mounted in a remote probe connected to the main unit via a thirty-six inch long cable. The probe is a nickel-plated brass tube with a window that can be opened to varying degrees to admit beta radiation. This unit will detect both beta and gamma radiation.
To make matters even more curious, certain manufacturers built multiple different models or design levels of specific devices. For example, from one manufacturer, there was a CD V-700 Model 6, Model 6A, and Model 6B. The circuits in these different design levels were not identical, with each successive sub-model having some sort of design advantage over its previous counterpart.
Of the units that were brought to me for repair, this article will discuss the Victoreen CD V-700 Model 6A Radiological Survey Meter. This unit is a two-transistor design that uses a Geiger tube as the sensing element, and originally used a corona discharge regulator tube in the high voltage power supply, which operated at about 900 volts. The unit is powered by four standard “D” cells as found in most flashlights at that time. The Geiger tube is mounted in a remote probe connected to the main unit via a thirty-six inch long cable. The probe is a nickel-plated brass tube with a window that can be opened to varying degrees to admit beta radiation. This unit will detect both beta and gamma radiation.
The high voltage power supply, operating from about 850 to 920 volts, consists of an oscillator, a flyback transformer, a rectifier and a filter capacitor, as well as the 900V corona discharge regulator tube mentioned earlier. This power supply is operated from only two of the four “D” cells installed in the unit.
There is also a pulse shaping and metering circuit, supplied by the remaining two “D” cells, and using the second transistor for its oscillator. This circuit responds to output pulses from the Geiger tube, and forms amplified pulses that trigger the meter as well as the headphone circuit, where the characteristic “clicking” sound of the Geiger counter can be heard, as well as being seen on the meter.
The most apparent problem with this unit was the fact that both transistors had failed, as had the corona discharge tube. I was able to source a kit that contained all of the necessary parts including a Zener diode stack on a small PCB that replaced the corona discharge tube and now serves as the 900V regulator.
While the ceramic capacitors in this unit had not failed, I replaced them with their counterparts from the kit, as the replacements were rated for considerably higher voltages, some of which were operating at voltages very near their rated limits. The sole electrolytic capacitor exhibited severe leakage, with an ESR off the high end of the scale on my ESR meter. It too was in the repair kit, and was thus easily replaced.
The range switch was severely oxidized and required extensive cleaning and restoration. This was a job for the DeoxIT® G100L (DeoxIT Gold) cleaner and lubricant. A quarter-hour with some cotton swabs and the DeoxIT® did the trick, and the switch was restored to a fully operational condition. This might be a good point for a word or two about the DeoxIT® products that I use. I regularly use the DeoxIT® D5 cleaner and lubricant, which I purchase in an aerosol can. This is my everyday go-to product for switch and pot cleaning and restoration. I also use the DeoxIT® X10S Precision Instrument Lubricant for lubrication of such things as meter movements, tuning capacitor bearings and bushings, control shaft bushings, and so forth. However, when a really bad switch or pot shows up, I reach for the DeoxIT® G100L. This product is expensive (about $50 for a 25ml bottle), and as a result I use it only when I really need to, but when it is needed, there is no substitute! Sales talk ended…
A thorough cleaning of the contacts in the battery boxes, and a general cleaning of the exterior of the unit, and it was time for final assembly, testing, and calibration.
Testing consisted of measuring the operating voltages and comparing them to those provided on the unit schematic, which is found in the instruction manual. Next up was a check of the pulse shaping and integrating circuit using an oscilloscope. A three-volt square wave of 150 microseconds duration, followed by a -20V flyback pulse, is what we were looking for and what we found.
Calibration is accomplished simply enough, as a radioactive sample is mounted directly to the outside of the unit lower housing. The instruction manual, readily obtainable online, has calibration instructions that are well-written and easy to follow, so calibration was a breeze.
This unit turned out to be a relatively simple repair, and it was fun working on something that had a place in our national history during the Cold War era. I will write up the second unit, the CD V-715, in another article. That was a little bit different…
See you next month.
There is also a pulse shaping and metering circuit, supplied by the remaining two “D” cells, and using the second transistor for its oscillator. This circuit responds to output pulses from the Geiger tube, and forms amplified pulses that trigger the meter as well as the headphone circuit, where the characteristic “clicking” sound of the Geiger counter can be heard, as well as being seen on the meter.
The most apparent problem with this unit was the fact that both transistors had failed, as had the corona discharge tube. I was able to source a kit that contained all of the necessary parts including a Zener diode stack on a small PCB that replaced the corona discharge tube and now serves as the 900V regulator.
While the ceramic capacitors in this unit had not failed, I replaced them with their counterparts from the kit, as the replacements were rated for considerably higher voltages, some of which were operating at voltages very near their rated limits. The sole electrolytic capacitor exhibited severe leakage, with an ESR off the high end of the scale on my ESR meter. It too was in the repair kit, and was thus easily replaced.
The range switch was severely oxidized and required extensive cleaning and restoration. This was a job for the DeoxIT® G100L (DeoxIT Gold) cleaner and lubricant. A quarter-hour with some cotton swabs and the DeoxIT® did the trick, and the switch was restored to a fully operational condition. This might be a good point for a word or two about the DeoxIT® products that I use. I regularly use the DeoxIT® D5 cleaner and lubricant, which I purchase in an aerosol can. This is my everyday go-to product for switch and pot cleaning and restoration. I also use the DeoxIT® X10S Precision Instrument Lubricant for lubrication of such things as meter movements, tuning capacitor bearings and bushings, control shaft bushings, and so forth. However, when a really bad switch or pot shows up, I reach for the DeoxIT® G100L. This product is expensive (about $50 for a 25ml bottle), and as a result I use it only when I really need to, but when it is needed, there is no substitute! Sales talk ended…
A thorough cleaning of the contacts in the battery boxes, and a general cleaning of the exterior of the unit, and it was time for final assembly, testing, and calibration.
Testing consisted of measuring the operating voltages and comparing them to those provided on the unit schematic, which is found in the instruction manual. Next up was a check of the pulse shaping and integrating circuit using an oscilloscope. A three-volt square wave of 150 microseconds duration, followed by a -20V flyback pulse, is what we were looking for and what we found.
Calibration is accomplished simply enough, as a radioactive sample is mounted directly to the outside of the unit lower housing. The instruction manual, readily obtainable online, has calibration instructions that are well-written and easy to follow, so calibration was a breeze.
This unit turned out to be a relatively simple repair, and it was fun working on something that had a place in our national history during the Cold War era. I will write up the second unit, the CD V-715, in another article. That was a little bit different…
See you next month.
ICOM IC-3210 - July 2023
|
This month’s repair tale involves an Icom IC-3210 dual-band mobile radio (Figure 1), which came in for two separate problems. First of all, the front panel backlighting was inoperative, making it almost impossible to read the display without the use of a flashlight. The second problem was that the radio would not lock in properly on the UHF band most of
|
the time, though occasionally it would work normally. That problem is one of a type that is normally quite difficult to locate – an intermittent problem.
The backlight problem was one that was to be expected with a radio of the age of this particular unit. The front panel on this model is backlit by a set of three T-1 12VDC incandescent lamps that are soldered in place on the front panel printed circuit board (PCB), called the logic board by Icom. Each of these lamps is covered with a yellow plastic boot (Figure 2) that provides the desired color to the illumination provided. The lamps sit down into holes in the PCB (Figure 3 & Figure 4) and have their wire leads soldered to pads on the PCB. The PCB holes index with recesses in the front panel carrier housing, directing the provided light into the rear area of the panel. All three of the lamps were burned out.
While replacements for the original lamps are readily available from standard component sources. I decided to replace them with LED’s instead, so as to preclude the probability of a repeat failure of the backlight system. In order to access the PCB and remove the failed lamps, the front panel subassembly must first be removed from the radio chassis, and then further disassembled. This involves removal of the steel frame and the plastic front cover, followed by removal of the three rotary controls. Finally, the LCD panel and its insulator can be removed by twisting the locking tabs to align them with the slots in the PCB. Once the tabs are aligned with the slots, the LCD panel can be pulled straight out from the PCB. After the LCD panel is removed, the plastic front panel carrier housing can be removed from the PCB by removing the small screws that secure the PCB to the carrier. Finally, some of the wiring harnesses can be gotten out of the way by unplugging them. As always, this is the time for some photos of the harness connections to be taken, against the future reconnection of these plugs to the main PCB.
Once the PCB is stripped down as far as is possible, removal of the lamps was a simple matter of heating their soldered lead connections and lifting the lamps out of their holes. I then cleaned the excess solder off the pads using a soldering iron and some flux-impregnated braided solder wick.
As mentioned above, I had decided to use LED’s instead of the OEM incandescent type of lamps for the replacements. I chose cool white LED’s in the 3mm (T-1) size, and I paired each LED with a 1kΩ resistor for current-limiting purposes. I removed the yellow plastic boots from the original lamps and installed them onto the LED’s. I then placed the LED’s in the lamp holes of the PCB, soldering the cathode leads to the appropriate pads. Next, I added a resistor to each of the LED anode leads, and then soldered the opposite end of the resistors to the appropriate PCB pads. Application of 12VDC from a power supply to the PCB showed that all three LED’s worked perfectly. It was time to move on to the other problem that the radio’s owner had reported.
I chose to tackle this problem while the front panel was still disassembled due to the fact that the most likely problem was the switch that is used to switch between bands. That switch is a 6mm x 6mm normally-open (NO) tactile pushbutton switch. When tested, the switch would make only when pressed very firmly. A normal pressing action on the switch would have no effect on the band selection. This one turned out to be a simple replacement of the switch. I desoldered the original switch, and installed the replacement, which I had on hand as it is a standard switch. Easy peasy, right? Not so much as you might think. It turned out that there was also a known problem with this radio model in that two capacitors on the main PCB are known to fail together with this switch. What happens is that two tantalum capacitors, C87 (0.22µF/35V) and C97 (4.7µF/35V) (Figure 5 & 6) have a tendency to fail with high leakage, causing the UHF phase-locked loop circuit to lose phase lock. The user causes the switch damage by repeatedly working the switch, often aggressively, in an attempt to get the radio to lock onto the UHF band. This action causes the switch to become fatigued internally, leading to the switch failure found on this unit. As a result, the switch merited replacement, as did the two tantalum capacitors. On testing of the removed capacitors, they both had extremely high DC leakage values, and had ESR readings of 14.6Ω for C97 and 9.3Ω for C87.
I next checked the memory keep-alive battery, a BR-2032 coin cell. Yes, that is correct and not a typographical error. It turns out that the BR-series of coin cells are designed for low current drain over an extended period of time. Whereas I had CR-2032 cells in stock with the right welded tabs, I did not want to change the life expectancy of the coin cell in the radio by installing a CR-2032 cell.
The radio dates back to the late 1980’s - its production was discontinued in 1990. The cell in place in the radio had the Icom part number on it, so it was either an original part or a replacement installed by an authorized service center (or someone who bought the cell from Icom). While it is possible that this was the factory cell, it is equally unlikely that it was still original after all of these intervening years. I disconnected it from the circuit for testing, and found that the open-circuit voltage was reading right about 3 volts (3.04V to be exact), which is the nominal voltage of the cell. However, when tested under load, the voltage dropped down to just over 1 volt (1.156V to be exact). Load testing of these cells is best done by installing a 100Ω resistor between the voltmeter leads when measuring the cell voltage. The resistor provides the requisite load, which really tells the story.
I keep a couple of resistors of different values, soldered between small alligator clips, on hand for just this purpose. To use them, I simply select the one with the load value that I want to use, and connect the alligator clips to the voltmeter probes. Then, whenever I measure a battery or cell with the voltmeter with the resistor clipped in place, it is automatically providing a load test for the battery or cell. You can develop a list of desired resistor values for this task by perusing the various battery or cell datasheets. The datasheet will usually provide testing information which includes the load placed on the DUT during testing.
Anyway, I ordered in the correct BR-2032 with the necessary welded tabs for this application, and when it came in, I installed it. However, I did do a load test on the new cell before installation. This one started out at 3.49V open circuit, and only dropped to 3.15V under the 100Ω load test.
After the installation of the coin cell, it was time to re-assemble the radio. Re-assembly went without a hitch, with the only point of note being that the contact fingers along the edge of the PCB where the rubberized contact pad for the LCD panel mates with the PCB need to be clean. I scrubbed them with a pencil eraser, and then removed any skin oil using 99% isopropyl alcohol (IPA) on a cotton swab. This provides for trouble-free connection to the LCD panel after handling the PCB as much as I had done. If you had inadvertently touched the business edge of the rubberized contact pad, that too should be cleaned of skin oil with some 99% IPA on a cotton swab.
Assembly is otherwise the reverse of the disassembly operation. Take care to properly tighten the control nuts on the three rotary controls, and to tighten the PCB to plastic carrier screws without overtightening and stripping them. A quick word about screwdrivers, which maybe should have been mentioned earlier. This radio was manufactured in Japan and therefore uses JIS screws throughout. As a result, JIS screwdrivers are needed to loosen any tight screws without stripping the drive recess in the screw head. Standard Phillips screwdrivers or any variation thereof will certainly cause damage to the screw heads. During disassembly, I found that one of the screws that secured the shield plate and the front panel metal frame to the radio chassis had been stripped in that manner, telling me that someone had been into this radio before and most likely had not realized at first that the screws were JIS screws. I used a specialized extractor to remove the screw, and I replaced that screw upon reassembly with a new JIS 3mm-0.5mm x 6mm flat head machine screw from my inventory.
Remember that in screw dimensioning, the first part (before the hyphen) is the nominal thread diameter, while the second part (after the hyphen) is the thread pitch reference (more about that later). The number after the “x” is the fastener length. Metric fasteners and Imperial fasteners utilize different thread pitch designation methods. With a metric threaded fastener, the pitch information is reported as the distance from the peak of one thread to the peak of the adjacent thread. Thus, a machine screw with a pitch designation of 0.5mm will have a measured distance of one-half of a millimeter from one thread peak to the next. Imperial fasteners use a system that reports the number of thread peaks in an inch of fastener length. Thus, a machine screw with a pitch designation of 32 will have 32 thread peaks in an inch of screw length. Keep in mind also that while most headed fasteners are length-measured from the underside of the head, flat-head fasteners are length-measured for overall length, including the head length.
Reconnecting of the various wire harness plugs to the main PCB is pretty much a straight-forward matter of matching the plug size to the socket size. The is only one possible mix-up, and that is with the squelch control harness plug and the speaker harness plug. This can be resolved easily if the photos recommended earlier were taken. If not, refer to the schematic diagram found in the IC-3210 service manual to determine that the squelch control harness plug goes to connector J6 on the main PCB, while the speaker harness plug goes to connector J9.
Once the reassembly is complete, it is time for a functional test of the repairs. As luck would have it, another problem became evident quite quickly. It turned out that the rotary control used as the main up/down control signal source was inoperative. As a result, frequency could not be adjusted within each band, although the radio was otherwise fully functional on each of its two bands. In a similar manner, none of the radio’s optional settings that require an up/down selection normally made via that control were operational. Thus, the tuning step intervals, the CTCSS tones, and several other functions could not be changed. The problem gets worse… it turns out that the microphone Up/Down controls were also inoperable. This would seem to point to some circuit or component that is common to both control methods. In this case, I worked through the block diagram, the unit schematic, and the X-Ray views of the printed circuit boards in an effort to try to isolate the cause of this problem. Unfortunately, all of this testing and probing led to the inescapable conclusion that the problem lies within the logic board CPU integrated circuit, a µPD75308GF-101-3B9 device that is no longer available. So… while the relatively minor faults for which the radio came in were all corrected, the radio is nonetheless still inoperable, as the VFO frequencies cannot be changed. When powered on, the radio comes up on the designated calling frequencies of 146.520 MHz for VHF and 446.000 MHz for UHF.
Continued testing showed that one of the four output strobe lines from the CPU to the control matrices was extremely low in voltage as compared to the other three strobe lines, though its signal waveform was of the correct shape - just lower in amplitude than it should have been. I also noted that when exercising any of the switches on that particular strobe line, there was no response in the CPU, as those lines were not brought to a deep low with the switch activation - they were already low, so the CPU did not see the switch activations as changes of state on those lines. Unfortunately, no ready repair was available for this problem, as the CPU integrated circuit is obsolete and is therefore currently unavailable.
Sometimes, due to the so-called “planned obsolescence” so prevalent in the output of many of today’s manufacturing plants, an otherwise great little dual-band radio is relegated to the junk pile. I will keep my eyes and ears open on the lookout for another IC-3210 that I can pick up for parts, but I imagine that to be a rather futile effort. There are surprisingly few hits on Google when searching for that model number. I cannot in good conscience charge this radio owner a penny for my time spent and for the repairs that were made, as the end result was not a working radio.
See you next month!
I next checked the memory keep-alive battery, a BR-2032 coin cell. Yes, that is correct and not a typographical error. It turns out that the BR-series of coin cells are designed for low current drain over an extended period of time. Whereas I had CR-2032 cells in stock with the right welded tabs, I did not want to change the life expectancy of the coin cell in the radio by installing a CR-2032 cell.
The radio dates back to the late 1980’s - its production was discontinued in 1990. The cell in place in the radio had the Icom part number on it, so it was either an original part or a replacement installed by an authorized service center (or someone who bought the cell from Icom). While it is possible that this was the factory cell, it is equally unlikely that it was still original after all of these intervening years. I disconnected it from the circuit for testing, and found that the open-circuit voltage was reading right about 3 volts (3.04V to be exact), which is the nominal voltage of the cell. However, when tested under load, the voltage dropped down to just over 1 volt (1.156V to be exact). Load testing of these cells is best done by installing a 100Ω resistor between the voltmeter leads when measuring the cell voltage. The resistor provides the requisite load, which really tells the story.
I keep a couple of resistors of different values, soldered between small alligator clips, on hand for just this purpose. To use them, I simply select the one with the load value that I want to use, and connect the alligator clips to the voltmeter probes. Then, whenever I measure a battery or cell with the voltmeter with the resistor clipped in place, it is automatically providing a load test for the battery or cell. You can develop a list of desired resistor values for this task by perusing the various battery or cell datasheets. The datasheet will usually provide testing information which includes the load placed on the DUT during testing.
Anyway, I ordered in the correct BR-2032 with the necessary welded tabs for this application, and when it came in, I installed it. However, I did do a load test on the new cell before installation. This one started out at 3.49V open circuit, and only dropped to 3.15V under the 100Ω load test.
After the installation of the coin cell, it was time to re-assemble the radio. Re-assembly went without a hitch, with the only point of note being that the contact fingers along the edge of the PCB where the rubberized contact pad for the LCD panel mates with the PCB need to be clean. I scrubbed them with a pencil eraser, and then removed any skin oil using 99% isopropyl alcohol (IPA) on a cotton swab. This provides for trouble-free connection to the LCD panel after handling the PCB as much as I had done. If you had inadvertently touched the business edge of the rubberized contact pad, that too should be cleaned of skin oil with some 99% IPA on a cotton swab.
Assembly is otherwise the reverse of the disassembly operation. Take care to properly tighten the control nuts on the three rotary controls, and to tighten the PCB to plastic carrier screws without overtightening and stripping them. A quick word about screwdrivers, which maybe should have been mentioned earlier. This radio was manufactured in Japan and therefore uses JIS screws throughout. As a result, JIS screwdrivers are needed to loosen any tight screws without stripping the drive recess in the screw head. Standard Phillips screwdrivers or any variation thereof will certainly cause damage to the screw heads. During disassembly, I found that one of the screws that secured the shield plate and the front panel metal frame to the radio chassis had been stripped in that manner, telling me that someone had been into this radio before and most likely had not realized at first that the screws were JIS screws. I used a specialized extractor to remove the screw, and I replaced that screw upon reassembly with a new JIS 3mm-0.5mm x 6mm flat head machine screw from my inventory.
Remember that in screw dimensioning, the first part (before the hyphen) is the nominal thread diameter, while the second part (after the hyphen) is the thread pitch reference (more about that later). The number after the “x” is the fastener length. Metric fasteners and Imperial fasteners utilize different thread pitch designation methods. With a metric threaded fastener, the pitch information is reported as the distance from the peak of one thread to the peak of the adjacent thread. Thus, a machine screw with a pitch designation of 0.5mm will have a measured distance of one-half of a millimeter from one thread peak to the next. Imperial fasteners use a system that reports the number of thread peaks in an inch of fastener length. Thus, a machine screw with a pitch designation of 32 will have 32 thread peaks in an inch of screw length. Keep in mind also that while most headed fasteners are length-measured from the underside of the head, flat-head fasteners are length-measured for overall length, including the head length.
Reconnecting of the various wire harness plugs to the main PCB is pretty much a straight-forward matter of matching the plug size to the socket size. The is only one possible mix-up, and that is with the squelch control harness plug and the speaker harness plug. This can be resolved easily if the photos recommended earlier were taken. If not, refer to the schematic diagram found in the IC-3210 service manual to determine that the squelch control harness plug goes to connector J6 on the main PCB, while the speaker harness plug goes to connector J9.
Once the reassembly is complete, it is time for a functional test of the repairs. As luck would have it, another problem became evident quite quickly. It turned out that the rotary control used as the main up/down control signal source was inoperative. As a result, frequency could not be adjusted within each band, although the radio was otherwise fully functional on each of its two bands. In a similar manner, none of the radio’s optional settings that require an up/down selection normally made via that control were operational. Thus, the tuning step intervals, the CTCSS tones, and several other functions could not be changed. The problem gets worse… it turns out that the microphone Up/Down controls were also inoperable. This would seem to point to some circuit or component that is common to both control methods. In this case, I worked through the block diagram, the unit schematic, and the X-Ray views of the printed circuit boards in an effort to try to isolate the cause of this problem. Unfortunately, all of this testing and probing led to the inescapable conclusion that the problem lies within the logic board CPU integrated circuit, a µPD75308GF-101-3B9 device that is no longer available. So… while the relatively minor faults for which the radio came in were all corrected, the radio is nonetheless still inoperable, as the VFO frequencies cannot be changed. When powered on, the radio comes up on the designated calling frequencies of 146.520 MHz for VHF and 446.000 MHz for UHF.
Continued testing showed that one of the four output strobe lines from the CPU to the control matrices was extremely low in voltage as compared to the other three strobe lines, though its signal waveform was of the correct shape - just lower in amplitude than it should have been. I also noted that when exercising any of the switches on that particular strobe line, there was no response in the CPU, as those lines were not brought to a deep low with the switch activation - they were already low, so the CPU did not see the switch activations as changes of state on those lines. Unfortunately, no ready repair was available for this problem, as the CPU integrated circuit is obsolete and is therefore currently unavailable.
Sometimes, due to the so-called “planned obsolescence” so prevalent in the output of many of today’s manufacturing plants, an otherwise great little dual-band radio is relegated to the junk pile. I will keep my eyes and ears open on the lookout for another IC-3210 that I can pick up for parts, but I imagine that to be a rather futile effort. There are surprisingly few hits on Google when searching for that model number. I cannot in good conscience charge this radio owner a penny for my time spent and for the repairs that were made, as the end result was not a working radio.
See you next month!
NanoVNA H4 Touch Screen - June 2023
|
One recent Saturday afternoon, one of our fellow Club members had cause to use the Club’s NanoVNA for some new equipment testing. Unfortunately, when he tried to operate the unit, the touch-screen feature was not working, and in fact, it seemed that the menu system was completely inoperative. I decided to bring it home with me to make the required repairs.
The Club’s NanoVNA is the H4 (Figure 1) variant which, at the time, was loaded with the DiSlord version 1.1.01 firmware dated 30 December 2021. While the firmware was most |
likely not the cause of the problem, as the unit had been working fine for a long while, I did notice that the firmware was about a year and a half old, which is a lifetime by today’s electronic equipment standards. I slated it for a firmware update as a part of the repair.
In testing the NanoVNA quite thoroughly, I found that occasionally, I could get the menu system to operate via the multi-function control (MFC) wheel on the unit’s top edge, after which the touch screen would occasionally operate until the next power-off. However, it was not consistent enough to say that this would be a usable work-around, so I kept on digging for an answer.
I opened up the unit and disconnected the battery and the touch screen ribbon cable. I then reseated the ribbon cable, reconnected the battery, and powered up the device. No change was evident, with the touch screen and menu system operating the same as it had before the disconnects.
A few more words about the actual behavior would seem appropriate at this point. If I was able to get the menu system to launch using the MFC wheel, it was then possible to navigate the menu using the stylus via the touch screen. It was even possible to re-launch the menu system via the touch screen, until the unit was powered off. Then the problem re-asserted itself and it was pot luck as to whether or not the menus would open via the MFC.
I turned to that giant reference resource called the internet for some help, and I came across an obscure reference in a forum somewhere - I never noticed where - that made mention of NanoVNA stability. This seemed to fit, so I looked some more into that concept - stability and how to control it. What I found was that the default settings for the DiSlord firmware versions are set to slightly over-clock the NanoVNA. I decided to slow it down a little bit and see what happens.
The clock speed of the NanoVNA is controlled by a firmware value called Threshold, which is set to 300.000100MHz by default. The Threshold setting (Figure 2) is found under Config > Expert Settings. I decided to set it down to 290MHz. Voilá! The touch screen now behaved normally in every regard! I figured that I had resolved this issue, though I still did not understand what had happened, or specifically why it spontaneously stopped working after operating for so long, but I chose not to worry about that at this point.
In testing the NanoVNA quite thoroughly, I found that occasionally, I could get the menu system to operate via the multi-function control (MFC) wheel on the unit’s top edge, after which the touch screen would occasionally operate until the next power-off. However, it was not consistent enough to say that this would be a usable work-around, so I kept on digging for an answer.
I opened up the unit and disconnected the battery and the touch screen ribbon cable. I then reseated the ribbon cable, reconnected the battery, and powered up the device. No change was evident, with the touch screen and menu system operating the same as it had before the disconnects.
A few more words about the actual behavior would seem appropriate at this point. If I was able to get the menu system to launch using the MFC wheel, it was then possible to navigate the menu using the stylus via the touch screen. It was even possible to re-launch the menu system via the touch screen, until the unit was powered off. Then the problem re-asserted itself and it was pot luck as to whether or not the menus would open via the MFC.
I turned to that giant reference resource called the internet for some help, and I came across an obscure reference in a forum somewhere - I never noticed where - that made mention of NanoVNA stability. This seemed to fit, so I looked some more into that concept - stability and how to control it. What I found was that the default settings for the DiSlord firmware versions are set to slightly over-clock the NanoVNA. I decided to slow it down a little bit and see what happens.
The clock speed of the NanoVNA is controlled by a firmware value called Threshold, which is set to 300.000100MHz by default. The Threshold setting (Figure 2) is found under Config > Expert Settings. I decided to set it down to 290MHz. Voilá! The touch screen now behaved normally in every regard! I figured that I had resolved this issue, though I still did not understand what had happened, or specifically why it spontaneously stopped working after operating for so long, but I chose not to worry about that at this point.
I next went about performing a firmware upgrade on the NanoVNA. This is a simple operation that is done using the STMicroelectronics DfuSe software. I had the software (Figure 3) installed on my PC already, so all that I needed to do was to download the newest DiSlord firmware file in the commonly-used .dfu firmware format. That filename is NanoVNA.H4.v1.2.20.dfu which indicates that the firmware is version 1.2.20, dated 12 March 2023. The various firmware files can be downloaded from https://github.com/DiSlord/NanoVNA-D/releases under the Assets listing.
To update the firmware in the NanoVNA, the device must be placed into DFU mode. Start out by launching the STMicro DfuSe software and connecting the NanoVNA to the PC via an appropriate USB cable. Then, put the NanoVNA into DFU mode by holding down the MFC wheel while powering up the unit. Note that the screen will remain black in DFU mode, but the STMicro DfuSe software should indicate that the NanoVNA is connected and accessible. The net step is to use the Choose button in the DfuSe software to open the .dfu firmware file. The software will show (Figure 4) that the firmware file was successfully loaded into the utility and that it is ready for upload to the device. Upload that file to the device by clicking the Upgrade button. Once the upgrade is completed as indicated in the software (Figure 5), power off the NanoVNA and disconnect it from the PC.
The interesting thing about this repair is that post-upgrade of the firmware, that new firmware Threshold setting was once again set to 300.000100MHz… but the unit was operating properly and with many more menu options than it had before.
OK - so slowing the clock speed solved the initial touch screen response issue in the old firmware. Of that there is no doubt. As a result, I feel comfortable suggesting that as a solution for anyone who may encounter a similar issue with the touch screen on a NanoVNA H4 and needs an immediate fix.
I also feel comfortable recommending the firmware upgrade to DiSlord version 1.2.20, as I have now installed and tested it extensively, and everything works as it should. Some of the new features include the ability to save a calibration set to the SD card, enter a custom name for any image file saved to the SD card (or simply check the Autoname check box to avoid having to enter a name - it will default to a date and time format naming convention). The new firmware allows loading an image from the SD card into the display, and there is also a Pause Sweep and Resume Sweep capability now. There are several changes to the Calibrate menu item as well as to several other menu items. This new firmware version is feature-rich and is well worth installing.
Having explored the new menu items and capabilities of the NanoVNA H4 under DiSlord firmware 1.2.20, I am happy to report that all of the new features work well, and are for the most part self-explanatory or very intuitive. This makes these new features easy to use without needing any type of documentation for them. I like the new firmware so much that I also installed it onto my personal H4 unit.
See you next month…
To update the firmware in the NanoVNA, the device must be placed into DFU mode. Start out by launching the STMicro DfuSe software and connecting the NanoVNA to the PC via an appropriate USB cable. Then, put the NanoVNA into DFU mode by holding down the MFC wheel while powering up the unit. Note that the screen will remain black in DFU mode, but the STMicro DfuSe software should indicate that the NanoVNA is connected and accessible. The net step is to use the Choose button in the DfuSe software to open the .dfu firmware file. The software will show (Figure 4) that the firmware file was successfully loaded into the utility and that it is ready for upload to the device. Upload that file to the device by clicking the Upgrade button. Once the upgrade is completed as indicated in the software (Figure 5), power off the NanoVNA and disconnect it from the PC.
The interesting thing about this repair is that post-upgrade of the firmware, that new firmware Threshold setting was once again set to 300.000100MHz… but the unit was operating properly and with many more menu options than it had before.
OK - so slowing the clock speed solved the initial touch screen response issue in the old firmware. Of that there is no doubt. As a result, I feel comfortable suggesting that as a solution for anyone who may encounter a similar issue with the touch screen on a NanoVNA H4 and needs an immediate fix.
I also feel comfortable recommending the firmware upgrade to DiSlord version 1.2.20, as I have now installed and tested it extensively, and everything works as it should. Some of the new features include the ability to save a calibration set to the SD card, enter a custom name for any image file saved to the SD card (or simply check the Autoname check box to avoid having to enter a name - it will default to a date and time format naming convention). The new firmware allows loading an image from the SD card into the display, and there is also a Pause Sweep and Resume Sweep capability now. There are several changes to the Calibrate menu item as well as to several other menu items. This new firmware version is feature-rich and is well worth installing.
Having explored the new menu items and capabilities of the NanoVNA H4 under DiSlord firmware 1.2.20, I am happy to report that all of the new features work well, and are for the most part self-explanatory or very intuitive. This makes these new features easy to use without needing any type of documentation for them. I like the new firmware so much that I also installed it onto my personal H4 unit.
See you next month…
Brother P-Touch® 1400 Label Printer – May 2023
|
Fairly recently, I was presented with a somewhat different type of repair. One of my fellow radio Club members asked me if I would take a look at a favorite and trusted piece of his shack equipment, namely a Brother P-touch® 1400 hand-held label printer (Figure 1). The printer had stopped responding to the “Y” key, and its owner was hoping that I could repair the machine for him. Enjoying a challenge, I told him that I would take it on, but without any up-front guarantee of success.
The owner brought the machine to me, and I quickly determined that not only did the “Y” key not work at all, the other keys along the right edge of the keyboard were rather “mushy” and not crisp and quick as they should have been. I opened up the unit to find that the printed circuit board on which the key contacts were etched had delaminated at a mounting pad along its right-hand edge, directly in alignment with the “Y” key, and breaking the circuit traces for that key and one other. This was apparently a product of years of use and pressure on that portion of the board. The keyboard consists of a matrix of conductive pads etched onto the top surface of a phenolic board that also serves as a printed circuit board for some of the related circuitry. Each key |
contains a carbon button on its underside that bridges the conductive pads when the key is pressed. Simple enough, right? The problem was that the board had split between its layers (Figure 2), tearing the circuit traces on its upper surface. I was faced with a dual problem – how to first repair the delaminated phenolic board, and then how to repair the circuit traces (Figure 3) so that the machine would operate properly afterwards.
The first problem was solved with some cyanoacrylate glue, applied between the layers, with the layers then being clamped together with the broken section positioned back where it belonged. I clamped it up and set it aside to cure, having placed some waxed paper between the clamp faces and the board surfaces so that the clamp would not end up glued to the board by the excess glue squeeze-out. I then started thinking about the most effective manner in which to repair the circuit traces, assuming that the glue job would hold, of which I was not certain yet.
The most common method of repairing lifted or broken printed circuit traces, by far, is to simply scrape the trace to expose the conductive surface, and then to overlay the trace with some bare wire, and to then solder the wire to the trace. While this might work in some cases, it would clearly not be an effective repair in this situation, as one broken trace was directly in the area where the “Y” key’s carbon button would have to make contact with the board if that key were to be pressed. Any raised area of the board would be problematic in allowing the carbon button to successfully bridge the pads, which actually contain interlaced “fingers” (Figure 4) rather than being geometrically shaped areas. I needed a better solution.
The first problem was solved with some cyanoacrylate glue, applied between the layers, with the layers then being clamped together with the broken section positioned back where it belonged. I clamped it up and set it aside to cure, having placed some waxed paper between the clamp faces and the board surfaces so that the clamp would not end up glued to the board by the excess glue squeeze-out. I then started thinking about the most effective manner in which to repair the circuit traces, assuming that the glue job would hold, of which I was not certain yet.
The most common method of repairing lifted or broken printed circuit traces, by far, is to simply scrape the trace to expose the conductive surface, and then to overlay the trace with some bare wire, and to then solder the wire to the trace. While this might work in some cases, it would clearly not be an effective repair in this situation, as one broken trace was directly in the area where the “Y” key’s carbon button would have to make contact with the board if that key were to be pressed. Any raised area of the board would be problematic in allowing the carbon button to successfully bridge the pads, which actually contain interlaced “fingers” (Figure 4) rather than being geometrically shaped areas. I needed a better solution.
The next day, still unsure of how to repair the traces, I removed the clamp and waxed paper to find that the board was indeed back into a semblance of its original condition. I used some acetone on a cotton swab to clean the squeezed-out CA glue from the board surface in the area of concern, and the board was ready for trace repairs to begin. Still not having a repair scheme in mind, I put it aside for the day and moved on to something else, having already sent photos of the damage to the machine’s owner and having told him that a repair might not be feasible. I went to bed that night thinking about the problem.
At some point during the night, and driven by some unknown and not understood “force”, I hit upon an idea that might just work. I had read a while back about pens that write with conductive ink, which contains powdered silver in a volatile carrier. It was well worth a try, so I ordered one of the pens from Amazon and waited another day for it to arrive. Lo and behold, when I tried the pen on some paper, and then measured the resistance of the drawn lines, I found them to be very low impedance traces, and with almost no appreciable height on the paper surface.
I tried some basic experiments to determine the current-carrying capability of the ink, and found that I could easily pass 500mA through a trace that was two pen-points in width. This looked very promising indeed! I decided to try the ink on the phenolic board.
To make this idea work, I would have to expose some of the conductive surface of the existing traces for the ink to connect into the original circuit properly. That was a chore best done with the edge of a hobby knife blade, and that is exactly how I achieved the exposure that I needed. I then laid the ink down in place (Figure 5) over the almost invisible cracks in the repaired surface of the board, and checked the results with an ohmmeter. So far, do good. Now for the acid test. Will the key work when coming into contact with the ink and the original traces? A quick test with the keyboard membrane laid over the board proved that it would actually work as intended.
After that, all that was required was to reassemble the machine with the repaired PCB (Figure 6) and to do a final working test of the entire keyboard. That post-assembly test proved successful, and so the repair was complete. The lessons found in this repair are two-fold.
First, think out of the box when faced with an unusual problem, as unusual problems often require unusual repair methods.
Second, do not give up too easily. Plan for the worst, but work towards the best, and let your unconscious mind work on the problem for a while.
You might just know how to achieve a repair, even if you don’t know that you know how to do it!
See you next month.
Icom ID-800H – April 2023
|
Sometimes, finding the cause of a problem can be more than the repair technician is up to. At those times, the technician has to be careful not to do any harm to the equipment and cause further failures while trying to ferret out the root cause of the initial failure. Sometimes, like the infamous Zorro, the technician leaves his/her mark in the night, gives up, and moves on. That is when the failure becomes another technician’s problem to solve.
|
A little while ago, I got an email from a ham out in Cleveland, Tennessee who asked if I would be willing and able to take on a “mystery” repair on an Icom ID-800H 2-meter/70-centimeter dual-band mobile radio (Figure 1). The unit had an intermittent fault that two other shops had attempted to repair and both gave up without finding the problem. In addition, one of the two shops caused an additional failure, which we will get into in a little while.
The original problem was related to the occasional and unpredictable blown fuse on the incoming power line. The ID-800H was vehicle-mounted in a 2022 Peterbilt 579 (Figure 2) Class 8 truck-tractor. The secondary problem was a lack of audio from the radio unless an external speaker was installed and connected. This problem showed up when the radio came back from the second repair shop. The owner is an over-the-road long-distance trucker who has historically had his radio - CB’s and ham - all repaired at truck stop radio shops.
When the problem first appeared, the owner took the radio to a radio shop at a truck stop in Carlisle, PA. Of course, as nothing was actually repaired other than replacement of the blown fuse, the problem eventually re-occurred. At this point, the owner replaced the fuse himself, and the radio worked as it was intended to, for a while. At some point, the owner happened to have some time to kill while in Kenly, NC, so he took the radio to a radio shop at a truck stop there. This time when he reinstalled it in the truck, it worked again, except that there was no audio from the internal speaker. This was annoying, and the owner assumed that the repairman simply forgot to reconnect the speaker wire harness to the mainboard on re-assembly. However, due to the ambient noise level in the truck, he customarily used an amplified external speaker anyway, so he didn’t fret too much about it. Needless to say, the radio was still blowing fuses at random times.
Fast-forward to the first of the year. As of 1 January 2023, the owner came off the road and began operating as a local, home-every-night driver, and the radio came out of the truck to be used in his shack at home, except that it still had that pesky fuse-blowing problem, which is where I entered the story.
The owner explained the entire history to me, and after some judicious questions, I determined that the fuse most often blew while the truck was in motion, though it would occasionally blow when the vehicle was stationary. He wanted me to find and fix the fuse blowing issue once and for all… and oh yeah - plug in the speaker, too. He shipped the radio to me, but he did not include the power cable, so I had to use a bench cable with a fuse holder (Figure 3) to power the radio for testing, to which I added Anderson PowerPole® for my own convenience.
I put the radio on the bench and connected up the incoming power, a dummy load, and an external speaker… and the radio worked normally. I then decided to connect it to an antenna - my trusty Ed Fong J-Pole - and to use it on the Tuesday net. The radio worked flawlessly, albeit through the external speaker. I decided that I would try to emulate the rough ride of the truck where the radio used to live… I picked it up and I shook it while it was operating. I shook it, I banged on it, I bounced it on a stack of towels… and nothing. It never missed a beat. Next, I tried some “unusual attitudes” as we used to call it in flight school. I started twisting and turning the radio while bouncing it on the stack of towels. Finally, when I stood the unit up on end with the front face upwards, and bounced it hard on the towel stack, it finally blew the fuse. I replaced the fuse and tried the same thing again, and once more the fuse blew with the same maneuvers.
So, what did I prove? Well… I showed two things to be true :
The original problem was related to the occasional and unpredictable blown fuse on the incoming power line. The ID-800H was vehicle-mounted in a 2022 Peterbilt 579 (Figure 2) Class 8 truck-tractor. The secondary problem was a lack of audio from the radio unless an external speaker was installed and connected. This problem showed up when the radio came back from the second repair shop. The owner is an over-the-road long-distance trucker who has historically had his radio - CB’s and ham - all repaired at truck stop radio shops.
When the problem first appeared, the owner took the radio to a radio shop at a truck stop in Carlisle, PA. Of course, as nothing was actually repaired other than replacement of the blown fuse, the problem eventually re-occurred. At this point, the owner replaced the fuse himself, and the radio worked as it was intended to, for a while. At some point, the owner happened to have some time to kill while in Kenly, NC, so he took the radio to a radio shop at a truck stop there. This time when he reinstalled it in the truck, it worked again, except that there was no audio from the internal speaker. This was annoying, and the owner assumed that the repairman simply forgot to reconnect the speaker wire harness to the mainboard on re-assembly. However, due to the ambient noise level in the truck, he customarily used an amplified external speaker anyway, so he didn’t fret too much about it. Needless to say, the radio was still blowing fuses at random times.
Fast-forward to the first of the year. As of 1 January 2023, the owner came off the road and began operating as a local, home-every-night driver, and the radio came out of the truck to be used in his shack at home, except that it still had that pesky fuse-blowing problem, which is where I entered the story.
The owner explained the entire history to me, and after some judicious questions, I determined that the fuse most often blew while the truck was in motion, though it would occasionally blow when the vehicle was stationary. He wanted me to find and fix the fuse blowing issue once and for all… and oh yeah - plug in the speaker, too. He shipped the radio to me, but he did not include the power cable, so I had to use a bench cable with a fuse holder (Figure 3) to power the radio for testing, to which I added Anderson PowerPole® for my own convenience.
I put the radio on the bench and connected up the incoming power, a dummy load, and an external speaker… and the radio worked normally. I then decided to connect it to an antenna - my trusty Ed Fong J-Pole - and to use it on the Tuesday net. The radio worked flawlessly, albeit through the external speaker. I decided that I would try to emulate the rough ride of the truck where the radio used to live… I picked it up and I shook it while it was operating. I shook it, I banged on it, I bounced it on a stack of towels… and nothing. It never missed a beat. Next, I tried some “unusual attitudes” as we used to call it in flight school. I started twisting and turning the radio while bouncing it on the stack of towels. Finally, when I stood the unit up on end with the front face upwards, and bounced it hard on the towel stack, it finally blew the fuse. I replaced the fuse and tried the same thing again, and once more the fuse blew with the same maneuvers.
So, what did I prove? Well… I showed two things to be true :
- That the fuse did blow after some violent jarring of the radio.
- The behavior was repeatable.
Now it was time to open up the radio and the service manual, and to start investigating the internals. It just so happens that I have one of these radios myself, which may come into play for some comparisons, if necessary.
I disconnected the radio and opened it up, and the very first thing that I noted was that the speaker wire harness was indeed connected to the mainboard. This meant that I would need to dig a bit into the audio issue as well, to get to the cause of that problem. More on that later.
As usual, I began by looking for any visible indications of something burnt, arced, or otherwise indicating a short circuit, but nothing jumped out at me. I removed the RF shield from the mainboard to look underneath it as well. Finding nothing the easy way, I decided to emulate my vigorous treatment of the radio. With a new fuse in the power wire fuse holder and the unit power on, I began to gently poke and prod various points in the radio using a plastic alignment tool as the prod. Nothing happened until I prodded the wire harness for the cooling fan. As soon as I touched this wire pair, it arced against the chassis rear heat sink and the fuse blew. Success!
Closer examination revealed a chafed area (Figure 4) in the red wire to the fan, exposing the bare wire inside the red insulation. I surmise that this wire would, with enough of a jar to the radio, move just enough to short against the heat sink, causing the fuse to blow. A look at the schematic shows that the fan is fed almost full supply voltage, dropped only by a 6.8Ω resistor in series with the fan positive lead. The fan supply, on lead HVI, traces back from the 6.8Ω fuse R102 directly to the incoming 13.8VDC power inlet. Fan control is all done on the fan’s negative lead. Thus, shorting the fan’s positive lead to ground is tantamount to placing a direct short on the positive power feed to the radio, causing the fuse to open.
The repair was fairly simple. Using the tip of a hobby knife, I gently lifted the latch of the red wire terminal in the fan harness plug, and pulled the wire and terminal from the plug (Figure 5). I then slipped a short piece of narrow heat shrink tube on the wire and hit it with hot air from the heat gun. Once the HST was shrunk in place, I inserted the terminal back into the plug (Figure 6). After that, it was a simple matter to re-mount the fan and plug it in onto the mainboard.
Now it was time to look for the audio problem. As a refresher, the radio had audio only via an external speaker. No sound came from the internal speaker, which was plugged in onto the mainboard in the correct location. The owner had thought that perhaps the last repairman had forgotten to connect the speaker harness, but that was not the case, as I discovered. I had to start somewhere, so I started at the speaker connector on the mainboard. To my surprise, there was a strong audio signal there at the speaker header. Thus, the problem had to be in either the speaker or its connecting harness. I took a “AA” battery that I keep on hand with a clip lead soldered to each end, and I did a momentary “scratch” test of the speaker, which responded with a typical characteristic static scratch. The speaker coil was intact, which narrowed down the problem. It had to be a harness issue.
I took a good close look at the plug end of the harness and found that one of the wires was out of the plug body, and therefore was not able to make contact with the header pin. My guess is that when the last repairman disconnected the speaker on opening the radio, he pulled the wire from the plug (Figure 7) and did not notice it. I certainly did not notice it until I had reason to take a good look at the plug. I pushed the wire all the way into the plug body and connected the harness. Magic! The dead audio was once again alive.
I reassembled the radio and once more subjected it to a violent thrashing in an attempt to blow another fuse, but failed to do so. I took that as a sign that the repair was effective, so I boxed it up, less the power cord, and shipped it back to Tennessee, together with my invoice and two spare fuses.
What lessons can be learned from this repair? I see a couple of them. Let’s take them one at a time, and explore their validity and value.
First off, I think that the fix isn’t made until the repair person actually finds the cause of the problem. Fixing a symptom, in this case the blown fuses, does not repair the equipment, not so long as the root cause has not been located. Without correcting the root cause, the symptom is bound to re-appear at some point in time. The fact that this radio was riding around in an eighteen-wheeler, and taking an aggressive hammering as the truck traveled America’s highways and byways, meant that the unit was being put through some unusual operating conditions. It was when I emulated that pounding ride that I was able to reproduce the symptom, reliably and repeatedly. Think outside the box and consider all operating conditions when tracking down a symptom like this one.
Second, it is obvious to me that the second repair shop failed to do any kind of active post-repair testing of the radio, because if such testing had been done, it would have been obvious that a new problem had been introduced in that the speaker audio output was nil. Perhaps the repairman thought that the radio had been like that when it came to him, but the owner says otherwise. It is important that the repaired radio be put through all of its paces post-repair just to make sure that something like this has not happened. It is understandable how it happened; it is inexcusable that it left the shop like that.
I am not saying that my repairs are perfect - I am human, and so I will make mistakes and miss things, as I have in the past. However, any shop should be able to pick the low-hanging fruit and fix the easy ones. The more difficult ones just take a little bit longer, or maybe a lot longer.
See you next month!
I disconnected the radio and opened it up, and the very first thing that I noted was that the speaker wire harness was indeed connected to the mainboard. This meant that I would need to dig a bit into the audio issue as well, to get to the cause of that problem. More on that later.
As usual, I began by looking for any visible indications of something burnt, arced, or otherwise indicating a short circuit, but nothing jumped out at me. I removed the RF shield from the mainboard to look underneath it as well. Finding nothing the easy way, I decided to emulate my vigorous treatment of the radio. With a new fuse in the power wire fuse holder and the unit power on, I began to gently poke and prod various points in the radio using a plastic alignment tool as the prod. Nothing happened until I prodded the wire harness for the cooling fan. As soon as I touched this wire pair, it arced against the chassis rear heat sink and the fuse blew. Success!
Closer examination revealed a chafed area (Figure 4) in the red wire to the fan, exposing the bare wire inside the red insulation. I surmise that this wire would, with enough of a jar to the radio, move just enough to short against the heat sink, causing the fuse to blow. A look at the schematic shows that the fan is fed almost full supply voltage, dropped only by a 6.8Ω resistor in series with the fan positive lead. The fan supply, on lead HVI, traces back from the 6.8Ω fuse R102 directly to the incoming 13.8VDC power inlet. Fan control is all done on the fan’s negative lead. Thus, shorting the fan’s positive lead to ground is tantamount to placing a direct short on the positive power feed to the radio, causing the fuse to open.
The repair was fairly simple. Using the tip of a hobby knife, I gently lifted the latch of the red wire terminal in the fan harness plug, and pulled the wire and terminal from the plug (Figure 5). I then slipped a short piece of narrow heat shrink tube on the wire and hit it with hot air from the heat gun. Once the HST was shrunk in place, I inserted the terminal back into the plug (Figure 6). After that, it was a simple matter to re-mount the fan and plug it in onto the mainboard.
Now it was time to look for the audio problem. As a refresher, the radio had audio only via an external speaker. No sound came from the internal speaker, which was plugged in onto the mainboard in the correct location. The owner had thought that perhaps the last repairman had forgotten to connect the speaker harness, but that was not the case, as I discovered. I had to start somewhere, so I started at the speaker connector on the mainboard. To my surprise, there was a strong audio signal there at the speaker header. Thus, the problem had to be in either the speaker or its connecting harness. I took a “AA” battery that I keep on hand with a clip lead soldered to each end, and I did a momentary “scratch” test of the speaker, which responded with a typical characteristic static scratch. The speaker coil was intact, which narrowed down the problem. It had to be a harness issue.
I took a good close look at the plug end of the harness and found that one of the wires was out of the plug body, and therefore was not able to make contact with the header pin. My guess is that when the last repairman disconnected the speaker on opening the radio, he pulled the wire from the plug (Figure 7) and did not notice it. I certainly did not notice it until I had reason to take a good look at the plug. I pushed the wire all the way into the plug body and connected the harness. Magic! The dead audio was once again alive.
I reassembled the radio and once more subjected it to a violent thrashing in an attempt to blow another fuse, but failed to do so. I took that as a sign that the repair was effective, so I boxed it up, less the power cord, and shipped it back to Tennessee, together with my invoice and two spare fuses.
What lessons can be learned from this repair? I see a couple of them. Let’s take them one at a time, and explore their validity and value.
First off, I think that the fix isn’t made until the repair person actually finds the cause of the problem. Fixing a symptom, in this case the blown fuses, does not repair the equipment, not so long as the root cause has not been located. Without correcting the root cause, the symptom is bound to re-appear at some point in time. The fact that this radio was riding around in an eighteen-wheeler, and taking an aggressive hammering as the truck traveled America’s highways and byways, meant that the unit was being put through some unusual operating conditions. It was when I emulated that pounding ride that I was able to reproduce the symptom, reliably and repeatedly. Think outside the box and consider all operating conditions when tracking down a symptom like this one.
Second, it is obvious to me that the second repair shop failed to do any kind of active post-repair testing of the radio, because if such testing had been done, it would have been obvious that a new problem had been introduced in that the speaker audio output was nil. Perhaps the repairman thought that the radio had been like that when it came to him, but the owner says otherwise. It is important that the repaired radio be put through all of its paces post-repair just to make sure that something like this has not happened. It is understandable how it happened; it is inexcusable that it left the shop like that.
I am not saying that my repairs are perfect - I am human, and so I will make mistakes and miss things, as I have in the past. However, any shop should be able to pick the low-hanging fruit and fix the easy ones. The more difficult ones just take a little bit longer, or maybe a lot longer.
See you next month!
Icom ID-4100A – March 2023
|
Sometimes, you have to repair - or at least I have to repair - my own equipment. And, sometimes the old adage about “getting what you pay for” is true. In this case, it certainly came true. I had been having occasional problems with my Icom ID-4100A (Figure 1) powering itself off, most often at the end of a transmission, but occasionally during receive operations. |
There was no rhyme or reason to when this would happen. It might happen twice during a net, or it might go several weeks without occurring. I was always able to restore the radio to operation by power-cycling the power supply, and I was therefore half convinced that the problem was internal to the radio, so I set about trying to locate the problem.
My first step was to take the ID-4100A out of service. I unplugged the power cord at the “T” connector (Figure 2) that is so common on mobile radios today. The radio that I was swapping in there temporarily, an Icom ID-800H, had the same type of power cord, so it was a plug-in replacement as far as the connections went - power cord and antenna cable.
I fired up the ID-800H and all was well. I set the ID-4100A aside for repairs when I could fit the job into my schedule, reasoning that there was no hurry as I had yet another 2-meter set available if the ID-800H should fail, a Yaesu FT-1900. In this way, I should not have to resort to my handheld for the nets, right?
Two weeks go by, meaning four nets in which I participated, for two of which I was the Net Control Station, and all was working well. I sat there thinking through the ID-4100A problem, and poring over the schematic and block diagram, looking for the most likely place to start in troubleshooting the shutdown issue, but had not yet reached any definite conclusions.
Another week goes by, with two more nets. During the Thursday net, the old faithful ID-800H shut down, exactly as the ID-4100A had been doing! Stop the truck and back it up. I concluded now that the problem was not in the radio after all. At this point, I began suspecting the power supply instead, as it was common to the two radios. I decided to watch carefully the next time the radio went dead to see how the power supply behaved. I got a bit of a surprise doing that.
The next time the radio fell dead was the Tuesday net two weeks later. Throughout the net, I sat there staring at the front of the power supply, studying its backlighting and the output monitor meter. What I saw there puzzled me for a few minutes… the power supply showed a momentary spike in output current just as the radio died, but then dropped to a zero-current state.
The output voltage had momentarily sagged a little bit, but then jumped right back up to the normal 13.8VDC available output. This told me that the problem was neither the radio nor the power supply, but something in between them. The only thing between the power supply and the radio was the six-port Powerpole® distribution block that I had mounted behind the desk, and of course the power cables themselves. No fuses had blown through all of this, with either radio.
I went to the Powerpole® distribution block and carefully examined both it and the power cords connected to it. Much to my surprise, I found that the port to which my 2-meter radio was connected looked melted, very slightly on the black connector shell, but quite heavily on the red shell (Figure 3). This melting had occurred on both the cable end (Figure 4) and the distribution block port. I disconnected the cable from that port and got another surprise. Inside the red shell of the cable, the contact was not all the way out to the end of the connector shell as it should have been. Instead, it was pushed back a little bit, enough to cause the connection made when the plug bodies were joined to be somewhat less than optimal. Apparently, this connection would occasionally open, usually when heavier current was drawn during transmission. The heat caused by the resistance formed there is what melted the connector bodies.
This particular cable was an ebay.com buy that I picked up before I got my Powerpole® assembly kit in house. I needed a power pigtail for the mobile-type radios, so I bought a couple of inexpensive ones on the auction site.
My guess is that the actual contact was never fully inserted into the connector body far enough to lock into place. It simply pushed away from its mating contact, maintaining a light touch with its mate, but opening up under load. This caused me to inspect the second cable that I bought at that time, but it was assembled correctly, with the contacts in place where they belonged.
The fix for the cable was simple. Cut off the melted connector and crimp on a new pair of Powerpole® connectors. I keep the Powerpole® parts on hand, so that was no problem. The repair to the distribution block was not quite as simple.
The distribution block has a metal cover secured in place by four small flat-head machine screws, so disassembly was easy. I removed the screws and lifted off the cover, exposing the inside of the unit. Inside, there was a small printed circuit board (Figure 5) having bus bars along its outer edges to help handle the rated current of the unit. Each of the Powerpole® shells was installed to a blade-type contact that is soldered into the PCB. I fooled around with trying to release the contact from the body and to slide the body off, but that was going nowhere fast. Ultimately, I decided to try a more direct approach. I took a pair of pliers and simply crushed the melted red connector body, causing it to separate from its contact a bit.
Then it was just a matter of using pliers to grip and wiggle it off the contact, sort of like pulling a tooth (Figure 6). After that, all that was left was the job of forcing a new connector body down in place of the melted one. The black connector body was intact, so I was able to leave that one alone.
After the connector shell was replaced, reassembly of the distribution block was the reverse of the disassembly procedure. The only tricky part was reinstalling the three miniature truss-head machine screws that secure the PCB to the lower enclosure half, as they are buried down between the Powerpole® shells.
With the distribution block repaired and reassembled (Figure 7), it was time to put it back into service, which I did. The new connectors on the power cable, properly assembled this time, worked as they should, and the problem of the dead radio has not occurred since the repairs.
The lesson in all of this is to inspect every piece of kit that you buy, because even “brand new” items might be defective. Had I inspected this cable before use, I may have noticed that the contact was not seated and I could have corrected it. All that would have been needed was to properly seat the contact in the connector shell by pushing in until it clicked into place. I failed to do so, and ended up with a mystery to solve as a result.
See you next month!
I went to the Powerpole® distribution block and carefully examined both it and the power cords connected to it. Much to my surprise, I found that the port to which my 2-meter radio was connected looked melted, very slightly on the black connector shell, but quite heavily on the red shell (Figure 3). This melting had occurred on both the cable end (Figure 4) and the distribution block port. I disconnected the cable from that port and got another surprise. Inside the red shell of the cable, the contact was not all the way out to the end of the connector shell as it should have been. Instead, it was pushed back a little bit, enough to cause the connection made when the plug bodies were joined to be somewhat less than optimal. Apparently, this connection would occasionally open, usually when heavier current was drawn during transmission. The heat caused by the resistance formed there is what melted the connector bodies.
This particular cable was an ebay.com buy that I picked up before I got my Powerpole® assembly kit in house. I needed a power pigtail for the mobile-type radios, so I bought a couple of inexpensive ones on the auction site.
My guess is that the actual contact was never fully inserted into the connector body far enough to lock into place. It simply pushed away from its mating contact, maintaining a light touch with its mate, but opening up under load. This caused me to inspect the second cable that I bought at that time, but it was assembled correctly, with the contacts in place where they belonged.
The fix for the cable was simple. Cut off the melted connector and crimp on a new pair of Powerpole® connectors. I keep the Powerpole® parts on hand, so that was no problem. The repair to the distribution block was not quite as simple.
The distribution block has a metal cover secured in place by four small flat-head machine screws, so disassembly was easy. I removed the screws and lifted off the cover, exposing the inside of the unit. Inside, there was a small printed circuit board (Figure 5) having bus bars along its outer edges to help handle the rated current of the unit. Each of the Powerpole® shells was installed to a blade-type contact that is soldered into the PCB. I fooled around with trying to release the contact from the body and to slide the body off, but that was going nowhere fast. Ultimately, I decided to try a more direct approach. I took a pair of pliers and simply crushed the melted red connector body, causing it to separate from its contact a bit.
Then it was just a matter of using pliers to grip and wiggle it off the contact, sort of like pulling a tooth (Figure 6). After that, all that was left was the job of forcing a new connector body down in place of the melted one. The black connector body was intact, so I was able to leave that one alone.
After the connector shell was replaced, reassembly of the distribution block was the reverse of the disassembly procedure. The only tricky part was reinstalling the three miniature truss-head machine screws that secure the PCB to the lower enclosure half, as they are buried down between the Powerpole® shells.
With the distribution block repaired and reassembled (Figure 7), it was time to put it back into service, which I did. The new connectors on the power cable, properly assembled this time, worked as they should, and the problem of the dead radio has not occurred since the repairs.
The lesson in all of this is to inspect every piece of kit that you buy, because even “brand new” items might be defective. Had I inspected this cable before use, I may have noticed that the contact was not seated and I could have corrected it. All that would have been needed was to properly seat the contact in the connector shell by pushing in until it clicked into place. I failed to do so, and ended up with a mystery to solve as a result.
See you next month!
MFJ-259 HF/VHF SWR Analyzer - February 2023
|
This month’s case history is a slight departure from the norm, in that it involves the repair of a piece of test equipment. Notably, the unit under repair is one that I had already done some repair work to, prior to donating this piece to the Club for the test and repair bench. On a recent Saturday afternoon, Frank N3PUU had occasion to use the MFJ-259 SWR Analyzer while setting up the VHF station for an upcoming contest. Unfortunately, the unit did not operate as expected, and Frank left me a note to that effect. Naturally, I picked up the unit and brought it home for repair. What should have been a quite simple repair job turned into a little bit more than I had bargained for. The reported problem was that the meter was not reading, meaning that there was no indication of the tested SWR value. A quick check verified the condition, showing that the LCD panel was operational as to displaying the test frequency, but the meter movement was inoperative. However, I noticed that the meter came alive when I happened to jar the unit when I went to place it on the bench. That gave me a hint as to where to look for the problem. |
Diving in “under the hood”, so to speak, I quickly found some cracked solder joints on the unit’s main printed circuit board. There are two meters on the front panel of this unit. One is the SWR meter, and the other is a resistance meter. These two meters are connected to the main PCB via a three-wire harness with a 90° plug at its end (Figure 1). The plug connects to a three-pin right-angle pin header on the PCB. It was this header that had the cracked solder joints (Figure 2). A simple fix - I simply reflowed the solder on those pins and the meters worked as intended. However, I did not stop there.
You see, I had been bothered by this unit ever since I put it on the test and repair bench. I felt that I did not do as thorough a refurb job on this unit as I could have, and this was borne out by the fact that Frank had trouble with the unit when he tried to use it. One of the items that I had intended to replace but did not was the SO-239 jack on the top of the unit. I decided to go ahead and give the whole unit a closer look and to replace the SO-239 jack.
Replacement of the SO-239 connector requires removal of the main PCB, which in turn requires desoldering of the two pushbutton switches and the BNC jack on the unit’s upper surface. The SO-239 itself is connected to the main PCB in an unusual fashion. The center pin of the SO-239, when the main PCB is in place, sits about an eighth of an inch above the PCB. That gap is simply filled with solder at the factory. Each of the two mounting screws used for the SO-239 has a solder lug installed under its nut. The lugs are then bent over to reach the main PCB and are soldered to pads on the PCB. These solder lugs also do not quite reach the board surface, and so their gaps are also solder-filled in production (Figure 3). Large solder bridges of this type are prone to cracking with time, a condition with which I was not happy. I therefore decided to correct this as well.
Diving in “under the hood”, so to speak, I quickly found some cracked solder joints on the unit’s main printed circuit board. There are two meters on the front panel of this unit. One is the SWR meter, and the other is a resistance meter. These two meters are connected to the main PCB via a three-wire harness with a 90° plug at its end (Figure 1). The plug connects to a three-pin right-angle pin header on the PCB. It was this header that had the cracked solder joints (Figure 2). A simple fix - I simply reflowed the solder on those pins and the meters worked as intended. However, I did not stop there.
You see, I had been bothered by this unit ever since I put it on the test and repair bench. I felt that I did not do as thorough a refurb job on this unit as I could have, and this was borne out by the fact that Frank had trouble with the unit when he tried to use it. One of the items that I had intended to replace but did not was the SO-239 jack on the top of the unit. I decided to go ahead and give the whole unit a closer look and to replace the SO-239 jack.
Replacement of the SO-239 connector requires removal of the main PCB, which in turn requires desoldering of the two pushbutton switches and the BNC jack on the unit’s upper surface. The SO-239 itself is connected to the main PCB in an unusual fashion. The center pin of the SO-239, when the main PCB is in place, sits about an eighth of an inch above the PCB. That gap is simply filled with solder at the factory. Each of the two mounting screws used for the SO-239 has a solder lug installed under its nut. The lugs are then bent over to reach the main PCB and are soldered to pads on the PCB. These solder lugs also do not quite reach the board surface, and so their gaps are also solder-filled in production (Figure 3). Large solder bridges of this type are prone to cracking with time, a condition with which I was not happy. I therefore decided to correct this as well.
Another poor manufacturing technique, in my view, was the manner in which the BNC jack and the pushbutton switches were connected. The two pushbutton switches are normally-open switches that, when pressed, connect their respective circuits to ground. The way that MFJ chose to implement this was to bend one solder lug of each switch over and solder them to the solder lug under the nut on the BNC jack (also shown in Figure 3). It was a stretch at best, and it put undue stress on the bodies of the pushbutton switches. As it turned out, when I removed these switches, I found that the bodies of both switches were cracked. Solution? Two new switches… which turned out to be an adventure in and of itself.
I installed the new SO-239 to the enclosure. Then, I went over the main and display PCB’s carefully, touching up any solder joints that looked the least bit suspicious. I then installed the main PCB to the enclosure, and I added lengths of bus wire between the mainboard solder pads and the SO-239 center pin and also at the solder lugs on its mounting screws (Figure 4). Next, I installed the BNC jack and the two pushbutton switches, wiring them up to the main PCB as they were originally. I added some bus wire to connect the grounded sides of the pushbutton switches to the BNC jack ground lug to make it a more comfortable fit. Now for the moment of truth.
I connected the battery banks (there are two of them) and powered up the unit, only to find that the LCD panel was not working. Now what? Did I damage the LCD panel in doing my solder touch-ups? I did not think so, but I went ahead and removed the main PCB again so that I could inspect the display PCB carefully. As luck would have it, I found nothing wrong there.
I sat back and thought about it a little bit, and then I decided to eliminate possibilities by testing the unit operation at each step of assembly. I installed the main PCB and checked the LCD operation, finding that it worked normally. I connected the SO-239 jack and again checked the LCD operation, and it worked just fine, which makes sense, as the jack was open.
So, next I wired up the BNC jack, and as expected (as this jack too was open), the LCD operated as it was meant to. I then connected the first of the two pushbutton switches, the one labeled “GATE”. Once again, the LCD panel worked normally. Finally, a bit confused, I connected the “INPUT” pushbutton switch. Of course, now the LCD panel did not work.
As mentioned earlier, the pushbutton switches are normally-open switches, so connecting that last switch should not have made any difference, but it did… which meant that the switch was obviously not open! I checked the switch with an ohmmeter, and sure enough, it was a normally-closed switch that had somehow gotten mixed in with my supply of normally-open switches. Swapping out that switch for another (verified NO) switch from my stock solved the problem (Figures 5 & 6).
The lesson to be learned from this repair is actually a dual lesson.
When things don’t work out the way that you expect them to, think it through and carefully go back over what you have done and especially any changes that you have made.
A thorough search will usually turn up the culprit.
See you next month!
I installed the new SO-239 to the enclosure. Then, I went over the main and display PCB’s carefully, touching up any solder joints that looked the least bit suspicious. I then installed the main PCB to the enclosure, and I added lengths of bus wire between the mainboard solder pads and the SO-239 center pin and also at the solder lugs on its mounting screws (Figure 4). Next, I installed the BNC jack and the two pushbutton switches, wiring them up to the main PCB as they were originally. I added some bus wire to connect the grounded sides of the pushbutton switches to the BNC jack ground lug to make it a more comfortable fit. Now for the moment of truth.
I connected the battery banks (there are two of them) and powered up the unit, only to find that the LCD panel was not working. Now what? Did I damage the LCD panel in doing my solder touch-ups? I did not think so, but I went ahead and removed the main PCB again so that I could inspect the display PCB carefully. As luck would have it, I found nothing wrong there.
I sat back and thought about it a little bit, and then I decided to eliminate possibilities by testing the unit operation at each step of assembly. I installed the main PCB and checked the LCD operation, finding that it worked normally. I connected the SO-239 jack and again checked the LCD operation, and it worked just fine, which makes sense, as the jack was open.
So, next I wired up the BNC jack, and as expected (as this jack too was open), the LCD operated as it was meant to. I then connected the first of the two pushbutton switches, the one labeled “GATE”. Once again, the LCD panel worked normally. Finally, a bit confused, I connected the “INPUT” pushbutton switch. Of course, now the LCD panel did not work.
As mentioned earlier, the pushbutton switches are normally-open switches, so connecting that last switch should not have made any difference, but it did… which meant that the switch was obviously not open! I checked the switch with an ohmmeter, and sure enough, it was a normally-closed switch that had somehow gotten mixed in with my supply of normally-open switches. Swapping out that switch for another (verified NO) switch from my stock solved the problem (Figures 5 & 6).
The lesson to be learned from this repair is actually a dual lesson.
- First, I should have done a more complete job on this unit the first time around, before I put it on the Club’s test and repair bench.
- Second, and more to the point, remember that each and every “repair” that is made can actually introduce a previously non-existing problem.
When things don’t work out the way that you expect them to, think it through and carefully go back over what you have done and especially any changes that you have made.
A thorough search will usually turn up the culprit.
See you next month!
Henry 1KD-5 Amplifier - January 2023
Let me start out this month’s case history with an apology. No repair should take as long as this one (and one other, to be discussed in another article) did. There is no real excuse other than that the job was a bear to do, and I kind of dragged my feet on digging into the guts of this thing. I am talking about the Henry Radio 1KD-5 HF linear amplifier. This was a circa 1977 model, heavier than you can believe, with a one-tube grounded-grid circuit. The tube is a PL3-500ZG tube of about four and a half inches diameter, nestled inside an external glass bell chimney. The tube socket is buried deep inside the unit, behind a board that carries the tuning coils for the amplifier.
I am getting ahead of myself. Let’s start at the beginning. The owner brought this unit to me, explaining that the tube would light, and then go out, then light again, and then go out, and would repeat this behavior while switched on. He also told me that he was in no hurry to get it back.
I set up my 30A 230V outlet with the correct receptacle to match the Henry’s power cord, and fired it up to confirm the reported behavior. It took just about a minute or so before the on/off action became evident, so I set out to find the cause. As it turned out, that was the easy part. Some gentle pressure on tube while it was out would cause it to light up again.
The problem was that the tube socket, a humongous ceramic thing about three inches square and about three-eighths of an inch thick, had fatigued with age and the effects of heat. The result was that the contacts that grip the tube pins had relaxed quite a bit - enough so that when they got hot, the circuit would open until they cooled down, at which time the circuit would close and the process would repeat. Solution? A new tube socket.
I tracked down a source for the socket, but I had to wait for the socket to come in from China, and I had to order two of them at an exorbitant price to get the one that I needed. I buttoned up the amp and set it aside to wait for the part to come in.
Let me start out this month’s case history with an apology. No repair should take as long as this one (and one other, to be discussed in another article) did. There is no real excuse other than that the job was a bear to do, and I kind of dragged my feet on digging into the guts of this thing. I am talking about the Henry Radio 1KD-5 HF linear amplifier. This was a circa 1977 model, heavier than you can believe, with a one-tube grounded-grid circuit. The tube is a PL3-500ZG tube of about four and a half inches diameter, nestled inside an external glass bell chimney. The tube socket is buried deep inside the unit, behind a board that carries the tuning coils for the amplifier.
I am getting ahead of myself. Let’s start at the beginning. The owner brought this unit to me, explaining that the tube would light, and then go out, then light again, and then go out, and would repeat this behavior while switched on. He also told me that he was in no hurry to get it back.
I set up my 30A 230V outlet with the correct receptacle to match the Henry’s power cord, and fired it up to confirm the reported behavior. It took just about a minute or so before the on/off action became evident, so I set out to find the cause. As it turned out, that was the easy part. Some gentle pressure on tube while it was out would cause it to light up again.
The problem was that the tube socket, a humongous ceramic thing about three inches square and about three-eighths of an inch thick, had fatigued with age and the effects of heat. The result was that the contacts that grip the tube pins had relaxed quite a bit - enough so that when they got hot, the circuit would open until they cooled down, at which time the circuit would close and the process would repeat. Solution? A new tube socket.
I tracked down a source for the socket, but I had to wait for the socket to come in from China, and I had to order two of them at an exorbitant price to get the one that I needed. I buttoned up the amp and set it aside to wait for the part to come in.
Fast-forward a few months. I have the part in hand, and I finally put the Henry back on the bench. Major disassembly of the unit was required to enable access to the tube socket. I removed the glass chimney and the tube and set them aside for safe-keeping. The chimney is probably irreplaceable at this point, and the tube runs anywhere from two to four hundred dollars, depending on availability and seller. I did not want anything to happen to them!
After removal of the sheet metal covers and shields, I had to laboriously remove the forced-air cooling system fan and motor. Next, it was necessary to dismount the tuning coil board and carefully move it out of the way. A large toroidal transformer was next to be removed for access to the tube socket, which had two of its heavy wire leads soldered to the tube socket terminals. My 240-watt soldering gun was required to desolder these connections. Now I was able to get to the tube socket and ground lug mounting hardware and remove the machine screws, lock washers, and nuts. Finally, again using my 240-watt gun, I was able to desolder the capacitors from the connecting tabs of the tube socket and lift the socket out.
At the solder station, I moved the ground lugs from the old tube socket to the new one. I also drilled the tube socket solder lugs as necessary for the heavy wire from the toroidal transformer to fit. Then it was time to reassemble the whole shooting match, which was quite a tedious task due to hardware locations and difficulty in reaching some of the screws to install lock washers and nuts on them. I finally got the tube socket mounted, and then soldered its capacitor connections in place. I reinstalled the toroidal transformer and soldered its leads to the tube socket.
Reassembly of the rest was the reverse of the disassembly procedure, with the exception that I replaced many of the sheet metal screws due to their holes having been stripped or worn oversized.
After final reassembly, it was time to test and align the amplifier, which went exactly according the manual instructions with no surprises. All in all, it was a rewarding repair, though I could never charge the owner the full amount of time spent on the unit.
Sometimes, repairs are just tedious replacement of connecting parts rather than active or even passive components. This was one of those times. None the less, it was a necessary repair in order to bring the amplifier back to operational status.
See you next month!
After removal of the sheet metal covers and shields, I had to laboriously remove the forced-air cooling system fan and motor. Next, it was necessary to dismount the tuning coil board and carefully move it out of the way. A large toroidal transformer was next to be removed for access to the tube socket, which had two of its heavy wire leads soldered to the tube socket terminals. My 240-watt soldering gun was required to desolder these connections. Now I was able to get to the tube socket and ground lug mounting hardware and remove the machine screws, lock washers, and nuts. Finally, again using my 240-watt gun, I was able to desolder the capacitors from the connecting tabs of the tube socket and lift the socket out.
At the solder station, I moved the ground lugs from the old tube socket to the new one. I also drilled the tube socket solder lugs as necessary for the heavy wire from the toroidal transformer to fit. Then it was time to reassemble the whole shooting match, which was quite a tedious task due to hardware locations and difficulty in reaching some of the screws to install lock washers and nuts on them. I finally got the tube socket mounted, and then soldered its capacitor connections in place. I reinstalled the toroidal transformer and soldered its leads to the tube socket.
Reassembly of the rest was the reverse of the disassembly procedure, with the exception that I replaced many of the sheet metal screws due to their holes having been stripped or worn oversized.
After final reassembly, it was time to test and align the amplifier, which went exactly according the manual instructions with no surprises. All in all, it was a rewarding repair, though I could never charge the owner the full amount of time spent on the unit.
Sometimes, repairs are just tedious replacement of connecting parts rather than active or even passive components. This was one of those times. None the less, it was a necessary repair in order to bring the amplifier back to operational status.
See you next month!
Kenwood TM-241A 2M Transceiver - December 2022
Every now and then, a repair comes along that is both easy and difficult at the same time. This month’s repair case history is one of those occasions. This is the story of a simple - and not so simple - repair of a Kenwood TM-241A fifty-watt 2-meter mobile transceiver.
The radio came to me with the complaint of being inoperative on transmit, which was easily verified with a simple output test into my Bird 43 directional wattmeter and a dummy load. The Bird 43 showed zero output power from the radio. During this test, however, I also noted that the unit failed to maintain its last-used settings, which told me that there was a second problem with the radio, and therefore the need for some deeper troubleshooting.
Armed with a TM-241A service manual and schematic, I set out to isolate the output power problem first. It took only a few minutes with an oscilloscope to determine that the signal was present at the input of the final amplifier, but that there was no output from that amplifier stage. A quick check of the power supply voltages to the final amp IC (Kenwood calls this the power module) showed that the operating voltages were correct, meaning that the IC was most likely a failed device. A quick online search showed that the power module, a Toshiba S-AV17, was available from many sources, including East Coast Transistor, an authorized Kenwood parts distributor. In the interest of sticking with original factory replacement parts, I ordered the IC from ECT and waited for it to come in.
Before ordering the IC, I went ahead and checked out the most likely cause of the radio failing to store any settings - a failed memory “keep-alive” battery. Kenwood did not make it very easy to replace this battery, which is a CR2032 coin cell with an insulating outer ring and welded tabs for connection to the printed circuit board. When installed, this coin cell is sandwiched between two insulators, one of which is double-sided adhesive foam which is used to affix the coin cell to the PCB.
Every now and then, a repair comes along that is both easy and difficult at the same time. This month’s repair case history is one of those occasions. This is the story of a simple - and not so simple - repair of a Kenwood TM-241A fifty-watt 2-meter mobile transceiver.
The radio came to me with the complaint of being inoperative on transmit, which was easily verified with a simple output test into my Bird 43 directional wattmeter and a dummy load. The Bird 43 showed zero output power from the radio. During this test, however, I also noted that the unit failed to maintain its last-used settings, which told me that there was a second problem with the radio, and therefore the need for some deeper troubleshooting.
Armed with a TM-241A service manual and schematic, I set out to isolate the output power problem first. It took only a few minutes with an oscilloscope to determine that the signal was present at the input of the final amplifier, but that there was no output from that amplifier stage. A quick check of the power supply voltages to the final amp IC (Kenwood calls this the power module) showed that the operating voltages were correct, meaning that the IC was most likely a failed device. A quick online search showed that the power module, a Toshiba S-AV17, was available from many sources, including East Coast Transistor, an authorized Kenwood parts distributor. In the interest of sticking with original factory replacement parts, I ordered the IC from ECT and waited for it to come in.
Before ordering the IC, I went ahead and checked out the most likely cause of the radio failing to store any settings - a failed memory “keep-alive” battery. Kenwood did not make it very easy to replace this battery, which is a CR2032 coin cell with an insulating outer ring and welded tabs for connection to the printed circuit board. When installed, this coin cell is sandwiched between two insulators, one of which is double-sided adhesive foam which is used to affix the coin cell to the PCB.
Accessing the battery is the not-so-easy part and involves removal of the front bezel of the radio, followed by the removal of a metal structural cover, and finally the front panel display unit printed circuit board. At this point, the battery voltage can be measured easily. When measured in-circuit, the coin cell showed a voltage of only 0.36 volts. With the battery basically “dead”, it was necessary to continue the disassembly. To do so, the main front panel PCB is removed from the chassis to allow access to the coin cell, which is mounted between this PCB and the main chassis. Care must be taken when de-soldering the coin cell so as not to overheat and damage the PCB.
An important point is to be certain to use JIS screwdrivers for this job, especially for the tiny screws that secure the metal front structure to the main chassis. It is extremely easy to strip the heads of these screws if the wrong screwdriver is used. Polarity alignment of the coin cell is aided by indications on the PCB referring to the + and - terminal connect points.
I ordered the coin cell from East Coast Transistor in the same order as the power module, and then I sat back and waited for the parts to come in. Delivery took eight business days. The parts arrived well-packaged and in good condition, though they had to travel via ground transportation due to the fact that the coin cell is a lithium battery and thus falls under certain transportation restrictions.
Installation of the coin cell and reassembly of the front panel was basically a reversal of the disassembly process. I noted that the control pushbutton extenders have a tendency to fall out when reassembling the unit. Apart from that hiccup, it is a straightforward process.
Installation of the power module, on the other hand, required removal of the main PCB from the radio chassis. I had elected not to remove this board until the new parts arrived, primarily so that the removal procedure would be fresh in my mind when it came to reassembly time.
I had taken several photographs prior to disassembly, which is a standard practice for me. This provides a reference for reassembly. In this case, it helped me to resolve a puzzle in that there is one plug with seven wires for which I could not seem to find the connect point. For several minutes, I struggled with trying to remember disconnecting the plug, but I simply did not remember unplugging it. Finally, by referring back to my photos, I realized that this is a plug that goes nowhere. It was simply hanging free underneath the loudspeaker behind the front panel. The other end of this harness is a seven-wire plug that connects to the front panel PCB.
Removing the PCB is not complex at all, and replacement of the power module on the PCB requires the normal care about excessive heat. Be aware that there are two mounting tabs on the S-AV17, which are secured to the rear of the chassis via machine screws, thus providing heat sinking for the IC. When reinstalling the PCB with the new power module, be sure to coat the rear surface of the IC with silicone thermal transfer grease for best heat transfer to the chassis. Again, be sure to use a JIS screwdriver for this task as well.
After reassembly was completed, it was time to test the operation of the repaired unit. The first thing that I checked was the ability of the radio to “remember” the last used settings. This was no problem; all worked as expected. Next up was the power output test. When tested with my faithful Bird 43 into a dummy load, the radio showed an output of >47 watts into a dummy load.
While the customer had made no mention of the settings memory issue, I would not have considered the radio to have been repaired completely if the battery had not been replaced. Had the customer squawked about the additional and not requested repair expense, I would probably have attempted to work out a parts/labor split with the customer for that specific part of the repair bill. As it turned out, the customer was satisfied with the overall repair and its cost as presented.
The moral of the story here is that there is often more to repair than just what the customer reports. A thorough repair tech will go the extra mile, though it is usually best to discuss any additional repairs with the radio’s owner before proceeding with those additional repair items.
See you next month…
An important point is to be certain to use JIS screwdrivers for this job, especially for the tiny screws that secure the metal front structure to the main chassis. It is extremely easy to strip the heads of these screws if the wrong screwdriver is used. Polarity alignment of the coin cell is aided by indications on the PCB referring to the + and - terminal connect points.
I ordered the coin cell from East Coast Transistor in the same order as the power module, and then I sat back and waited for the parts to come in. Delivery took eight business days. The parts arrived well-packaged and in good condition, though they had to travel via ground transportation due to the fact that the coin cell is a lithium battery and thus falls under certain transportation restrictions.
Installation of the coin cell and reassembly of the front panel was basically a reversal of the disassembly process. I noted that the control pushbutton extenders have a tendency to fall out when reassembling the unit. Apart from that hiccup, it is a straightforward process.
Installation of the power module, on the other hand, required removal of the main PCB from the radio chassis. I had elected not to remove this board until the new parts arrived, primarily so that the removal procedure would be fresh in my mind when it came to reassembly time.
I had taken several photographs prior to disassembly, which is a standard practice for me. This provides a reference for reassembly. In this case, it helped me to resolve a puzzle in that there is one plug with seven wires for which I could not seem to find the connect point. For several minutes, I struggled with trying to remember disconnecting the plug, but I simply did not remember unplugging it. Finally, by referring back to my photos, I realized that this is a plug that goes nowhere. It was simply hanging free underneath the loudspeaker behind the front panel. The other end of this harness is a seven-wire plug that connects to the front panel PCB.
Removing the PCB is not complex at all, and replacement of the power module on the PCB requires the normal care about excessive heat. Be aware that there are two mounting tabs on the S-AV17, which are secured to the rear of the chassis via machine screws, thus providing heat sinking for the IC. When reinstalling the PCB with the new power module, be sure to coat the rear surface of the IC with silicone thermal transfer grease for best heat transfer to the chassis. Again, be sure to use a JIS screwdriver for this task as well.
After reassembly was completed, it was time to test the operation of the repaired unit. The first thing that I checked was the ability of the radio to “remember” the last used settings. This was no problem; all worked as expected. Next up was the power output test. When tested with my faithful Bird 43 into a dummy load, the radio showed an output of >47 watts into a dummy load.
While the customer had made no mention of the settings memory issue, I would not have considered the radio to have been repaired completely if the battery had not been replaced. Had the customer squawked about the additional and not requested repair expense, I would probably have attempted to work out a parts/labor split with the customer for that specific part of the repair bill. As it turned out, the customer was satisfied with the overall repair and its cost as presented.
The moral of the story here is that there is often more to repair than just what the customer reports. A thorough repair tech will go the extra mile, though it is usually best to discuss any additional repairs with the radio’s owner before proceeding with those additional repair items.
See you next month…
ICOM IC-706 HF/6M/2M Transceiver - November 2022
Sometimes you wish that the customer would just be honest with you and tell you what really happened, and this month’s At the Repair Bench is an example of one of those times. It all began with a phone call from a gentleman out in western Pennsylvania. I should have realized that something was wonky when he couldn’t tell me who it was that referred him to me - or maybe he wouldn’t say. Anyway, he asked if he could ship his faithful Icom® IC-706 to me for repair, saying only that the front panel was “dead”. Naturally, I agreed to look at it, so he shipped it in.
He did an over-the-top job of packing the radio and mic, going so far as to buy some Lowe’s sheet foam and cut custom blocks to surround the radio, and then gluing the blocks together to make two half shells that fit the radio quite well, and also fit the carton perfectly. Kudos on that part! He lost some points, however, when I got into the repair… but I am getting ahead of myself.
After unpacking the radio, I put it on the bench and connected it to my power supply and dummy load, and powered it on… or at least I tried to power it on. Nothing happened. The unit was stone cold dead and unresponsive. I took the cover screws out and lifted the top cover, and I saw immediately what the problem was.
The Icom® IC-706 has a removable front panel, which connects behind the panel to a set of eight spring contacts, which in turn connect to the main PCB via a “flex circuit” or Kapton cable. Connection to the main PCB is made through the use of a top-entry edge connector that is surface-mount soldered to the main PCB. This connector was off the PCB and floating free inside the radio, tethered to the end of the Kapton cable.
Here is the part where the owner lost points… someone had been inside the radio and most likely pulled that connector off the board. How do I know this? Simple… the speaker connection (the speaker is mounted to the top cover) was unplugged.
Sometimes you wish that the customer would just be honest with you and tell you what really happened, and this month’s At the Repair Bench is an example of one of those times. It all began with a phone call from a gentleman out in western Pennsylvania. I should have realized that something was wonky when he couldn’t tell me who it was that referred him to me - or maybe he wouldn’t say. Anyway, he asked if he could ship his faithful Icom® IC-706 to me for repair, saying only that the front panel was “dead”. Naturally, I agreed to look at it, so he shipped it in.
He did an over-the-top job of packing the radio and mic, going so far as to buy some Lowe’s sheet foam and cut custom blocks to surround the radio, and then gluing the blocks together to make two half shells that fit the radio quite well, and also fit the carton perfectly. Kudos on that part! He lost some points, however, when I got into the repair… but I am getting ahead of myself.
After unpacking the radio, I put it on the bench and connected it to my power supply and dummy load, and powered it on… or at least I tried to power it on. Nothing happened. The unit was stone cold dead and unresponsive. I took the cover screws out and lifted the top cover, and I saw immediately what the problem was.
The Icom® IC-706 has a removable front panel, which connects behind the panel to a set of eight spring contacts, which in turn connect to the main PCB via a “flex circuit” or Kapton cable. Connection to the main PCB is made through the use of a top-entry edge connector that is surface-mount soldered to the main PCB. This connector was off the PCB and floating free inside the radio, tethered to the end of the Kapton cable.
Here is the part where the owner lost points… someone had been inside the radio and most likely pulled that connector off the board. How do I know this? Simple… the speaker connection (the speaker is mounted to the top cover) was unplugged.
The repair was simple enough. Fortunately, no damage was done to the PCB - all of the pads were intact and in fact had plenty of solder on them. All I had to do was to reflow the solder on the connector pins once I put the connector in position. Of course, I had to remove the FL-100 CW Narrow Filter and the FL-223 SSB Narrow Filter to allow clear work access to the connector location on the PCB. The Kapton cable itself was unhurt, so after I resoldered the connector in place, I was able to simply re-insert the Kapton cable into the connector slot.
Was it embarrassment? Was it ignorance? Who knows? All that I know is that the radio performed properly once the repair was made, and I repeated the inbound packing job for the outbound trip back to the owner. A simple repair with a nebulous cause… but one thing is certain. That connector most likely did not fall off by itself.
I would much rather have the customer tell me the truth as to what is going on when a unit comes in for repair, as it takes a lot of the guesswork out of the equation. See you next month!
Was it embarrassment? Was it ignorance? Who knows? All that I know is that the radio performed properly once the repair was made, and I repeated the inbound packing job for the outbound trip back to the owner. A simple repair with a nebulous cause… but one thing is certain. That connector most likely did not fall off by itself.
I would much rather have the customer tell me the truth as to what is going on when a unit comes in for repair, as it takes a lot of the guesswork out of the equation. See you next month!
Heathkit® HP-23B Power Supply - October 2022
Every now and then, I will come across a repair that should have been avoidable with proper equipment maintenance. Unfortunately, some maintenance is beyond the skill set of the equipment owner. This month’s repair is just such a repair.
The Heathkit® HP-23B is a multi-output power supply used in conjunction with several of that company’s ham radio equipment offerings. The PSU provides outputs of 700VDC at 250mA, 350VDC at 150mA, 250VDC at 100mA, -100VDC at 20mA, and 12.6VAC at 5.5A. The incoming power is a standard 120VAC at about 350 watts. The unit is heavy, weighing in at about sixteen pounds.
Every now and then, I will come across a repair that should have been avoidable with proper equipment maintenance. Unfortunately, some maintenance is beyond the skill set of the equipment owner. This month’s repair is just such a repair.
The Heathkit® HP-23B is a multi-output power supply used in conjunction with several of that company’s ham radio equipment offerings. The PSU provides outputs of 700VDC at 250mA, 350VDC at 150mA, 250VDC at 100mA, -100VDC at 20mA, and 12.6VAC at 5.5A. The incoming power is a standard 120VAC at about 350 watts. The unit is heavy, weighing in at about sixteen pounds.
This particular HP-23B came to me with the complaint that it would repeatedly trip the chassis-mounted 2.92-ampere circuit breaker. The owner would press the reset button, and almost immediately it would trip out again. This behavior led me to believe that there was either a dead short circuit somewhere, or a condition that would mimic a short circuit very closely. Time for some detective work.
The circuit breaker is installed in the power transformer primary winding circuit, so I started out by applying some judicious use of the ohmmeter to the primary circuit, only to find that all was as it should be. No problem there, so it was off to the secondary side.
I decided to eliminate the simplest circuit first, which is the 12.6VAC output. This circuit is simply taken from an isolated secondary winding and carried to the output plug as the two secondary leads from the winding - no additional components. There was no short circuit there, and the winding resistance was reasonable. I moved on to the DC outputs.
The three DC output circuits are easily isolated by opening a single wire lead in each circuit, which would then allow for resistance readings to ground at various points in those circuits. It did not take very long to identify an “almost” shorted 125µF filter capacitor in the medium/low voltage output circuit. This capacitor had extremely high leakage and would obviously require replacement.
I next removed and bench-tested all of the electrolytic capacitors in the unit, and I found relatively high leakage in three of the four 125µF filter capacitors and in one of the 40µF electrolytics used in the -100VDC bias circuit.
|
There is a company called Hayseed Hamfest (www.hayseedhamfest.com) who provides re-cap kits for this power supply. The beauty of their kit is that the unit retains its original appearance, though it functions like brand new. The kit is offered in multiple formats - either with or without the smaller capacitors, and in standard or in increased working voltage versions. I ordered up the standard voltage kit in the complete (all capacitors) version and sat back and waited for it to come in. |
The installation of the capacitors was a straightforward repair, as all of the parts are intended to fit exactly in place of the originals so as to preserve the factory appearance of the unit. Post-repair testing showed all to be functional and the voltages to be at the manual specified levels. I wrapped and boxed the PSU and shipped it back to the owner (after he paid my bill, of course!)
This put another one in the “WIN” column, but it did reveal an important point. When it comes to older electronic equipment, periodic maintenance should probably include at least the testing of, if not the actual replacement of, any and all capacitors that are likely to age poorly. This obviously includes filter capacitors, as they do a huge part of the job when making clean DC from the transformed AC supply.
See you next month!
Simpson 260 Series 5 Analog VOMM - September 2022
A few weeks ago, I received a carton in the mail, with a plea for help tucked into the carton alongside a Simpson 260 Series 5 analog VOMM. (Yes - VOMM is correct in this case, as the meter is a volts, ohms, and milliamperes meter.) The owner wrote that it had quit working in all modes and he had no idea why. Of course, I was up for the challenge, and it turned out to be quite interesting.
I first verified that there was no response in the meter on any function or scale. I then took off the rear cover - four screws and it was off. The first thing that I noticed was that there was no battery installed for the ohmmeter function. The 260 uses a total of five cells – four “AA” cells and one “D” cell to power the ohmmeter. Naturally, I installed a set of cells and tested the ohmmeter function again, to find that it was still inoperative.
A few weeks ago, I received a carton in the mail, with a plea for help tucked into the carton alongside a Simpson 260 Series 5 analog VOMM. (Yes - VOMM is correct in this case, as the meter is a volts, ohms, and milliamperes meter.) The owner wrote that it had quit working in all modes and he had no idea why. Of course, I was up for the challenge, and it turned out to be quite interesting.
I first verified that there was no response in the meter on any function or scale. I then took off the rear cover - four screws and it was off. The first thing that I noticed was that there was no battery installed for the ohmmeter function. The 260 uses a total of five cells – four “AA” cells and one “D” cell to power the ohmmeter. Naturally, I installed a set of cells and tested the ohmmeter function again, to find that it was still inoperative.
I began a more thorough examination of the meter componentry, looking for burned components or broken wire solder points. What I found instead was quite surprising, and goes to show that you cannot always believe what people say. A close inspection revealed that the PCB on which most of the meter’s components are installed was cracked along its left (from the rear) side, about an inch in from the edge of the board and at an angle from the outer corner towards the center.
I removed the PCB to examine the opposite (foil) side, and found that five traces were broken along the crack. This might turn out to be a simple repair. I began by applying some cyanoacrylate glue to the crack to strengthen the board. When the glue had cured, I simply solder-bridged the cracks in the foil traces, a task made easier by the fact that the traces were solder-covered. I re-installed the “AA” and “D” cells, and tested the meter. Full operation was restored! I did some cleaning of the switches and pots inside the meter with some DeoxIT® Gold, cleaned up the exterior, and secured the back to the meter assembly.
The meter’s folding handle was quite misshapen (read : bent). I decided to remove it and repair it. The handle is secured by a shoulder bolt on either side of the case, so I removed those bolts. The handle itself is a sandwich of metal encased by a plastic covering, making it a simple task to straighten the handle completely, and then to re-bend it to its proper contour. I then re-installed the handle and the job was done.
I do not know how the PCB got broken, but it is quite obvious to me that the unit had been dropped at some point in its history, based upon the way the handle was bent. I also have a hard time believing that the owner was unaware of the broken PCB, especially as he had removed the battery for shipping the meter. He also did not take any care in packing the meter for shipment – he simply stuck it in a carton with its test leads, but with no wrapping or packing at all, leaving the meter free to bounce around in the carton. Needless to say, it did NOT go back to him the same way.
I removed the PCB to examine the opposite (foil) side, and found that five traces were broken along the crack. This might turn out to be a simple repair. I began by applying some cyanoacrylate glue to the crack to strengthen the board. When the glue had cured, I simply solder-bridged the cracks in the foil traces, a task made easier by the fact that the traces were solder-covered. I re-installed the “AA” and “D” cells, and tested the meter. Full operation was restored! I did some cleaning of the switches and pots inside the meter with some DeoxIT® Gold, cleaned up the exterior, and secured the back to the meter assembly.
The meter’s folding handle was quite misshapen (read : bent). I decided to remove it and repair it. The handle is secured by a shoulder bolt on either side of the case, so I removed those bolts. The handle itself is a sandwich of metal encased by a plastic covering, making it a simple task to straighten the handle completely, and then to re-bend it to its proper contour. I then re-installed the handle and the job was done.
I do not know how the PCB got broken, but it is quite obvious to me that the unit had been dropped at some point in its history, based upon the way the handle was bent. I also have a hard time believing that the owner was unaware of the broken PCB, especially as he had removed the battery for shipping the meter. He also did not take any care in packing the meter for shipment – he simply stuck it in a carton with its test leads, but with no wrapping or packing at all, leaving the meter free to bounce around in the carton. Needless to say, it did NOT go back to him the same way.
NanoVNA - August 2022
Fairly recently, another member – Rich Subers W2RHS – and I entered into a complex trade agreement wherein he would give me an unbuilt MFJ antenna tuner kit for me to build, and in exchange, I would replace his failed NanoVNA with a new and slightly larger one. Rich threw in the failed NanoVNA, so I figured I would give it a try to see if I could repair it.
This particular NanoVNA is encased in a multi-piece 3-D printed plastic enclosure, which does a good job of protecting the unit. It would also serve to keep things in place post-repair. Rich had told me that the unit worked, even though there was no display on the screen, as he could connect it to his phone or PC and use the functions of the NanoVNA with no trouble via the software. I suspected that the problem was in the display backlight wiring.
We were fairly sure that the problem was a bad solder joint underneath the display, which was attached to the main PCB with some strong adhesive. The first question was whether or not I could successfully separate the display and the main board. I tried using some monofilament line to cut the adhesive, but the line kept breaking, Ultimately, I tried using some AWG24 solid copper wire, which did the trick nicely.
Once I had the unit open, I powered it up and starting putting localized pressure on the end of the Kapton cable that connects the display to the main board. There are about twenty individual connections carried in that cable, so I had to determine which ones were faulty. It soon became evident that there were multiple joints open, as pressing on various connections would illuminate different LED’s in the four-LED backlight system.
These wire connections are on a pitch or spacing of about 0.050”, so I chose NOT to attack this job with a soldering iron. Instead, I fired up my hot air reflow gun and heated the area with the hot air while placing light pressure across the entire Kapton cable end. This approach was quite successful, restoring the unit backlight to full operation. The best part was that no undue damage was done to the Kapton cable, and I did not have to worry about solder bridges.
I flipped the display back in place, where the original adhesive bonded back together and held the display tightly. I then reassembled the plastic enclosure and the job was complete. Just for fun, I tried a calibration and then swept some coax, some lamp cord, and a couple of antennas. All worked as it should.
Because Rich had a new unit and did not want this one back, I casually offered it to the first taker on a Tuesday Noonday Net, and it was gone inside of five minutes. Now, another member, Anthony Cerami N2OAC, is the proud owner of a resurrected NanoVNA.
Fairly recently, another member – Rich Subers W2RHS – and I entered into a complex trade agreement wherein he would give me an unbuilt MFJ antenna tuner kit for me to build, and in exchange, I would replace his failed NanoVNA with a new and slightly larger one. Rich threw in the failed NanoVNA, so I figured I would give it a try to see if I could repair it.
This particular NanoVNA is encased in a multi-piece 3-D printed plastic enclosure, which does a good job of protecting the unit. It would also serve to keep things in place post-repair. Rich had told me that the unit worked, even though there was no display on the screen, as he could connect it to his phone or PC and use the functions of the NanoVNA with no trouble via the software. I suspected that the problem was in the display backlight wiring.
We were fairly sure that the problem was a bad solder joint underneath the display, which was attached to the main PCB with some strong adhesive. The first question was whether or not I could successfully separate the display and the main board. I tried using some monofilament line to cut the adhesive, but the line kept breaking, Ultimately, I tried using some AWG24 solid copper wire, which did the trick nicely.
Once I had the unit open, I powered it up and starting putting localized pressure on the end of the Kapton cable that connects the display to the main board. There are about twenty individual connections carried in that cable, so I had to determine which ones were faulty. It soon became evident that there were multiple joints open, as pressing on various connections would illuminate different LED’s in the four-LED backlight system.
These wire connections are on a pitch or spacing of about 0.050”, so I chose NOT to attack this job with a soldering iron. Instead, I fired up my hot air reflow gun and heated the area with the hot air while placing light pressure across the entire Kapton cable end. This approach was quite successful, restoring the unit backlight to full operation. The best part was that no undue damage was done to the Kapton cable, and I did not have to worry about solder bridges.
I flipped the display back in place, where the original adhesive bonded back together and held the display tightly. I then reassembled the plastic enclosure and the job was complete. Just for fun, I tried a calibration and then swept some coax, some lamp cord, and a couple of antennas. All worked as it should.
Because Rich had a new unit and did not want this one back, I casually offered it to the first taker on a Tuesday Noonday Net, and it was gone inside of five minutes. Now, another member, Anthony Cerami N2OAC, is the proud owner of a resurrected NanoVNA.
|
Heathkit HD-1234 - July 2022
The typical ham wouldn’t usually think of an antenna coax switch as being a repairable item, but sometimes it is - especially when the name “Heathkit® ” is involved. I recently encountered a six-position (four live connections) switch, a Heathkit® HD-1234, that had two dead positions. Its owner had added another antenna, and so needed to use an additional position on the switch. Of course, I decided to give it a shot. This unit has a six-position switch mechanism which connects each of the four live connectors to a common connector in turn as the switch is rotated. The device is of a hexagonal shape, |
with an SO-239 connector on each of five of the sides, and a ground post on the sixth side. The way the unit is designed, when a given position is selected, all of the other positions’ connectors are grounded. The connectors are labeled “1” through “4”, “C”, and “G”. The internal switching mechanism has no physical stop, which means that it can be rotated a full 360° if so desired.
The complaint was that positions “3” and “4” were defunct, with no connection to the common connector or to ground when selected. At first, it seemed like a straight-forward open circuit problem, such as a broken solder joint at each of the non-working connectors. Close examination, however, showed that all of the solder joints were intact. On the off chance that there were hidden defects there, I went ahead and reflowed the solder on all of the connectors, but to no avail. The problem still existed.
I decided that the problem had to be inside the switch itself, so I disassembled the unit, de-soldering all of the connectors from the switch. The switch is a double-sided rotary switch on a ceramic substrate, with a contact disc on either side of the ceramic base, and a fixed brush at each of the connector positions. In its assembled condition, only the ground side of the switch substrate or base is visible; the detent plate at the top conceals the upper active connection disc and brushes.
This meant that I would need to disassemble the switch to get at the upper contact disc. No problem — it is held together by a pair of machine screws with spacers, washers, and nuts. Once the switch was apart, I began to investigate just why there was no continuity at those two switch positions. What I found was a bit of a surprise. The whole problem was a heavy build-up of oxidation on the brush contacts at those two positions. The fix was fairly simple - some cotton swabs, a toothbrush, and some DeoxIT® Gold. Twenty minutes of cleaning on both sides of the ceramic disc, and the switch contacts were operational again. Another ten minutes, and the switch was reassembled and ready to go back into the unit, with a fresh application of DeoxIT® X10S on the shaft and bushing to aid in long-life operation.
I cleaned up all of the parts, including wire-brushing the threads on the SO-239 connectors. Then I re-assembled the entire unit, and soldered the connectors to the switch terminals. Testing with an ohmmeter showed good clean continuity and zero resistance through all positions of the switch. Passing 30 VDC through the switch from common to each output in turn showed zero voltage drop internally in the switch.
So what happened here? Why did only two of the switch positions have this heavy oxidation? As it turns out, the owner has had this switch in service for over thirty-five years, but he has never used anything but switch positions “1” and “2”, and never turned the switch all of the way around the dial - he simply switched it back and forth between the two positions he used. This led to a lack of “scrubbing” at the unused positions, and age and time took over from there.
Moral of the story? Sometimes, it pays to take the long way around. Exercising the switch through its entire range of travel from time to time will help to keep the contacts clean and oxidation free, allowing the switch to perform up to it design specifications. See you next month!
The complaint was that positions “3” and “4” were defunct, with no connection to the common connector or to ground when selected. At first, it seemed like a straight-forward open circuit problem, such as a broken solder joint at each of the non-working connectors. Close examination, however, showed that all of the solder joints were intact. On the off chance that there were hidden defects there, I went ahead and reflowed the solder on all of the connectors, but to no avail. The problem still existed.
I decided that the problem had to be inside the switch itself, so I disassembled the unit, de-soldering all of the connectors from the switch. The switch is a double-sided rotary switch on a ceramic substrate, with a contact disc on either side of the ceramic base, and a fixed brush at each of the connector positions. In its assembled condition, only the ground side of the switch substrate or base is visible; the detent plate at the top conceals the upper active connection disc and brushes.
This meant that I would need to disassemble the switch to get at the upper contact disc. No problem — it is held together by a pair of machine screws with spacers, washers, and nuts. Once the switch was apart, I began to investigate just why there was no continuity at those two switch positions. What I found was a bit of a surprise. The whole problem was a heavy build-up of oxidation on the brush contacts at those two positions. The fix was fairly simple - some cotton swabs, a toothbrush, and some DeoxIT® Gold. Twenty minutes of cleaning on both sides of the ceramic disc, and the switch contacts were operational again. Another ten minutes, and the switch was reassembled and ready to go back into the unit, with a fresh application of DeoxIT® X10S on the shaft and bushing to aid in long-life operation.
I cleaned up all of the parts, including wire-brushing the threads on the SO-239 connectors. Then I re-assembled the entire unit, and soldered the connectors to the switch terminals. Testing with an ohmmeter showed good clean continuity and zero resistance through all positions of the switch. Passing 30 VDC through the switch from common to each output in turn showed zero voltage drop internally in the switch.
So what happened here? Why did only two of the switch positions have this heavy oxidation? As it turns out, the owner has had this switch in service for over thirty-five years, but he has never used anything but switch positions “1” and “2”, and never turned the switch all of the way around the dial - he simply switched it back and forth between the two positions he used. This led to a lack of “scrubbing” at the unused positions, and age and time took over from there.
Moral of the story? Sometimes, it pays to take the long way around. Exercising the switch through its entire range of travel from time to time will help to keep the contacts clean and oxidation free, allowing the switch to perform up to it design specifications. See you next month!

